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34-155-22078

Well Details

Well ID: 34-155-22078
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Country: United States
State: Ohio
County: Trumbull
Municipality: Bristol Township
Operator Name: PETROX, INC
Well Pad ID:
Farm/Lease Name: WILLIAMS
License Status: Final Restoration
License Date: 2013-10-21
Spud Date: 1982-02-26
Spud Drilling Contractor:
Final Drill Date: 1982-03-03
Well Total Depth: 4100.00 ft
Configuration: Vertical
Latitude: 41.390000
Longitude: -80.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-31 1777 ALTOS PETROLEUM SERV INC GeoDate 12/31/81
Original Spud 1982-02-26 FORM 55 RCD 11-29-2013
Completed 1982-03-03 FORM 55 RCD 11-29-2013
Reached Total Depth 1982-03-03 FORM 55 RCD 11-29-2013
CO 1993-10-18 1966 PETROX INC GeoDate 12/31/81
CO 1994-06-02 1966 PETROX INC GeoDate 6/2/94
Unknown 1994-06-02 Issued Date 6/2/94 Expired Date 6/2/95 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
APP 1998-01-27 Proposed Formations:CLINTON, Issued Date:1/27/98, Expired Date:1/27/99 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2013-10-21 Proposed Formations:CLINTON, Issued Date:10/21/2013, Expired Date:10/21/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-10-22 FORM 55 RCD 11-29-2013
Construction Permit Expires 2015-10-21 FORM 55 RCD 11-29-2013
Record Last Modified 2016-08-11 FORM 55 RCD 11-29-2013

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3916 3952 15
3916 3952 15
3916 3952 15

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 57970 Gal 50000
N2 0 145 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 YEI INC 2262.00 506.00 0
1985 YEI INC 1609.00 341.00 189
1987 ALTOS PETROLEUM SERV INC 920.00 305.00 209
1988 ALTOS PETROLEUM SERV INC 1572.00 274.00 358
1989 ALTOS PETROLEUM SERV INC 999.00 280.00 340
1990 ALTOS PETROLEUM SERV INC 727.00 268.00 344
1991 CGAS EXPLORATION 385.00 226.00 365
1992 ALSID OIL & GAS 490.00 224.00 365
1993 PETROX, INC 103.00 0.00 80
1994 CGAS EXPLORATION 500.00 173.00 365
1995 PETROX, INC 0.00 0.00 365
1996 PETROX, INC 0.00 0.00 365
1997 PETROX, INC 0.00 0.00 365
1998 PETROX, INC 0.00 0.00 365
1999 PETROX, INC 0.00 0.00 365
2001 PETROX, INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 YEI INC Brine 0 0
1985 YEI INC Brine 325 189
1987 ALTOS PETROLEUM SERV INC Brine 141 209
1988 ALTOS PETROLEUM SERV INC Brine 290 358
1989 ALTOS PETROLEUM SERV INC Brine 265 340
1990 ALTOS PETROLEUM SERV INC Brine 261 344
1991 CGAS EXPLORATION Brine 0 365
1992 ALSID OIL & GAS Brine 195 365
1993 PETROX, INC Brine 140 80
1994 CGAS EXPLORATION Brine 0 365
1995 PETROX, INC Brine 0 365
1996 PETROX, INC Brine 0 365
1997 PETROX, INC Brine 0 365
1998 PETROX, INC Brine 0 365
1999 PETROX, INC Brine 0 365
2001 PETROX, INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2066222449 2013-10-22 0:00 PB No Violations 8.50
1532465027 2016-06-03 Final Restoration No Violations I was on location for a final restoration. I found during my inspection all of the production equipment removed. The site was graded. Vegetation was well established. The pits were filled and closed. All debris was removed. The lease road was being used to service an existing well. Final restoration passed.
1842110072 2014-07-30 Final Restoration No Violations I was on location for a final restoration. I found during my inspection all of the production equipment removed. The site was graded. Vegetation was well established. The pits were filled and closed. All debris was removed. The lease road was being used to service an existing well. Final restoration passed.
2066222449 2013-10-22 Plug / Plug Back No Violations I witnessed Nicks Well Plugging plug the well for Petrox, Inc. Nick bull headed 25 sacks of Class A cement for Plug #1. The cement was displace with 60 bbls of salt water. Plug #1 was set from 3,716 to 4,002. The operator pressured up to 900 psi and held it for 30 minutes. Next, the 4.5 casing was ripped at 2,760 and 8 joints were removed. Nick established circulation and pumped 86 sacks of Class A cement. The cement was displaced with 36 bbls of fresh water. Plug #2 was set from 2,172 to 2,472 to cover the top of the Big Lime. The operator pull 61 joints. Nick established circulation and pumped 139 bbls of Class A cement. I witnessed a good cement returned to surface. Plug #3 was set from 450 to surface. The operator pulled the remaining 13 joints and the cement was topped off. Cement was static at surface after 20 minutes. A total of 82 joints of 4.5 casing was removed from the well.

For data sources see[9]

References