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34-155-23611

Well Details

Well ID: 34-155-23611
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Country: United States
State: Ohio
County: Trumbull
Municipality: Weathersfield Township
Operator Name: BOBCAT WELL & PIPELINE LLC
Well Pad ID:
Farm/Lease Name: WOODLEY
License Status: Plugged and Abandoned
License Date: 2018-12-06
Spud Date: 1996-04-13
Spud Drilling Contractor: MOHAWK DRLG
Final Drill Date: 1996-04-17
Well Total Depth: 5010.00 ft
Configuration: Vertical
Latitude: 41.160000
Longitude: -80.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1996-02-26 2651 D & L ENERGY INC GeoDate 2/26/96
Oil and Gas 1996-02-26 Issued Date 2/26/96 Expired Date 2/25/97 Acres 0042590 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05010 Proposed Drill Depth 05010
Original Spud 1996-04-13
Completed 1996-04-17
Reached Total Depth 1996-04-17
Completion Report Received 1996-05-09
Change of Owner 2015-01-27 Operator changed from 2651, D & L ENERGY INC to 9426, BOBCATE WELL AND PIPELINE LLC
APP 2018-12-06 Proposed Formations:CLINTON SAND, Issued Date:12/6/2018, Expired Date:12/5/2020 12:00:00 PM, Drilling unit acres:42, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2018-12-13
Construction Permit Expires 2020-12-05

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4693 4846 0
4693 4846 0
2006-09-11 4724 4790 40
4724 4790 40
4693 4846 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 8 500 Gal 0 FRAC W/109,200 GAL WATER AND 92M#
H2O 0 109200 Gal 92000 AVG RATE 33.4, AVG PRESS 1216, ISIP 668, 5 MIN ISIP 640.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1997 D & L ENERGY INC 23896.00 369.00 334
1998 D & L ENERGY INC 18462.00 165.00 365
1999 D & L ENERGY INC 14617.00 110.00 365
2000 D & L ENERGY INC 11909.00 41.00 365
2001 D & L ENERGY INC 10022.00 61.00 365
2002 D & L ENERGY INC 7903.00 44.00 365
2003 D & L ENERGY INC 8077.00 0.00 365
2004 D & L ENERGY INC 8405.00 47.00 365
2005 D & L ENERGY INC 6801.00 0.00 365
2006 D & L ENERGY INC 7031.00 0.00 365
2007 D & L ENERGY INC 6897.00 0.00 365
2008 D & L ENERGY INC 6560.00 65.00 366
2009 D & L ENERGY INC 5920.00 0.00 365
2010 D & L ENERGY INC 4896.00 0.00 365
2011 D & L ENERGY INC 4543.00 33.00 0
2012 D & L ENERGY INC 5728.00 0.00 365
2013 D & L ENERGY INC 5061.00 0.00 365
2014 D & L ENERGY INC 3482.00 0.00 365
2015 BOBCAT WELL & PIPELINE LLC 3402.00 0.00 365
2016 BOBCAT WELL & PIPELINE LLC 2965.00 0.00 302
2017 BOBCAT WELL & PIPELINE LLC 3727.00 23.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1997 D & L ENERGY INC Brine 258 334
1998 D & L ENERGY INC Brine 72 365
1999 D & L ENERGY INC Brine 26 365
2000 D & L ENERGY INC Brine 0 365
2001 D & L ENERGY INC Brine 0 365
2002 D & L ENERGY INC Brine 35 365
2003 D & L ENERGY INC Brine 0 365
2004 D & L ENERGY INC Brine 0 365
2005 D & L ENERGY INC Brine 0 365
2006 D & L ENERGY INC Brine 0 365
2007 D & L ENERGY INC Brine 0 365
2008 D & L ENERGY INC Brine 30 366
2009 D & L ENERGY INC Brine 0 365
2010 D & L ENERGY INC Brine 0 365
2011 D & L ENERGY INC Brine 0
2012 D & L ENERGY INC Brine 0 365
2013 D & L ENERGY INC Brine 0 365
2014 D & L ENERGY INC Brine 0 365
2015 BOBCAT WELL & PIPELINE LLC Brine 365
2016 BOBCAT WELL & PIPELINE LLC Brine 0 302
2017 BOBCAT WELL & PIPELINE LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1845132177 2019-2-19 0:00: UP No Violations
-341746137 2013-10-24 0:00 UP No Violations 0.50
-662700319 2019-2-6 0:00:0 UP No Violations 2.00
-95034759 2004-3-10 0:00: PL No Violations
0095034759 2004-03-10 Preliminary Restoration No Violations Restoration approved .
0160301605 2017-04-12 UrbanProduction Wells No Violations

