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34-175-20315

Well Details

Well ID: 34-175-20315
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Country: United States
State: Ohio
County: Wyandot
Municipality: Eden Township
Operator Name: FRANTZ ENTERPRISES LTD.
Well Pad ID:
Farm/Lease Name: WOOD
License Status: Producing
License Date: 1995-05-12
Spud Date: 1995-05-15
Spud Drilling Contractor: LBJ DRILLING
Final Drill Date: 1995-05-17
Well Total Depth: 2380.00 ft
Configuration: Vertical
Latitude: 40.900000
Longitude: -83.120000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1995-05-12 Issued Date 5/12/95 Expired Date Acres 0020000 Tool Type RTA Proposed Formation TREMPEALEAU Proposed Depth Proposed Drill Depth
Original Spud 1995-05-13 PROD. FORM=CPRC
Completed 1995-05-17 PROD. FORM=CPRC
Reached Total Depth 1995-05-17 PROD. FORM=CPRC
CO 1995-06-01 3069 MURNANE JOSEPH M GeoDate 5/12/95
Completion Report Received 1996-01-02 PROD. FORM=CPRC
Construction Permit Expires 1996-05-11 PROD. FORM=CPRC
Change of Owner 2003-08-29 Operator changed from 3069, COLUMBUS OILFIELD EXPL. CO. to 4062, FRANTZ ENTERPRISES LTD.
Record Last Modified 2017-02-15 PROD. FORM=CPRC

