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34-155-22500

Well Details

Well ID: 34-155-22500
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Country: United States
State: Ohio
County: Trumbull
Municipality: Bristol Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: BRISTOL SPRINGS COUNTRY CLUB
License Status: Producing
License Date: 1984-01-18
Spud Date: 1984-02-01
Spud Drilling Contractor: GRISWALD & ASSOC.
Final Drill Date: 1984-02-12
Well Total Depth: 4165.00 ft
Configuration: Vertical
Latitude: 41.410000
Longitude: -80.860000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-01-18 130 LESLIE OIL & GAS CO INC GeoDate 1/18/84
Oil and Gas 1984-01-18 Issued Date 12/30/83 Expired Date 6/27/84 Acres 0043324 Tool Type RTF Proposed Formation CLINTON Proposed Depth 04165 Proposed Drill Depth 04165
Original Spud 1984-02-01
Completed 1984-02-12
Reached Total Depth 1984-02-12
Completion Report Received 1984-03-08
Construction Permit Expires 1984-06-27
CO 1993-09-27 54 TITAN ENERGY CORP GeoDate 1/18/84
Change of Owner 1998-01-26 Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3900 4044 0
3900 4044 0
2006-09-11 3937 4010 14
3937 4010 14
3900 4044 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 60000 Gal 45000 NONE;PRELIMINARY

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 LESLIE OIL & GAS CO INC 8892.00 592.00 365
1986 LESLIE OIL & GAS CO INC 3907.00 469.00 351
1989 LESLIE OIL & GAS CO INC 762.00 150.00 365
1990 LESLIE OIL & GAS CO INC 1.00 169.00 365
1991 LESLIE OIL & GAS CO INC 1096.00 142.00 365
1992 TITAN ENERGY CORP 925.00 124.00 365
1994 TITAN ENERGY CORP 352.00 75.00 365
1997 TITAN ENERGY CORP 0.00 40.00 245
2000 BIG SKY ENERGY INC 0.00 0.00 365
2001 BIG SKY ENERGY INC 75.00 0.00 365
2002 BIG SKY ENERGY INC 162.00 0.00 365
2003 BIG SKY ENERGY INC 0.00 66.00 365
2004 BIG SKY ENERGY INC 457.00 25.00 365
2005 BIG SKY ENERGY INC 344.00 0.00 365
2006 BIG SKY ENERGY INC 235.00 287.00 365
2007 BIG SKY ENERGY INC 75.00 107.00 365
2008 BIG SKY ENERGY INC 0.00 0.00 365
2009 BIG SKY ENERGY INC 939.00 0.00 365
2010 BIG SKY ENERGY INC 395.00 92.00 365
2011 BIG SKY ENERGY INC 25.00 0.00 365
2012 BIG SKY ENERGY INC 193.00 0.00 366
2013 BIG SKY ENERGY INC 356.00 0.00 300
2014 BIG SKY ENERGY INC 805.00 106.00 365
2016 BIG SKY ENERGY INC 47.00 0.00 98
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 LESLIE OIL & GAS CO INC Brine 630 365
1986 LESLIE OIL & GAS CO INC Brine 545 351
1989 LESLIE OIL & GAS CO INC Brine 0 365
1990 LESLIE OIL & GAS CO INC Brine 489 365
1991 LESLIE OIL & GAS CO INC Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 70 365
1997 TITAN ENERGY CORP Brine 245
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 6 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 116 300
2014 BIG SKY ENERGY INC Brine 589 365
2016 BIG SKY ENERGY INC Brine 0 98
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1286411547 2014-4-10 0:00: PW No Violations 1.00
-1660003801 2013-9-24 0:00: PW No Violations
-1692148571 2013-11-6 0:00: PW No Violations 0.50
-1694037204 2016-4-29 0:00: PW No Violations 0.70
-2007848716 2014-4-14 0:00: PW No Violations 2.50
-2008131406 2016-6-27 0:00: PW No Violations 0.70
-2040744135 2013-9-10 0:00: PW No Violations 1.00
-2111719213 2017-12-7 0:00: PW No Violations 0.70
-233315096 2014-4-24 0:00: AM No Violations 0.20
-572123044 2014-6-4 0:00:0 PW No Violations 0.50
0000PL3783 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0097690663 2019-03-13 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1694037204, regarding cleanup of oil impacted soil at the well and tank battery locations, identification needing installed and repair of the fencing around the well. At the time of this inspection, the oil impacted soil at the separator and base of the 210 BBL storage tank had not been cleaned up. The identification sign posted is blank. The oil impacted soil and vegetation at the wellhead has not been removed. The wooden panels on the fence surrounding the pumping unit have fallen over onto the ground and need reinstalled.
0233315096 2014-04-24 Administrative Inspection No Violations I performed an administrative inspection in reference to Chiefs Order 2014-43. I received a call and spoke to the golf course owners lawyer. He stated Bob Barr Jr. was on location putting the pumping unit into production. He stated the golf course maintenance crew was video taping Bob performing the act.
0572123044 2014-06-04 Production Wells No Violations I received a call at 1:56pm from the Bristolwood Golf Course owner stating that Bob Barr Jr. was on location with three employees, a tanker truck and a pick-up truck operating the well. When I arrived at the golf course; Big Sky was not on location. I spoke to the owner; who showed me photos of Big Sky working at the well and tank battery. Big Skys operation of the well was in non-compliance with Chiefs Order 2014-43.
0763693824 2016-07-07 Production Wells No Violations I was on location to assess compliance notice # -1694037204. At the time of my inspection, I found the well not in production. Peat sorb is still spread over the oil impacted areas inside and outside the fence surrounding the well. The operator has not removed the impacted soil and vegetation from inside and outside of the fence surrounding the well. Another panel section of the fence surrounding the well has fallen. Photos have been taken and are available upon request.

