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Well ID: 34-169-22200 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Chippewa Township | |
Operator Name: AMTEX OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: HATFIELD R & K | |
License Status: Final Restoration | |
License Date: 2002-09-11 | |
Spud Date: 1980-02-26 | |
Spud Drilling Contractor: BOCOR DRLG | |
Final Drill Date: 1980-03-04 | |
Well Total Depth: 3662.00 ft | |
Configuration: Vertical | |
Latitude: 40.950000 | |
Longitude: -81.740000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-02-12 | 597 AMTEX OIL & GAS INC GeoDate 2/12/80 |
Original Spud | 1980-02-26 | R.I. 2-13-80 R.I. 02/13/1980 |
Completed | 1980-03-04 | R.I. 2-13-80 R.I. 02/13/1980 |
Reached Total Depth | 1980-03-04 | R.I. 2-13-80 R.I. 02/13/1980 |
CO | 1996-07-03 | 597 AMTEX OIL & GAS INC GeoDate 7/3/96 |
Unknown | 1996-07-03 | Issued Date 7/3/96 Expired Date 7/3/97 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
APP | 2002-09-11 | Proposed Formations:CLINTON, Issued Date:9/11/2002, Expired Date:9/11/2003 6:00:00 AM, Drilling unit acres:140.49, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2002-12-06 | R.I. 2-13-80 R.I. 02/13/1980 |
Construction Permit Expires | 2003-09-11 | R.I. 2-13-80 R.I. 02/13/1980 |
Record Last Modified | 2017-02-15 | R.I. 2-13-80 R.I. 02/13/1980 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3496 | 3522 | 12 |
3496 | 3522 | 12 | |
3496 | 3522 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | AMTEX OIL & GAS INC | 6068.00 | 0.00 | 365 |
1986 | AMTEX OIL & GAS INC | 0.00 | 0.00 | 0 |
1987 | AMTEX OIL & GAS INC | 0.00 | 0.00 | 0 |
1988 | AMTEX OIL & GAS INC | 3746.00 | 0.00 | 0 |
1989 | AMTEX OIL & GAS INC | 1234.00 | 0.00 | 0 |
1990 | AMTEX OIL & GAS INC | 1106.00 | 0.00 | 365 |
1993 | AMTEX OIL & GAS INC | 1189.00 | 0.00 | 360 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | AMTEX OIL & GAS INC | Brine | 29 | 365 |
1986 | AMTEX OIL & GAS INC | Brine | 0 | 0 |
1987 | AMTEX OIL & GAS INC | Brine | 0 | 0 |
1988 | AMTEX OIL & GAS INC | Brine | 15 | 0 |
1989 | AMTEX OIL & GAS INC | Brine | 105 | 0 |
1990 | AMTEX OIL & GAS INC | Brine | 0 | 365 |
1993 | AMTEX OIL & GAS INC | Brine | 0 | 360 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-200296968 | 2003-4-4 0:00:0 | FR | No Violations | 1.00 |
-2005737526 | 2002-12-4 0:00: | PB | No Violations | 1.50 |
-206781470 | 2002-12-9 0:00: | PB | No Violations | 0.70 |
0086080199 | 2003-09-10 | Final Restoration | No Violations | Check this well for Columbus --Tom Tugend and found it has been restored and meets requirements for restoration final.There is another well on site that uses the lease road so it does not have to be restored at this time. |
0200296968 | 2003-04-04 | Final Restoration | No Violations | Check this well for Sherry Young and found that restoration has ben done but there is a 2 inch riser pipe that connected the flow line to the well head that remains . The line is 3 ft high and has been cleared but not cut off . I spoke to the landowner and he advised that it would be ok to leave the flow line but he would like the pipe cut off . |
0206781470 | 2002-12-09 | Plug / Plug Back | No Violations | Pipe has been cut off and found no leaks . Pits are pumped off and are closed and area graded not seeded . There is a 2 inch flowline remaining needs to flushed and cut off . I talked with the landowner and he will sign a waiver for line . |
0469321919 | 2002-12-06 | Plug / Plug Back | No Violations | Arrive on site to find 1 1/2 tubing pulled . Hook up to 4 1/2 casing to pull stretch and found that it could be in two at 1600 ft. Next try to screw back into casing . Hook up power tongs to try and turn casing and could not get back on bottom string of pipe . Decided to shoot pipe off and then try to pull out and go back in with over shot to connect to bottom string . Shooter could not get there soon so operator decided to pull 4 1/2 casing out of hole and then go back in with tubing and shoot casing . Found out that casing was together to 2580 ft . Then ran tubing back in hole and place rip and lime plug together . Last finish plugging all the way to surface .See plug report . |
1254533225 | 2002-12-05 | Plug / Plug Back | No Violations | The rig is over the wellhead and pump truck is hooked up to the 1 1/2 tubing . Try and circulate well and could not , too much pressure .Pull 1 1/2 tubling out and run back in to 3470 ft . And set 200 ft bottom plug from 3470 to 3270 ft c /w 60 sks class A |
2005737526 | 2002-12-04 | Plug / Plug Back | No Violations | Arrive on site to meet plug contractor because Inspector Whorstall requested that I be on site to test for H2S . W/O Operator to arrive and found he would not . |
469321919 | 2002-12-6 0:00: | PB | No Violations | 8.70 |
86080199 | 2003-9-10 0:00: | FR | No Violations | 1.20 |
For data sources see[9]