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34-151-25762

Well Details

Well ID: 34-151-25762
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Country: United States
State: Ohio
County: Stark
Municipality: Marlboro Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: KIKO UNIT
License Status: Producing
License Date: 2011-09-26
Spud Date: 2011-10-17
Spud Drilling Contractor: ADVENT DRLG
Final Drill Date: 2011-11-01
Well Total Depth: 7545.00 ft
Configuration: Vertical
Latitude: 40.970000
Longitude: -81.250000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-09-26 Proposed Formations:ORISKANY-KNOX, Issued Date:9/26/2011, Expired Date:9/25/2013 12:00:00 PM, Drilling unit acres:52, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2011-11-01
Completion Report Received 2012-02-10
Construction Permit Expires 2013-09-25
Change of Owner 2014-05-28 Operator changed from 7626, M & M ROYALTY LTD to 7578, ENERVEST OPERATING L
Record Last Modified 2017-10-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-02-21 7278 7280 0
2012-02-21 7268 7275 0
7268 7275 0
7278 7280 0
7308 7312 0
7572 7580 0
7496 7508 0
7268 7275 0
2012-02-21 7308 7312 0
2012-02-21 7572 7580 0
2012-02-21 7496 7508 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-01-11 H2O 0 68055 Gal 40000 Universal Well Services Inc.
2012-01-02 ACID 20 2000 Gal 0 Universal Well Services Inc. SET PLUG@7450'

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2012 M & M ROYALTY LTD 6418.00 13402.00 366
2013 M & M ROYALTY LTD 6719.00 10699.00 365
2014 ENERVEST OPERATING LLC 3442.00 3409.00 292
2015 ENERVEST OPERATING LLC 3038.00 3334.00 365
2016 ENERVEST OPERATING LLC 3593.00 2855.00 366
2017 ENERVEST OPERATING LLC 5853.00 2194.00 365
2018 ENERVEST OPERATING LLC 5117.00 1732.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2012 M & M ROYALTY LTD Brine 6020 366
2013 M & M ROYALTY LTD Brine 5243 365
2014 ENERVEST OPERATING LLC Brine 1517 292
2015 ENERVEST OPERATING LLC Brine 4546 365
2016 ENERVEST OPERATING LLC Brine 5662 366
2017 ENERVEST OPERATING LLC Brine 4739 365
2018 ENERVEST OPERATING LLC Brine 5386 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-279610662 2011-11-2 0:00: DD No Violations
0279610662 2011-11-02 Drill / Deepen / Reopen No Violations Cemented 4.5 casing. Drilling pits and liners are intact.
1319837133 2011-10-28 Drill / Deepen / Reopen No Violations Finished coring from 6259 - 6435. The rig tripped back into the hole but the bit became plugged which required the rig to trip out of the hole again.
1417796113 2014-12-05 Preliminary Restoration No Violations I was on location to pass preliminary restoration for this well. The lease road is graveled and has a gate. The tank battery is shared with well #25819 and contains six 210bbl production tanks, four separators, two brine knockout tanks and a 280bbl horizontal brine tank. The tank battery is contained in a dike and contains proper ID. The wellhead has ID, all proper gauges and valves and the pumpjack is natural gas driven. All spacing requirements between tanks, separators, wellhead and roadways meet requirements. There are no violations and preliminary restoration has been passed at this time.

For data sources see[9]

References