The operator still needs to: Repair the wellhead to prevent further oil leaks. Remove and dispose of all oil impacted soil and vegetation at the well, separator, and 210 bbl tank. Repair all surface areas affected by the oil releases. Repair the fence around the pumping unit.

0824005944 2016-06-14 Production Wells No Violations I was on location to assess compliance notice # -1694037204. At the time of my inspection, I found the well not in production. Peat sorb is still spread over the oil impacted areas inside and outside the fence surrounding the well. The operator has not removed the impacted soil and vegetation from inside and outside of the fence surrounding the well. Photos have been taken and are available upon request.

The operator still needs to: Repair the wellhead to prevent further oil leaks. Remove and dispose of all oil impacted soil and vegetation at the well, separator, and 210 bbl tank. Repair all surface areas affected by the oil releases.

1286411547 2014-04-10 Production Wells No Violations I performed a follow-up inspection concerning the clean-up operations for the oil spill. My inspection found all of the impacted grass and soil removed. The 210 barrel production tank was cleaned of all oil. Peat moss was spread over the entire impacted area. The well tender was on location and stated a new identification sign had been ordered. I will follow-up on the identification sign. Photos were taken.
1336614562 2014-02-28 Production Wells Violations Noted I checked this well to determine if the company is in compliance with chiefs order # 2014-43 . I found the tank battery is equipped with 1 100 bbl , 1 210 bbl steel tanks and 1 separator . The 100 bbl tank was empty and the 210 bbl tank was 1/3 full of fluid . The date marked on chart on gas meter was 2-26 , the year was not indicated . The identification sign posted on the 210 bbl tank was mostly ripped off and was not legible which is in violation of 1501: 9-9-05 , A-10 of the Ohio Administrative Rule . The valve from the flow line to the separator was closed . The earthen dike protecting the tank battery is not of sufficient size to contain the amount of fluid which could be stored in the production tanks , which is in violation of 1501:9-9-05 , A-9 of the Ohio Administrative Rule . At the well location I found the well is equipped with a pumping unit , the pumping unit was not in operation at the time of my inspection . There is a domestic hook-up from the production casing with the valve closed . There is a 6 wood fence surrounding the pumping unit . NOTE : This well is located on the Bristolwood Golf Course . This well was not in production at the time of my inspection .
1378992713 2013-09-06 Production Wells No Violations I received a inspection request from the Bristolwood Golf Course. My inspection found the well not in production. The well was equipped with a pumping unit with all the valves to the flow line closed. The well was surrounded by a wooden fence with half of the panels either missing or lying on the ground. I noticed a 4 diameter greasy black stain and an 18 diameter muddy area on the grass located approximately 6 southeast from the pump unit. The head maintenance employee, Leroy, claimed a Big Sky crew had been on location working on the well the entire week (9/3/13 to 9/5/13). The tank battery contained a 100 barrel production tank, a 50 barrel brine tank, and a separator. The dike was slightly weathered; however, it meets containment requirements. There was no identification sign posted. I called Valerie Dunne of Well Completion Services at 440-858-2343. Valerie stated she would dispatch Ryan, their well tender, to meet me on location. Once Ryan arrived at the golf course, he claimed the well was shut-in to replace the rods, which caused the greasy black stain on the grass. Also, he said the muddy area was a flow line leak. Big Sky pumped fresh water from the tank battery through the flow line to locate the leak. I instructed Ryan to begin repairs on the flow line immediately, post the proper identification sign, and replace the wood fence panels. At 11:20am, I received a call from Bob Barr, Jr. He stated Big Sky would start repairs on the flow line by 9/10/13. I took photos of the well location.
