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34-155-24065

Well Details

Well ID: 34-155-24065
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Country: United States
State: Ohio
County: Trumbull
Municipality: Bristol Township
Operator Name: CEDAR VALLEY ENERGY INC
Well Pad ID:
Farm/Lease Name: LINDOW UNIT
License Status: Producing
License Date: 2013-02-25
Spud Date: 2013-03-25
Spud Drilling Contractor: POULSON DRILLING
Final Drill Date: 2013-03-29
Well Total Depth: 4123.00 ft
Configuration: Vertical
Latitude: 41.380000
Longitude: -80.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-02-25 Proposed Formations:CLINTON, Issued Date:2/25/2013, Expired Date:2/25/2015 12:00:00 PM, Drilling unit acres:64, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2013-03-29
Completion Report Received 2013-08-19
Correction to Well 2014-11-28 UNIT SIZE DECREASED TO 44 ACRES.
Construction Permit Expires 2015-02-25
Correction to Well 2015-03-06 UNIT SIZE INCREASED TO 93.32 ACRES.
Record Last Modified 2018-01-26

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-08-20 3923 3968 30
3923 3968 30
3923 3968 30

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-08-07 H2O 15 79956 Gal 55700 Universal Well Services Inc.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 CEDAR VALLEY ENERGY INC 59.00 157.00 365
2014 CEDAR VALLEY ENERGY INC 5498.00 1231.00 365
2015 CEDAR VALLEY ENERGY INC 1634.00 481.00 365
2016 CEDAR VALLEY ENERGY INC 2183.00 544.00 365
2017 CEDAR VALLEY ENERGY INC 1810.00 445.00 365
2018 CEDAR VALLEY ENERGY INC 1507.00 364.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 CEDAR VALLEY ENERGY INC Brine 365 365
2014 CEDAR VALLEY ENERGY INC Brine 1470 365
2015 CEDAR VALLEY ENERGY INC Brine 725 365
2016 CEDAR VALLEY ENERGY INC Brine 778 365
2017 CEDAR VALLEY ENERGY INC Brine 813 365
2018 CEDAR VALLEY ENERGY INC Brine 475 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-557075020 2013-4-8 0:00:0 PW No Violations 0.50
0557075020 2013-04-08 Production Wells No Violations My inspection found the pits solidified and closed.
0983645547 2013-03-25 Drill / Deepen / Reopen No Violations I witnessed PetroSet cement the conductor casing for Cedar Valley. The Poulson Rig drilled hole #1 with a size of 14.75 and to a depth of 82. The conductor was 11.75 and set at 75. PetroSet broke circulation and pumped 115 sacks of Class A cement. They displaced with 7 barrels of fresh water. The plug landed at 12:25 pm. I witnessed a good return of cement to surface.
1364991762 2013-04-03 Drill / Deepen / Reopen No Violations My inspection found Cedar Valley in the process of closing the pits.
1529815646 2013-03-20 Drill / Deepen / Reopen No Violations My inspection found the well pad built. The lease road was compacted and covered with gravel. Part of the lease road was the landowners driveway. Drainage controls were in place with a properly installed silt fence. There was a creek to the north of the well site with a new culvert. An identification sign was posted at the entrance of the lease road. I spoke to the field supervisor, Tim Cosma at 330-853-9565. The Poulson Rig is due to move onto location on 3/25/2013.
1991669433 2014-06-04 Preliminary Restoration No Violations I was on location for a preliminary restoration inspection. I found during my inspection the pumpjack in production. There was a barb wire fence surrounding the pumpjack. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank and a separator. A bull plug was installed on the load line. A dike surrounded the tank battery. An identification was properly posted. There was a 7 day production chart at the separator. The well site was properly graded. Vegetation was well established. The lease road was in excellent condition. The pits were closed and all debris removed. Drainage and erosion controls were in place. All drilling equipment was removed from the well site. Preliminary restoration passed.
983645547 2013-3-25 0:00: DD No Violations 1.50

For data sources see[9]

References