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2369 0
2369 0
2369 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1200 Gal 0 TREATED W/1200 GAL ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 COLUMBUS OILFIELD EXPLORATION 0.00 2404.00 199
1996 COLUMBUS OILFIELD EXPLORATION 0.00 2062.00 365
1997 COLUMBUS OILFIELD EXPLORATION 0.00 2005.00 257
1998 COLUMBUS OILFIELD EXPLORATION 0.00 2485.00 250
1999 COLUMBUS OILFIELD EXPLORATION 0.00 1252.00 264
2000 COLUMBUS OILFIELD EXPLORATION 0.00 537.00 310
2001 COLUMBUS OILFIELD EXPLORATION 0.00 777.00 309
2002 COLUMBUS OILFIELD EXPLORATION 0.00 619.00 296
2003 COLUMBUS OILFIELD EXPLORATION 0.00 258.00 168
2004 FRANTZ ENTERPRISES LTD. 0.00 1010.00 180
2006 FRANTZ ENTERPRISES LTD. 0.00 719.00 145
2007 FRANTZ ENTERPRISES LTD. 0.00 793.00 150
2008 FRANTZ ENTERPRISES LTD. 0.00 728.00 300
2009 FRANTZ ENTERPRISES LTD. 0.00 876.00 361
2010 FRANTZ ENTERPRISES LTD. 0.00 876.00 328
2011 FRANTZ ENTERPRISES LTD. 0.00 715.00 300
2012 FRANTZ ENTERPRISES LTD. 0.00 574.00 277
2013 FRANTZ ENTERPRISES LTD. 0.00 733.00 280
2014 FRANTZ ENTERPRISES LTD. 0.00 726.00 300
2015 FRANTZ ENTERPRISES LTD. 0.00 699.00 262
2016 FRANTZ ENTERPRISES LTD. 0.00 141.00 200
2017 FRANTZ ENTERPRISES LTD. 0.00 279.00 365
2018 FRANTZ ENTERPRISES LTD. 0.00 298.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 COLUMBUS OILFIELD EXPLORATION Brine 0 199
1996 COLUMBUS OILFIELD EXPLORATION Brine 1860 365
1997 COLUMBUS OILFIELD EXPLORATION Brine 9405 257
1998 COLUMBUS OILFIELD EXPLORATION Brine 1500 250
1999 COLUMBUS OILFIELD EXPLORATION Brine 580 264
2000 COLUMBUS OILFIELD EXPLORATION Brine 4223 310
2001 COLUMBUS OILFIELD EXPLORATION Brine 927 309
2002 COLUMBUS OILFIELD EXPLORATION Brine 888 296
2003 COLUMBUS OILFIELD EXPLORATION Brine 504 168
2004 FRANTZ ENTERPRISES LTD. Brine 10555 180
2006 FRANTZ ENTERPRISES LTD. Brine 5475 145
2007 FRANTZ ENTERPRISES LTD. Brine 10770 150
2008 FRANTZ ENTERPRISES LTD. Brine 6000 300
2009 FRANTZ ENTERPRISES LTD. Brine 7220 361
2010 FRANTZ ENTERPRISES LTD. Brine 6560 328
2011 FRANTZ ENTERPRISES LTD. Brine 6000 300
2012 FRANTZ ENTERPRISES LTD. Brine 5540 277
2013 FRANTZ ENTERPRISES LTD. Brine 5860 280
2014 FRANTZ ENTERPRISES LTD. Brine 5040 300
2015 FRANTZ ENTERPRISES LTD. Brine 5240 262
2016 FRANTZ ENTERPRISES LTD. Brine 1920 200
2017 FRANTZ ENTERPRISES LTD. Brine 4770 365
2018 FRANTZ ENTERPRISES LTD. Brine 5240 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1081459827 2002-10-16 0:00 PW No Violations
-1096348694 2014-9-16 0:00: PW No Violations
-1131870684 2002-2-5 0:00:0 PW No Violations
-1361100327 2014-9-16 0:00: PW No Violations
-1465679463 2003-9-17 0:00: PW No Violations
-1554875400 2006-1-18 0:00: PL No Violations
-1580278914 2017-6-22 0:00: PW No Violations
-2091143110 2018-6-4 0:00:0 PW No Violations
-470776001 2001-12-11 0:00 PW No Violations
-881057835 2015-8-28 0:00: PW No Violations
0001210i77 2002-02-05 Production Wells Violations Noted Well has pump jack and is capable. Storage tanks have existing violation to be diked as a result of a recent spill. Dike goes 3/4 way around tanks and is not of good soil only sand. Dike needs finished and other material brought in. Mike Murnane is aware of this. Id has faded and not legible, needs remarked.
0001873462 2001-05-15 Production Wells No Violations Spill clean up done. Excavations have been filled and field has been seeded w/agricultural crops.
001229i218 Production Wells No Violations Follow up on dike construction. Dirt has been brought in and put down over the sand.
0013273564 2001-12-19 Production Wells No Violations Chk on clean up of oil spill. Crew on site working on cleaning up water way. Oil has travelled approx 300 yd to the north in a small water way. The crew from the IT Corp. is going to use a vac-truck to pick up the free oil and a trackhoe to remove the
0013573566 2002-01-02 Production Wells No Violations Chk on progress of spill clean up, looks good at this time. No one at the site.
0021873649 2004-11-03 Production Wells No Violations Follow up on dike construction. Dirt has been brought in and put down over the sand.
0023373652 2002-05-01 Production Wells No Violations On site at 2:30 pm. Chk as the result of a complaint by Jeff Richey Wyandot Co Health Dept. It appears that a storage tank has run over. Oil has collected in the dike and has run out to the south of the tanks. Took photos and contacted Columbus Oil F
0023473653 2002-05-09 Production Wells No Violations Chk on the progress of oil spill clean up. Vac-Truck on site, no one around. Clean up started, needs more work. Sill has puddles of oil inside of dike and oil is leaching from the gravel around the south side of the tanks.
0025973661 2002-06-06 Production Wells No Violations Follow up on oil spill clean up. Still has oil in and around the dike that needs to be cleaned up.
0470776001 2001-12-11 Production Wells Violations Noted FOLLOW UP TO NOV # 1210i29 Oil spill happened on Saturday 12/08 . Heater tube in steel 210 Bbl. Tank rusted out allowing apprx. 20 to 30 Bbl. of crude oil to escape onto the ground surface. Tank battery has no dike. Oil traveled west in an open field apprx. 100 ft. in length and 1
0756270418 2005-06-14 Production Wells No Violations Inspect well. Two 210 bbl tanks and a 1000 gallon steel tank. Well is producing.
0876544612 2013-09-10 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard productive well status check. Check well, storage and identification. No change from previous inspection except the operator has posted No Trespassing signs at the storage. Status: ok.
0881057835 2015-08-28 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1021693039 2008-07-28 Production Wells No Violations Operator finishing service on well and put back into production.
1031318628 2002-09-06 Production Wells No Violations Oil still in dike from preveous spill. A pump and a plastic line have been installed on the water tank. Most likely for transporting brine to the injection well. The storage site is in need of further clean up.
1065457337 2001-12-11 Production Wells Violations Noted FOLLOW UP TO NOV # 1210i29 Oil spill happened on Saturday 12/08 . Heater tube in steel 210 Bbl. Tank rusted out allowing apprx. 20 to 30 Bbl. of crude oil to escape onto the ground surface. Tank battery has no dike. Oil traveled west in an open field ap
1081459827 2002-10-16 Production Wells No Violations Inspect Tank battery. Accumulation of oil released inside the diked field. Used and discarded Oil Absorbent pads present on top of dike. Trash and plastic containers thrown in diked area. Overall sloppy site.
1096348694 2014-09-16 Production Wells No Violations Location Information for the Wood #2 (#315). ENTRANCE: Lat. 40.89883 Long. -83.13163 / WELL HEAD: Lat. 40.90137 Long. -83.12444 / CENTER-OF-STORAGE: Lat. 40.89893 Long. -83.131117.
1131870684 2002-02-05 Production Wells Violations Noted FOLLOW UP TO NOV # 1210i77 Well has pump jack and is capable. Storage tanks have existing violation to be diked as a result of a recent spill. Dike goes 3/4 way around tanks and is not of good soil only sand. Dike needs finished and other material brought in. Mike Murnane is aware

Close NOV, New ownership.

