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34-167-28851

Well Details

Well ID: 34-167-28851
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Country: United States
State: Ohio
County: Washington
Municipality: Fairfield Township
Operator Name: AM-TEK OIL INC
Well Pad ID:
Farm/Lease Name: FREIER
License Status: Producing
License Date: 2007-06-29
Spud Date: 1991-07-31
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 1991-08-05
Well Total Depth: 5609.00 ft
Configuration: Vertical
Latitude: 39.400000
Longitude: -81.720000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1991-04-26 Issued Date 4/26/91 Expired Date 4/25/92 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05609 Proposed Drill Depth 05609
Original Spud 1991-08-01
Completed 1991-08-05
Reached Total Depth 1991-08-05
CO 1991-08-13 3434 GONZOIL INC GeoDate 4/26/91
Completion Report Received 1991-10-28
APP 2007-06-29 Proposed Formations:CLINTON, Issued Date:6/29/2007, Expired Date:6/28/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged Back 2007-07-05
Construction Permit Expires 2008-06-28
Change of Owner 2008-08-14 Operator changed from 3434, GONZOIL INC to 8404, CONLEY ENERGY CO LLC
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5398 5480 0
5398 5480 0
2006-09-11 5439 5544 31
5439 5544 31
5398 5480 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 78000 Gal 60000 FRAC W/78M GAL H20 & 600 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 GONZOIL INC 3850.00 0.00 117
1992 GONZOIL INC 9450.00 0.00 365
1993 GONZOIL INC 4531.00 0.00 365
1994 GONZOIL INC 2556.00 0.00 365
1995 GONZOIL INC 3188.00 0.00 365
1996 GONZOIL INC 2869.00 0.00 365
1997 GONZOIL INC 2078.00 0.00 365
1998 GONZOIL INC 1801.00 0.00 365
1999 GONZOIL INC 1641.00 0.00 365
2000 GONZOIL INC 1792.00 0.00 365
2001 GONZOIL INC 1436.00 0.00 365
2002 GONZOIL INC 1093.00 0.00 365
2003 GONZOIL INC 1322.00 0.00 365
2004 GONZOIL INC 884.00 0.00 365
2005 GONZOIL INC 1057.00 0.00 365
2006 GONZOIL INC 111.00 0.00 365
2007 GONZOIL INC 138.00 0.00 365
2008 GONZOIL INC 43.00 0.00 365
2012 CONLEY ENERGY CO LLC 0.00 0.00 363
2016 CONLEY ENERGY CO LLC 0.00 0.00 0
2017 CONLEY ENERGY CO LLC 0.00 0.00 0
2018 CONLEY ENERGY CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 GONZOIL INC Brine 940 117
1992 GONZOIL INC Brine 144 365
1993 GONZOIL INC Brine 0 365
1994 GONZOIL INC Brine 36 365
1995 GONZOIL INC Brine 0 365
1996 GONZOIL INC Brine 93 365
1997 GONZOIL INC Brine 0 365
1998 GONZOIL INC Brine 0 365
1999 GONZOIL INC Brine 77 365
2000 GONZOIL INC Brine 0 365
2001 GONZOIL INC Brine 75 365
2002 GONZOIL INC Brine 0 365
2003 GONZOIL INC Brine 82 365
2004 GONZOIL INC Brine 0 365
2005 GONZOIL INC Brine 0 365
2006 GONZOIL INC Brine 0 365
2007 GONZOIL INC Brine 314 365
2008 GONZOIL INC Brine 80 365
2012 CONLEY ENERGY CO LLC Brine 0 363
2016 CONLEY ENERGY CO LLC Brine 0 0
2017 CONLEY ENERGY CO LLC Brine 0 0
2018 CONLEY ENERGY CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1345104618 2007-11-14 0:00 FR No Violations
-1893147076 2006-8-17 0:00: PL No Violations
1345104618 2007-11-14 Final Restoration No Violations This is a plug-back but showing as FRD so will clear it. Hopefully, wont come back as PA - have re-completed well in Berea - about to get jack set and well producing. Ground not cleaned up yet.
1893147076 2006-08-17 Preliminary Restoration No Violations Inspection this day found well not in production, rabbit well and trail into well not traveled in long time. Tank has good IDs, needs more dike - not sure if tank leaking - dont believe dumping saltwater but salty water found in puddle outside tank. Maybe cows opened valve and drained tank? - not a big kill area. Told operators to get in production or plug - they have it on the list and will do something with it in next 2-4 months. Drill site has been reclaimed.

For data sources see[9]

References