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34-155-21944

Well Details

Well ID: 34-155-21944
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Country: United States
State: Ohio
County: Trumbull
Municipality: Greene Township
Operator Name: ANNAROCK PETROLEUM LLC
Well Pad ID:
Farm/Lease Name: LAJUNE
License Status: Producing
License Date: 1981-08-31
Spud Date: 1981-09-18
Spud Drilling Contractor:
Final Drill Date: 1981-09-24
Well Total Depth: 4190.00 ft
Configuration: Vertical
Latitude: 41.460000
Longitude: -80.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-08-31 224 ATLAS ENERGY GROUP INC GeoDate 8/31/81
Original Spud 1981-09-18
Completed 1981-09-24
Reached Total Depth 1981-09-24
Change of Owner 2001-02-16 Operator changed from 224, ATLAS ENERGY GROUP INC to 1919, EXPLORATION ENERGY INC
Change of Owner 2001-04-03 Operator changed from 1919, EXPLORATION ENERGY INC to 6857, ANNAROCK PETROLEUM LLC
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3976 3994 1
3976 3994 1
3976 3994 1

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2012 ANNAROCK PETROLEUM LLC 0.00 0.00 0
2013 ANNAROCK PETROLEUM LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2012 ANNAROCK PETROLEUM LLC Brine 0 0
2013 ANNAROCK PETROLEUM LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-557467624 2019-4-25 0:00: PW No Violations
0557467624 2019-04-25 Production Wells Violations Noted

-inch casing swage with a 2-inch valve on top. Valve was shut. There was a 2-inch plug inserted in the valve. There is oil saturated ground approximately 4 foot by 4 foot in diameter on the east side of the well head. Well is located approximately 450 feet from the road in the middle of a field. There is no tank battery, production equipment, or lease associated with this well that I could find. No production ever reported. The well is in violation of Revised code 1509.062 and shall be plugged in accordance with Ohio revived code section 1509.12 (B). The well owner/operator shall submit a written plugging schedule Shannon Mullins at 375 Forest Lake Dr. Ste. 150, Uniontown, Ohio 44685 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.

137240430 2020-4-2 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0557467624 US-OH-126144 2019-05-02 9-1-07 Well operation causing pollution and contamination
0557467624 US-OH-126145 2019-05-02 9-9-05(A)10 Failure to legibly identify well
0557467624 US-OH-126146 2019-05-02 NONE Well shall be plugged

For data sources see[8]

References