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34-155-20264

Well Details

Well ID: 34-155-20264
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Country: United States
State: Ohio
County: Trumbull
Municipality: Weathersfield Township
Operator Name: RMI TITANIUM COMPANY
Well Pad ID:
Farm/Lease Name: SWEGAN
License Status: Producing
License Date: 1975-09-22
Spud Date: 1975-10-23
Spud Drilling Contractor:
Final Drill Date: 1976-01-23
Well Total Depth: 4753.00 ft
Configuration: Vertical
Latitude: 41.170000
Longitude: -80.790000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1975-09-22 2125 EASTERN PETROLEUM CO GeoDate 9/22/75
Unknown 1975-09-22 Issued Date 9/22/75 Expired Date Acres 0000000 Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Original Spud 1975-10-23
Completed 1976-01-23
Reached Total Depth 1976-01-23
Completion Report Received 1976-02-23
Construction Permit Expires 1976-09-21
CO 1996-10-03 213 LOMAK OPERATING CO GeoDate 9/22/75
Change of Owner 2000-06-28 Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2000-07-06 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 6786, RMI TITANIUM COMPANY
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4560 4600 31
4560 4600 31
4560 4600 31

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 77000 Gal 60000 ISIP 72 HR.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RMI COMPANY 10875.00 226.00 0
2000 RMI TITANIUM COMPANY 3775.00 46.00 365
2001 RMI TITANIUM COMPANY 3948.00 48.00 365
2002 RMI TITANIUM COMPANY 3572.00 0.00 365
2003 RMI TITANIUM COMPANY 2889.00 0.00 365
2004 RMI TITANIUM COMPANY 2608.00 61.00 365
2005 RMI TITANIUM COMPANY 2629.00 0.00 365
2006 RMI TITANIUM COMPANY 2745.00 0.00 365
2007 RMI TITANIUM COMPANY 2466.00 77.00 365
2008 RMI TITANIUM COMPANY 2132.00 0.00 365
2009 RMI TITANIUM COMPANY 1351.00 0.00 365
2010 RMI TITANIUM COMPANY 1203.00 0.00 365
2011 RMI TITANIUM COMPANY 1037.00 0.00 0
2012 RMI TITANIUM COMPANY 1782.00 0.00 366
2013 RMI TITANIUM COMPANY 3195.00 0.00 365
2014 RMI TITANIUM COMPANY 3502.00 0.00 365
2015 RMI TITANIUM COMPANY 2969.00 0.00 365
2016 RMI TITANIUM COMPANY 2784.00 0.00 365
2017 RMI TITANIUM COMPANY 2760.00 0.00 365
2018 RMI TITANIUM COMPANY 1944.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RMI COMPANY Brine 0 0
2000 RMI TITANIUM COMPANY Brine 0 365
2001 RMI TITANIUM COMPANY Brine 26 365
2002 RMI TITANIUM COMPANY Brine 0 365
2003 RMI TITANIUM COMPANY Brine 0 365
2004 RMI TITANIUM COMPANY Brine 13 365
2005 RMI TITANIUM COMPANY Brine 0 365
2006 RMI TITANIUM COMPANY Brine 0 365
2007 RMI TITANIUM COMPANY Brine 23 365
2008 RMI TITANIUM COMPANY Brine 20 365
2009 RMI TITANIUM COMPANY Brine 0 365
2010 RMI TITANIUM COMPANY Brine 0 365
2011 RMI TITANIUM COMPANY Brine 0
2012 RMI TITANIUM COMPANY Brine 0 366
2013 RMI TITANIUM COMPANY Brine 0 365
2014 RMI TITANIUM COMPANY Brine 0 365
2015 RMI TITANIUM COMPANY Brine 0 365
2016 RMI TITANIUM COMPANY Brine 0 365
2017 RMI TITANIUM COMPANY Brine 0 365
2018 RMI TITANIUM COMPANY Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1689908997 2013-02-20 UrbanProduction Wells No Violations My inspection found the well equipped with a plunger lift unit. The tank battery contained one, 100 barrel production tank. It had a plug on the load line. The heat treated separator had the correct spacing and contained a 7 day production chart. The proper identification sign was posted. The proper dike was around both the tank and separator. The lease road was in good condition with a open gate at the entrance. The production records were up to date on our database. This well was placed into production prior to House Bill 278.

For data sources see[9]

References