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| Well ID: 34-151-25025 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Marlboro Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: VAUGHAN K & D COMMUNITY # 4-11980 | |
| License Status: Producing | |
| License Date: 1996-12-23 | |
| Spud Date: 1997-05-12 | |
| Spud Drilling Contractor: ROSE RUN DRILLING | |
| Final Drill Date: 1997-05-20 | |
| Well Total Depth: 7369.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.940000 | |
| Longitude: -81.280000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1996-12-23 | 182 BELDEN & BLAKE CO GeoDate 12/23/96 |
| Oil and Gas | 1996-12-23 | Issued Date 12/23/96 Expired Date 12/23/97 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON/COPPER RG. Proposed Depth Proposed Drill Depth |
| Original Spud | 1997-05-12 | RBDMS Rec |
| Completed | 1997-05-20 | RBDMS Rec |
| Reached Total Depth | 1997-05-20 | RBDMS Rec |
| Completion Report Received | 1997-07-09 | RBDMS Rec |
| Construction Permit Expires | 1997-12-23 | RBDMS Rec |
| End of Confidential Data | 1998-05-20 | RBDMS Rec |
| Change of Owner | 2007-04-27 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC |
| Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-09-09 | 7201 | 7210 | 37 |
| 7201 | 7210 | 37 | |
| 7236 | 7241 | 21 | |
| 1997-09-09 | 7236 | 7241 | 21 |
| 7201 | 7210 | 37 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 46044 Gal | 25000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1997 | BELDEN & BLAKE CORPORATION | 4727.00 | 1241.00 | 154 |
| 1998 | BELDEN & BLAKE CORPORATION | 5016.00 | 2413.00 | 320 |
| 1999 | BELDEN & BLAKE CORPORATION | 2810.00 | 1869.00 | 233 |
| 2000 | BELDEN & BLAKE CORPORATION | 2562.00 | 1783.00 | 244 |
| 2001 | BELDEN & BLAKE CORPORATION | 3360.00 | 1814.00 | 389 |
| 2002 | BELDEN & BLAKE CORPORATION | 2829.00 | 1431.00 | 367 |
| 2003 | BELDEN & BLAKE CORPORATION | 2363.00 | 1283.00 | 362 |
| 2004 | BELDEN & BLAKE CORPORATION | 2201.00 | 1175.00 | 366 |
| 2005 | BELDEN & BLAKE CORPORATION | 2108.00 | 1128.00 | 365 |
| 2006 | BELDEN & BLAKE CORPORATION | 2208.00 | 773.00 | 365 |
| 2007 | ENERVEST OPERATING LLC | 2349.00 | 1045.00 | 365 |
| 2008 | ENERVEST OPERATING LLC | 2101.00 | 1065.00 | 365 |
| 2009 | ENERVEST OPERATING LLC | 2307.00 | 927.00 | 365 |
| 2010 | ENERVEST OPERATING LLC | 1251.00 | 887.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 150.00 | 754.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 0.00 | 574.00 | 366 |
| 2013 | ENERVEST OPERATING LLC | 0.00 | 597.00 | 365 |
| 2014 | ENERVEST OPERATING LLC | 1543.00 | 248.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 1715.00 | 212.00 | 365 |
| 2016 | ENERVEST OPERATING LLC | 808.00 | 98.00 | 366 |
| 2017 | ENERVEST OPERATING LLC | 706.00 | 0.00 | 365 |
| 2018 | ENERVEST OPERATING LLC | 725.00 | 101.00 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 0033679116 | 2002-07-31 | Production Wells | No Violations | NO VIOLATIONS. |
| 1026568913 | 2014-02-20 | Production Wells | No Violations | I was on location to follow up on complaint #4604. An employee of M D Body Corp stated that natural gas came into his paining room system from the air inlet fan and forced the shut down of the facility on Thursday February 13th. The fire department responded and used gas meters to test the area but no detectable levels were found. Dominion checked and tested the gas lines on location and also found no issues. The tank battery of concern is 900 from the inlet fan of the shop. The employee had a picture of the lid of the 210 bbl production tank open. During my inspection I found the lid to be closed and the valves on the vertical separator and the 100 bbl brine tank to be shut in. The well at this time is shut in. The pumpjack is in good mechanical condition at this time. I could not detect any gas with a PHD 6 gas detector at the shop, well or tank battery. I gave the employee my contact information and let him know that if the odor/leak occurs again to give me a call so that I can follow up on the complaint. |
| 1891766217 | 2014-03-10 | Production Wells | No Violations | I was on location to follow up on complaint #4604. An employee of M D Body Corp stated that natural gas came into his paining room system from the air inlet fan and forced the shut down of the facility on Thursday February 13th. The fire department responded and used gas meters to test the area but no detectable levels were found. Dominion checked and tested the gas lines on location and also found no issues. The tank battery of concern is 900 from the inlet fan of the shop. The employee had a picture of the lid of the 210 bbl production tank open. During my inspection I found the lid to be completely open while the well was producing. The pumpjack is in good mechanical condition at this time. I could not detect any gas with a PHD 6 gas detector at the shop, well or tank battery. 1501:9-9-05 (d) of the OAC states that Tank hatch lids shall have a functioning seal and the hatch shall be secured at all times the well owner or his representative is not on-site. Enervest will be informed of this and the latch on the production tank shall be closed during production to prevent any possible escaping of gas from the tank battery. |
| 33679116 | 2002-7-31 0:00: | PW | No Violations | 0.50 |
| iANGE00060 | 1997-09-15 | Preliminary Restoration | No Violations | |
| iANGE000604 | 1997-9-15 0:00: | PL | No Violations |
For data sources see[9]