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34-173-20348

Well Details

Well ID: 34-173-20348
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: LOWTHER CHARLES
License Status: Final Restoration
License Date: 1975-08-15
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.370000
Longitude: -83.670000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Plugged/Abandoned 2015-12-09 NO PREVIOUS RECORD. I&O 2012 05 020
Record Last Modified 2017-05-27 NO PREVIOUS RECORD. I&O 2012 05 020

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1122587582 2015-9-25 0:00: OR No Violations
-1517910237 2015-11-30 0:00 OR No Violations
-1687241086 2015-12-10 0:00 OR No Violations
-1932275154 2012-5-11 0:00: OR No Violations
-248834089 2015-11-16 0:00 OR No Violations
-255671181 2015-9-9 0:00:0 OR No Violations
-312229138 2015-11-4 0:00: OR No Violations
-709425215 2015-10-26 0:00 OR No Violations
-71695635 2015-11-24 0:00 OR No Violations
0071695635 2015-11-24 Orphan No Violations
0248834089 2015-11-16 Orphan No Violations
0255671181 2015-09-09 Orphan No Violations At the time of the inspection I was on location with Bryan Smith and Dave Albrecht of the Division of Real Estate. They were on location to survey the well and I was on location to provide directions and monitor gas levels during the survey. The well was venting Hydrogen Sulfide gas from out the top of the 20 by 8 plastic riser pipe as intended. A faint smell from the gas was evident 20 to 80 south of the well but no gas levels were detected with the Division issued gas detector around the location. Winds were out of the north at 10 mph and the temperature was 78 degrees.
0312229138 2015-11-04 Orphan No Violations At the time of the inspection I was on location with Terry Whitehair, Emergency Operations and Response Regional Manager for an Organizational & Safety Meeting. This meeting is to discuss access through the park and safety concerns for the plugging of the well scheduled for November 16th. Glenn Davis of Glenn Davis Well Service, Mike Przysiecki of the Bowling Green Parks and Recreation Department, Bowling Green Fire Chief Tom Sanderson, Wood County Emergency Management Agency Director Brad Gilbert, along with other representatives of city and county government and first responders were in attendance. A slight odor of Hydrogen Sulfide gas was evident 200 to the east of the well as winds were out of the west at 15 miles per hour. A hand held gas meter was used to attempt determine the levels of Hydrogen Sulfide present but due to high winds all gas has dissipated and no levels were detected. Mobilization for plugging of the well is scheduled to begin on November 16th.
0515791564 2015-11-18 Orphan No Violations On 11-17-
0638578204 2015-11-23 Orphan No Violations

-

0652699949 2015-11-25 Orphan No Violations
0709425215 2015-10-26 Orphan No Violations At the time of the inspection I was on location with Mike Przysiecki of the Bowling Green Parks and Recreation Department to discuss access through the park for the plugging of the well scheduled for November 16th. We also discussed the setup of an Organizational & Safety Meeting scheduled for November 4th. A slight odor of Hydrogen Sulfide gas was evident 100 to the west of the well as winds were out of the east at 12 miles per hour. A hand held gas meter was used to attempt determine the levels of Hydrogen Sulfide present but due to high winds all gas has dissipated and no levels were detected.
0719695063 2015-12-07 Orphan No Violations

-4-

0800485479 2015-08-25 Orphan No Violations At the time of the inspection all risers when the well was discovered were still in place and in the same condition. There was still a small amount of gas leaking from the well and escaping from the top of the riser as designed. A faint odor of Hydrogen Sulfide was detected 50 east of the well but no gas reading were detected at the well or downwind from the well. Winds at the time of the inspection were at 12 mph from the west.
0828501513 2015-12-02 Orphan No Violations


0898713111 2012-05-14 Orphan No Violations At the time of my inspection the Hydrogen Sulfide gas level above the riser was at 10 ppm and at 140 ppm inside the riser. An 8 plastic riser was placed inside the 12 and raised about 15 above grade to help disapate the gas. Also fencing was placed around the well and will be left in place and monitored until plugging arrangements can be made.
0946306891 2015-12-03 Orphan No Violations
1122587582 2015-09-25 Orphan No Violations At the time of the inspection the well was still venting Hydrogen Sulfide gas from out the top of the 20 by 8 plastic riser pipe as intended. A faint smell from the gas was evident 40 to 100 south of the well but no gas levels were detected with the Division issued gas detector around the location. Winds were out of the east at 10 mph and the temperature was 80 degrees.
1337859073 2012-05-04 Orphan No Violations At the time of my inspection I was on site in response to Complaint # 3762. Troy Sonner, City of Bowling Green Engineer, called regarding a dead spot of grass in Simpson Garden Park. The location in question is 15 south of a split rail fence that marks the north boundry of south section of the park. Gas levels of 18 LEL were detected and a metal detector indicated some steel at the location.
1338979112 2015-12-01 Orphan No Violations
1399993777 2014-03-25 Orphan No Violations At the time of the inspection there was a 10 diameter PVC riser placed over the well from its discovery back in 2012. This riser extends to 15 above grade to allow for the venting of the Hydrogen Sulfide gas leaking from the well. There is a 16 x 16 split rail fence around the well that was put in place by the maintenance crew of the park. The winds on this day were approximately 10 mph from the west and a faint odor could be detected approximately 60 to the east.
1448467047 2015-11-20 Orphan No Violations
1450363886 2015-12-04 Orphan No Violations
1450710239 2015-12-08 Orphan No Violations

-3 and has made no oil at any point during the cleanout process. The decision was made to plug the well at this depth using Formation Cementing Services scheduled for 9am on 12-

1486736568 2017-02-10 Final Restoration No Violations At the time of the inspection the Final Restoration had been completed and the area was being used by Simpson Garden Park. The area around the plugged well had established grass and seven new trees were planted around the location. A new cement walkway had been completed by the park in the fall of 2016 where the access lane to the well had been. Final Restoration Passed.
1517910237 2015-11-30 Orphan No Violations
1528406565 2015-12-09 Plug / Plug Back No Violations
1687241086 2015-12-10 Orphan No Violations
1866511636 2012-05-18 Orphan No Violations At the time of my inspection a fence has been placed around the well and an 8 riser was placed inside existing riser and vented 15 feet above grade. No detectable levels of gas in the open air surrounding the well.
1932275154 2012-05-11 Orphan No Violations Well associated with Complaint # 3762. The well is located about 400 east of Wintergarden Rd. and 15 south of split rail fence. Site was excavated by the City of Bowling Green with Troy Sonner and others on site. The well has 8 casing filled with dirt about two feet below ground level with about 1 yard of impacted soil. No wellhead or other production equipment on site. Hydrogen Sulfide gas level above well at 34 ppm. A 12 plastic riser was placed over well and area was filled back in. Old records indicate well might have been plugged in 1976. Also well # 20347 is located about 400 to the west and was previously plugged with fire clay in the late 70s and replugged with cement in 2007 to a depth of 650. I reviewed well for the Orphan Well Program.
515791564 2015-11-18 0:00 OR No Violations
638578204 2015-11-23 0:00 OR No Violations
652699949 2015-11-25 0:00 OR No Violations
719695063 2015-12-7 0:00: OR No Violations
800485479 2015-8-25 0:00: OR No Violations
828501513 2015-12-2 0:00: OR No Violations
898713111 2012-5-14 0:00: OR No Violations
946306891 2015-12-3 0:00: OR No Violations

For data sources see[3]

References