1462365166 2016-05-04 Production Wells No Violations I was on location in reference to compliance to Chiefs Order 2016-105. At the time of my inspection, I found no change from my previous inspection on 4-29-
1464278238 2016-05-20 Production Wells No Violations I was on location to assess compliance to Chiefs Order 2016-
1464369127 2016-05-27 Production Wells No Violations I was on location to assess compliance to Chiefs Order 2016-
1512583642 2016-05-26 Production Wells No Violations I was on location with ODNR Operations and Response Manager Terry Whitehair and ODNR Operations Coordinator Fred Romeo. I found a pool of oil outside of the fenced pumping unit on the south side. The area of impact is approximately 6 in diameter. The wellhead is coated with oil and paraffin. The vegetation in an area approximately 6 x 3 in front of the wellhead is impacted by oil. The well is shut-in with closed 2 flow line ball valves coming off of the wellhead. I contacted Big Sky Energy to respond immediately to the oil spill. Photos were taken and are available upon request.
1522326807 2018-03-12 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1694037204. The oil impacted soil at the separator and base of the 210 BBL storage tank had not been cleaned up. The identification sign posted is blank. The oil impacted soil and vegetation at the wellhead has not been removed. The wooden panels on the fence surrounding the pumping unit have fallen over onto the ground and need reinstalled.
1546218246 2013-09-11 Production Wells No Violations My inspection found the flow line repaired, soil compacted, seeded, and straw spread. I took photos of the repair.
1561790158 2013-10-01 Production Wells No Violations I performed a follow up inspection of the brine spill from the tank battery. My inspection found lime spread throughout the tank battery and lease road. I noticed a section of grass next to the lease road southwest of the tank battery that was brine scolded. The approximate area was 2 wide by 15 long. According to ODNR Inspector Kevin Perry, Bob Barr, Jr. told Kevin that Big Sky would till up the brine scolded area next to the lease road and re-seed. I called Bob Barr, Jr. at 740-624-0434 and left a message to finish tilling the affected grass area, then seed.
1660003801 2013-09-24 Production Wells No Violations I was on location today in reference to complaint #4467. Bob Barr Jr. was on location with K.D.A. vac truck. The 100 BBL brine tank had rusted through on the bottom of the tank. The brine brine that escaped through the dike had pooled up in the lease road and some made it into the grass. Bob said that he has a crew on the way over to the location. The are going to till up the affected area, mix in soil and lime, and then seed and straw the area. The 100 BBL tank is going to be removed from the location. I informed him that he needs identification on the location. The fence around the pump jack needs repaired. The stuffing box seals need to be repaired and the area around the wellhead needs cleaned up.
1692148571 2013-11-06 Production Wells No Violations My inspection found the wooden fence surrounding the pumping unit repaired and newly painted. The brine scald near the tank battery was removed and the soil tilled; new grass seed was spread.
1694037204 2016-04-29 Production Wells Violations Noted I was on location in reference to compliance to Chiefs Order 2016--2-

