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34-169-22200

Well Details

Well ID: 34-169-22200
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Country: United States
State: Ohio
County: Wayne
Municipality: Chippewa Township
Operator Name: AMTEX OIL & GAS INC
Well Pad ID:
Farm/Lease Name: HATFIELD R & K
License Status: Final Restoration
License Date: 2002-09-11
Spud Date: 1980-02-26
Spud Drilling Contractor: BOCOR DRLG
Final Drill Date: 1980-03-04
Well Total Depth: 3662.00 ft
Configuration: Vertical
Latitude: 40.950000
Longitude: -81.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-02-12 597 AMTEX OIL & GAS INC GeoDate 2/12/80
Original Spud 1980-02-26 R.I. 2-13-80 R.I. 02/13/1980
Completed 1980-03-04 R.I. 2-13-80 R.I. 02/13/1980
Reached Total Depth 1980-03-04 R.I. 2-13-80 R.I. 02/13/1980
CO 1996-07-03 597 AMTEX OIL & GAS INC GeoDate 7/3/96
Unknown 1996-07-03 Issued Date 7/3/96 Expired Date 7/3/97 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
APP 2002-09-11 Proposed Formations:CLINTON, Issued Date:9/11/2002, Expired Date:9/11/2003 6:00:00 AM, Drilling unit acres:140.49, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2002-12-06 R.I. 2-13-80 R.I. 02/13/1980
Construction Permit Expires 2003-09-11 R.I. 2-13-80 R.I. 02/13/1980
Record Last Modified 2017-02-15 R.I. 2-13-80 R.I. 02/13/1980

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3496 3522 12
3496 3522 12
3496 3522 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1200 Bbl 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 AMTEX OIL & GAS INC 6068.00 0.00 365
1986 AMTEX OIL & GAS INC 0.00 0.00 0
1987 AMTEX OIL & GAS INC 0.00 0.00 0
1988 AMTEX OIL & GAS INC 3746.00 0.00 0
1989 AMTEX OIL & GAS INC 1234.00 0.00 0
1990 AMTEX OIL & GAS INC 1106.00 0.00 365
1993 AMTEX OIL & GAS INC 1189.00 0.00 360

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 AMTEX OIL & GAS INC Brine 29 365
1986 AMTEX OIL & GAS INC Brine 0 0
1987 AMTEX OIL & GAS INC Brine 0 0
1988 AMTEX OIL & GAS INC Brine 15 0
1989 AMTEX OIL & GAS INC Brine 105 0
1990 AMTEX OIL & GAS INC Brine 0 365
1993 AMTEX OIL & GAS INC Brine 0 360

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-200296968 2003-4-4 0:00:0 FR No Violations 1.00
-2005737526 2002-12-4 0:00: PB No Violations 1.50
-206781470 2002-12-9 0:00: PB No Violations 0.70
0086080199 2003-09-10 Final Restoration No Violations Check this well for Columbus --Tom Tugend and found it has been restored and meets requirements for restoration final.There is another well on site that uses the lease road so it does not have to be restored at this time.
0200296968 2003-04-04 Final Restoration No Violations Check this well for Sherry Young and found that restoration has ben done but there is a 2 inch riser pipe that connected the flow line to the well head that remains . The line is 3 ft high and has been cleared but not cut off . I spoke to the landowner and he advised that it would be ok to leave the flow line but he would like the pipe cut off .
0206781470 2002-12-09 Plug / Plug Back No Violations Pipe has been cut off and found no leaks . Pits are pumped off and are closed and area graded not seeded . There is a 2 inch flowline remaining needs to flushed and cut off . I talked with the landowner and he will sign a waiver for line .
0469321919 2002-12-06 Plug / Plug Back No Violations Arrive on site to find 1 1/2 tubing pulled . Hook up to 4 1/2 casing to pull stretch and found that it could be in two at 1600 ft. Next try to screw back into casing . Hook up power tongs to try and turn casing and could not get back on bottom string of pipe . Decided to shoot pipe off and then try to pull out and go back in with over shot to connect to bottom string . Shooter could not get there soon so operator decided to pull 4 1/2 casing out of hole and then go back in with tubing and shoot casing . Found out that casing was together to 2580 ft . Then ran tubing back in hole and place rip and lime plug together . Last finish plugging all the way to surface .See plug report .
1254533225 2002-12-05 Plug / Plug Back No Violations The rig is over the wellhead and pump truck is hooked up to the 1 1/2 tubing . Try and circulate well and could not , too much pressure .Pull 1 1/2 tubling out and run back in to 3470 ft . And set 200 ft bottom plug from 3470 to 3270 ft c /w 60 sks class A
2005737526 2002-12-04 Plug / Plug Back No Violations Arrive on site to meet plug contractor because Inspector Whorstall requested that I be on site to test for H2S . W/O Operator to arrive and found he would not .
469321919 2002-12-6 0:00: PB No Violations 8.70
86080199 2003-9-10 0:00: FR No Violations 1.20

For data sources see[9]

References