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34-151-24146

Well Details

Well ID: 34-151-24146
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Country: United States
State: Ohio
County: Stark
Municipality: Nimishillen Township
Operator Name: DORFMAN PRODUCTION COMPANY
Well Pad ID:
Farm/Lease Name: WEISEND UNIT
License Status: Final Restoration
License Date: 2010-07-06
Spud Date: 1985-09-30
Spud Drilling Contractor: SHERMAN DRLG
Final Drill Date: 1985-10-04
Well Total Depth: 5084.00 ft
Configuration: Vertical
Latitude: 40.820000
Longitude: -81.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1985-04-16 Issued Date 4/16/85 Expired Date 10/13/85 Acres 0200720 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05084 Proposed Drill Depth 05084
Original Spud 1985-09-30 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
Completed 1985-10-04 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
Reached Total Depth 1985-10-04 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
CO 1985-10-23 134 PETROCON INC GeoDate 4/16/85
Completion Report Received 1985-10-24 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
Change of Owner 1997-11-06 Operator changed from 134, PETROCON INC to 180, DORFMAN PRODUCTION COMPANY
APP 2010-07-06 Proposed Formations:CLINTON, Issued Date:7/6/2010, Expired Date:7/6/2011 6:00:00 AM, Drilling unit acres:200.47, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2010-07-28 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
Construction Permit Expires 2011-07-06 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE
Record Last Modified 2017-05-18 LANDOWNER WAIVER TO LEAVE FLOWLINE IN PLACE

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4916 5012 56
4916 5012 56
4916 5012 56

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 7000 Bbl 220000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 PETROCON INC 257.00 299.00 69
1986 PETROCON INC 42080.00 3137.00 365
1987 PETROCON INC 8926.00 847.00 365
1988 PETROCON INC 5146.00 322.00 365
1989 PETROCON INC 3964.00 388.00 365
1990 PETROCON INC 6086.00 691.00 365
1991 PETROCON INC 4048.00 406.00 365
1992 PETROCON INC 3119.00 312.00 365
1993 PETROCON INC 2924.00 244.00 365
1994 PETROCON INC 1706.00 171.00 365
1995 PETROCON INC 1999.00 154.00 365
1996 PETROCON INC 1790.00 179.00 365
1997 PETROCON INC 1232.00 95.00 304
1998 DORFMAN PRODUCTION COMPANY 2168.00 113.00 365
1999 DORFMAN PRODUCTION COMPANY 2359.00 72.00 365
2000 DORFMAN PRODUCTION COMPANY 510.00 118.00 365
2001 DORFMAN PRODUCTION COMPANY 635.00 77.00 365
2002 DORFMAN PRODUCTION COMPANY 528.00 63.00 365
2003 DORFMAN PRODUCTION COMPANY 792.00 120.00 365
2004 DORFMAN PRODUCTION COMPANY 695.00 48.00 365
2005 DORFMAN PRODUCTION COMPANY 485.00 74.00 365
2006 DORFMAN PRODUCTION COMPANY 696.00 95.00 365
2007 DORFMAN PRODUCTION COMPANY 605.00 0.00 365
2008 DORFMAN PRODUCTION COMPANY 593.00 43.00 365
2009 DORFMAN PRODUCTION COMPANY 571.00 45.00 365
2010 DORFMAN PRODUCTION COMPANY 411.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 PETROCON INC Brine 230 69
1986 PETROCON INC Brine 6064 365
1987 PETROCON INC Brine 4140 365
1988 PETROCON INC Brine 1449 365
1989 PETROCON INC Brine 1815 365
1990 PETROCON INC Brine 1015 365
1991 PETROCON INC Brine 789 365
1992 PETROCON INC Brine 907 365
1993 PETROCON INC Brine 700 365
1994 PETROCON INC Brine 490 365
1995 PETROCON INC Brine 500 365
1996 PETROCON INC Brine 520 365
1997 PETROCON INC Brine 583 304
1998 DORFMAN PRODUCTION COMPANY Brine 716 365
1999 DORFMAN PRODUCTION COMPANY Brine 480 365
2000 DORFMAN PRODUCTION COMPANY Brine 508 365
2001 DORFMAN PRODUCTION COMPANY Brine 354 365
2002 DORFMAN PRODUCTION COMPANY Brine 481 365
2003 DORFMAN PRODUCTION COMPANY Brine 600 365
2004 DORFMAN PRODUCTION COMPANY Brine 663 365
2005 DORFMAN PRODUCTION COMPANY Brine 770 365
2006 DORFMAN PRODUCTION COMPANY Brine 893 365
2007 DORFMAN PRODUCTION COMPANY Brine 525 365
2008 DORFMAN PRODUCTION COMPANY Brine 175 365
2009 DORFMAN PRODUCTION COMPANY Brine 245 365
2010 DORFMAN PRODUCTION COMPANY Brine 177 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1191029119 2010-7-23 0:00: PB No Violations
-828912697 2006-3-28 0:00: PW No Violations
-908980816 2010-7-20 0:00: PB No Violations
0000PL5243 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0123770760 2004-10-07 Production Wells No Violations NO VIOLATIONS. GPS WH & TB (1-shared 210 bbl oil, 1-shared 100 bbl brine).
0437580959 2010-07-28 Plug / Plug Back No Violations Petroset pumped the Big Lime, Berea/8-5/8, and surface plugs. Circulated cement to surface.
0828912697 2006-03-28 Production Wells No Violations Random inspection. No violations at wellhead or at tank battery.
0908980816 2010-07-20 Plug / Plug Back No Violations The pumping unit, tubing, and rods have been removed. The 4-1/2 dia casing is ready to plug.
1103228649 2004-12-16 Production Wells Violations Noted Stuffing box is starting to leak. Clean up free crude and stained soil from in front of the WH. Met with Jamie the well tender.
1105730451 2005-01-14 Production Wells No Violations N.O.V. has been RESOLVED.
1191029119 2010-07-23 Plug / Plug Back No Violations The well was on vacuum this morning. I discussed the options with Paul Shaw and Greg New. Paul and Greg elected to shoot the 4-1/2 dia casing and set a 200 rip plug. Appalachian shot the casing at 3616, started out of the hole, and got hung at 3416. The service rig will run a line cutter on tubing on Monday.
123770760 2004-10-7 0:00: PW No Violations
1280350166 2010-07-27 Plug / Plug Back No Violations Retrieved 4-1/2 dia casing. Welded on a new collar. Shot 4-1/2 casing at 3333.
1487084089 2017-02-14 Final Restoration No Violations I conducted a final restoration inspection on this well. There is no visual evidence of this well. The site is graded and vegetated. A signed landowner waiver for the flowlines was received on 07-19-2010. The final restoration is passed.
1732618060 2008-10-10 Production Wells No Violations I did a random inspection in association with the Weisend # 4 complaint. There were no violations at the wellhead or at the tank battery.
2053184174 2010-07-26 Plug / Plug Back No Violations The service rig cut the line, leaving 27 of line, the collar locator, and the cutting tool inside of the casing. The rig pulled tubing and then pulled on the 4-1/2 dia casing and parted the casing at the threads on the top collar. The casing dropped thru and below the slips and head. The rig will get a center spear to stab into the casing on Tuesday.
437580959 2010-7-28 0:00: PB No Violations
PL5243 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1103228649 US-OH-102531 2004-12-16 Well operation causing pollution and contamination

For data sources see[9]

References