-up line is secure with a plug. There is a deduct meter and 7-

The equipment on site:



0341746137 2013-10-24 UrbanProduction Wells No Violations My inspection found the well in production. The well was equipped with a plunger lift unit and three domestic gas lines. The tank battery contained a 100 barrel production tank, a 30 barrel brine tank, and a separator. There were locked, chain link fences surrounding the tank battery and well. The proper identification sign was posted. The dike was slightly weathered; however, it met containment requirements. There was a plug on the load line. The lease road was in good, working condition. The well was placed into production prior to House Bill 278.
0662700319 2019-02-06 UrbanProduction Wells Violations Noted On location to check the status of this Clinton Sandstone well. The well was reported by the operator, Bobcat Well & Pipeline, LLC (BWP), to Northeast Regional Supervisor Tom Hill to have a defective production casing. The operator also reported that they were temporally mitigating// controlling the annular gas pressure between the 8---pressure regulator and a gauge on the line indicates an annular pressure of 170psi. The geophysical log for the well confirms the 8-5/8 surface casing seat at a depth of 340 measured from ground level (GL). This casing seat is considered over-pressurized when the pressure at the surface exceeds 103psi (.303 X 340) and is currently in violation of 1501:9-1-08(N)(2) of the Ohio Administrative Code. An inspection of the surface production equipment found a Murphy Switch gauge at the separator that shows a pressure of 150psi on the vessel. The meter chart shows differential production pressures (line pressures) between 120psi and 150psi. Based on this information, the current remedial actions employed by Bobcat Well & Pipeline will not achieve compliance with the Ohio Administrative Code. Further, sustainable, remedial actions are required to lower the annular pressure below the maximum allowable pressure of 103psi by 1) repairing the defective casing, 2) properly plug & abandon the well, or 3) perform another activity that is approved by the Division that will mitigate the annular pressure. Supervisor Tom Hill informed Dave Rice (BWP) of t
1562683296 2019-5-23 0:00: PB No Violations
160301605 2017-4-12 0:00: UP No Violations 0.60
1845132177 2019-02-19 UrbanProduction Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice inspection issued on 2/7/19, regarding defective production casing. At the time of this inspection, the well was equipped with a plunger lift assembly. The gate valve on the tubing was closed, but the 2 inch flow line was open. The 4.5 inch casing valve was open was equipped with a pressure gauge that read 120 psi . The 8-5/8 inch surface casing head and port are below grade and the annular access port has been plumbed to surface with 2 inch and 1 inch piping, that is tied into the flow line. The annular flow line was equipped with a back-pressure regulator, however the pressure gauge on this line mentioned in the previous report dated 2-6-19, was not present at the time of this inspection. No pressure reading could be obtained on the 8 5/8 inch surface casing, during this inspection. The chart on the mechanical separator, located in the diked tank battery showed no pressure differential readings. I contacted Dave Rice from Bobcat Well & Pipeline, LLC and left a message requesting that a pressure gauge be reinstalled on the annular flow line to determine what the current line pressure was, in order to see if remedial actions have been taken to reduce the annular pressure below 103 psi, as required by OAC 1501:9-1-08(N)(2).
369833761 2019-5-24 0:00: PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0662700319 US-OH-127499 2019-02-13 NONE17 Defective casing, leaking well

For data sources see[9]

References