1146845801 2009-12-16 Production Wells No Violations Inspect well. Well shut in. rods froze in hole.
1210i29545 2001-12-11 Production Wells No Violations Oil spill happened on Saturday 12/08 . Heater tube in steel 210 Bbl. Tank rusted out allowing apprx. 20 to 30 Bbl. of crude oil to escape onto the ground surface. Tank battery has no dike. Oil traveled west in an open field apprx. 100 ft. in length and 15 ft. wide at the widest point. Two man crew At this time cleaning up spots of free oil with pads. Cleanup needs to continue until all oil removed. Initial notification came thru the Health Dept. , and the Ohio EPA to the Bellefontaine office, I responded after notice from Bellefontaine. Inspector Faust on another spill. Mike Murnane left a message Saturday on Sams recorder. Cleanup of all oil contaminated soils must be done and , the 210 Bbl. tank repaired or replaced. Immediate cleanup and TWO WEEKS from received date an earthen dike of sufficient size must be installed, and tank repairs made. Notice sent certified P 260 031 290.
1210i2954546 2001-12-11 0:00 PW No Violations
1210i77 2002-2-5 0:00:0 PW No Violations
1229i218 PW No Violations
1229i88495 2000-11-16 Production Wells No Violations On site due to a call from Mike Murnane. The tenant farmer was plowing and hit the flow line. Approx. 60 bbl of oil (fluid) leaked out on to the ground. The oil went into a field tile and under the road into a drainage ditch. A trench was dug across the ditch for the oil to run in to. The trench was lined w/a plastic liner. The flow line was repaired. No one on site at this time.
1229i8849510 2000-11-16 0:00 PW No Violations
1229i99493 2000-10-26 Production Wells No Violations Chk on progress of oil spill clean up. Free oil has been picked up and fresh top soil has been put down. Talked to Mike Murnane on 10/25/00 and told him that the Id has faded out and needs to be redone. On 10/20/00 Mike Murnane called and reported that a truck delivering a new storage tank, hit a valve on the bottom of a 100 bbl storage tank, allowing approx. 35bbl of fluid to leak out on to the ground. A Vac-Truck happened to be on site and clean up was started immediately.
1229i9949314 2000-10-26 0:00 PW No Violations
13273564 2001-12-19 0:00 PW No Violations
13573566 2002-1-2 0:00:0 PW No Violations
1361100327 2014-09-16 Production Wells No Violations Inspected the Wood #1 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1362414008 2013-03-04 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard productive well status check. The well is pumping by a black USS oilwell electric powered pump jack and the well pad is clean and free of excess contamination. The complete storage consists of three tanks (#42381, #42382 and #42383) commingled with #299 and #266. The storage complex serves as storage for the disposal well (two plastic brine tanks) for the Goodman #2 (SWIW #2) and is completely surrounded by a 43W x 66L x 30D galvanized steel sided gravel lined dike. The tanks have recently been painted and the identification is not sufficient. Mr. Frantz has new labels and is waiting on weather to attach to the storage tanks.
1378880970 2017-09-21 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1465679463 2003-09-17 Production Wells No Violations Inspect well. Pump jack. Well head covered in oil. ID posted at tanks. Two 100 bbl tanks.
1511544748 2015-04-29 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: pump jack unhooked, out-of-service.
1554875400 2006-01-18 Preliminary Restoration No Violations Update records with Preliminary Restoration. Site ok.
1580278914 2017-06-22 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Status: ok, the well was in operation at the time of inspection.
1643287979 2018-10-25 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection.
1721080438 2019-7-15 0:00: PW No Violations
1804486216 2016-01-20 Preliminary Restoration No Violations The well is in production, preliminary restoration complete.
1873462 2001-5-15 0:00: PW No Violations
2026178493 2007-07-19 Production Wells No Violations Inspect well. Site ok. Well producing during inspection.
2091143110 2018-06-04 Production Wells No Violations Inspected the Wood #2 (#315) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
2132015811 2016-01-20 Production Wells No Violations Inspect well and storage. Status: ok.
21873649 2004-11-3 0:00: PW No Violations
23373652 2002-5-1 0:00:0 PW No Violations
23473653 2002-5-9 0:00:0 PW No Violations
25973661 2002-6-6 0:00:0 PW No Violations
756270418 2005-6-14 0:00: PW No Violations
876544612 2013-9-10 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0001210i77 US-OH-105514 2002-02-05 Failure to legibly identify well
0470776001 US-OH-125104 2001-12-13 Well operation causing pollution and contamination
0470776001 US-OH-125105 2001-12-13 Well insufficiently equipped to prevent escape of oil and gas
1065457337 US-OH-101320 2014-05-05 Well operation causing pollution and contamination
1065457337 US-OH-101321 2014-05-05 Well insufficiently equipped to prevent escape of oil and gas
1131870684 US-OH-103355 2002-02-05 Failure to legibly identify well

For data sources see[9]

References