Big Sky needs to: Shut in the well immediately per the temporary restraining order issued by the Trumbull County Court of Common Pleas dated 4-11-2016 Repair the oil leak at the well. Remove and dispose of all oil impacted soil and vegetation at the well, separator, and 210 bbl tank. Repair all surface areas affected by the oil releases.

The equipment on the site consists of the following:


1 Mechanical separator 1 Production well

2007848716 2014-04-14 Production Wells No Violations I responded to a call about an oil spill at the tank battery. My inspection found the 210 barrel production tank covered with oil. There was an approximately 20 gallons of oil lying around the 210 barrel production tank and between the production tank and 100 barrel brine tank. All of the oil was contained inside the dike. I noticed the identification was ripped in half. Bobby Barr of Big Sky was on location. I instructed Bobby to suck up all of the oil, remove all of the impacted grass and soil, clean all of the oil off the production tank, and replace the identification sign. I questioned Bobby as to why the tank overflowed when the well was supposed to be shut-in per Chiefs Order 2014-43. Bobby claimed the well was shut-in. Photos were taken.
2008131406 2016-06-27 Production Wells No Violations I was on location to assess compliance notice # -1694037204. At the time of my inspection, I found the well not in production. Peat sorb is still spread over the oil impacted areas inside and outside the fence surrounding the well. The operator has not removed the impacted soil and vegetation from inside and outside of the fence surrounding the well. A panel section of the fence surrounding the well is still lying on the ground. Photos have been taken and are available upon request.

The operator still needs to: Repair the wellhead to prevent further oil leaks. Remove and dispose of all oil impacted soil and vegetation at the well, separator, and 210 bbl tank. Repair all surface areas affected by the oil releases.

2040744135 2013-09-10 Production Wells No Violations My inspection found Bob Barr, Jr. and crew making repairs to the flow line next to the well. I noticed a 2 black poly flow line was exposed. The line was approximately 12 deep. Bob stated once the flow line was repaired; the soil would be compacted into place and seeded. I noticed no evidence of any impacted soil from the flow line leak. To prevent a safety hazard to the golfers, I told Bob further inspections of the well would continue until the fallen and missing wooden panels surrounding the pumping unit where repaired.
2111719213 2017-12-07 Production Wells No Violations I was on location to assess compliance notice # -1694037204. I found the oil impacted soil at the separator and base of the 210 bbl. storage tank has not been cleaned up. The identification sign posted is blank. The bottom of the separator has holes from corrosion. The oil impacted soil and vegetation at the wellhead has not been removed. The wooden panels on the fence surrounding the pumping unit have fallen over onto the ground. Photos have been taken and are available upon request.

The operator still needs to: Repair the wellhead to prevent further oil leaks. Remove and dispose of all oil impacted soil and vegetation at the well, separator, and 210 bbl. tank. Repair all surface areas affected by the oil releases. Repair the fence around the pumping unit.

763693824 2016-7-7 0:00:0 PW No Violations 0.70
824005944 2016-6-14 0:00: PW No Violations 1.00
97690663 2019-3-13 0:00: PW No Violations
PL3783 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1336614562 US-OH-109687 2014-03-21 Failure to legibly identify well
1336614562 US-OH-109688 2014-03-21 No SPCC dike/or failure to keep dike free of water or oil
1694037204 US-OH-116792 2016-05-27 Well operation causing pollution and contamination

For data sources see[9]

References