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34-151-23406

Well Details

Well ID: 34-151-23406
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Country: United States
State: Ohio
County: Stark
Municipality: Paris Township
Operator Name: PDL SERVICES INC
Well Pad ID:
Farm/Lease Name: FORESTER UNIT
License Status: Producing
License Date: 1996-01-02
Spud Date: 1980-12-01
Spud Drilling Contractor:
Final Drill Date: 1980-12-06
Well Total Depth: 5417.00 ft
Configuration: Vertical
Latitude: 40.750000
Longitude: -81.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1980-12-01
Completed 1980-12-06
Reached Total Depth 1980-12-06
CO 1980-12-08 198 VIKING RESOURCES CORP GeoDate 12/8/80
Oil and Gas 1980-12-08 Issued Date 12/8/80 Expired Date Acres 0080000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Completion Report Received 1981-02-23
CO 1988-11-17 198 VIKING RESOURCES CORP GeoDate 11/17/88
Unknown 1988-11-17 Issued Date 11/17/88 Expired Date 11/17/89 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1996-01-02 198 VIKING RESOURCES CORP GeoDate 1/2/96
Unknown 1996-01-02 Issued Date 1/2/96 Expired Date 1/1/97 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1996-10-16 3766 PDL SERVICES INC GeoDate 1/2/96
Construction Permit Expires 1997-01-01
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5284 5343 13
5284 5343 13
5284 5343 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 F/W WATER AND SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 VIKING RESOURCES LLC 3349.00 477.00 0
1985 VIKING RESOURCES LLC 2773.00 379.00 320
1986 VIKING RESOURCES LLC 3150.00 279.00 308
1987 VIKING RESOURCES LLC 1003.00 90.00 332
1988 VIKING RESOURCES LLC 1084.00 193.00 365
1989 VIKING RESOURCES LLC 372.00 0.00 174
1990 VIKING RESOURCES LLC 1702.00 268.00 0
1996 PDL SERVICES INC 0.00 209.00 60
2001 PDL SERVICES INC 733.00 0.00 365
2002 PDL SERVICES INC 629.00 0.00 365
2008 PDL SERVICES INC 342.00 50.00 365
2009 PDL SERVICES INC 438.00 56.00 365
2010 PDL SERVICES INC 434.00 55.00 365
2011 PDL SERVICES INC 1645.00 139.00 365
2012 PDL SERVICES INC 1606.00 109.00 366
2013 PDL SERVICES INC 1651.00 112.00 365
2014 PDL SERVICES INC 1586.00 103.00 365
2015 PDL SERVICES INC 240.00 0.00 365
2016 PDL SERVICES INC 239.00 0.00 365
2017 PDL SERVICES INC 29.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 VIKING RESOURCES LLC Brine 0 0
1985 VIKING RESOURCES LLC Brine 260 320
1986 VIKING RESOURCES LLC Brine 160 308
1987 VIKING RESOURCES LLC Brine 80 332
1988 VIKING RESOURCES LLC Brine 120 365
1989 VIKING RESOURCES LLC Brine 0 174
1990 VIKING RESOURCES LLC Brine 240 0
1996 PDL SERVICES INC Brine 350 60
2001 PDL SERVICES INC Brine 60 365
2002 PDL SERVICES INC Brine 0 365
2008 PDL SERVICES INC Brine 25 365
2009 PDL SERVICES INC Brine 25 365
2010 PDL SERVICES INC Brine 25 365
2011 PDL SERVICES INC Brine 2 365
2012 PDL SERVICES INC Brine 3 366
2013 PDL SERVICES INC Brine 4 365
2014 PDL SERVICES INC Brine 4 365
2015 PDL SERVICES INC Brine 0 365
2016 PDL SERVICES INC Brine 0 365
2017 PDL SERVICES INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1592063110 2004-3-10 0:00: PW No Violations
-847126967 2004-6-29 0:00: PW No Violations
0847126967 2004-06-29 Production Wells No Violations N.O.V. has been RESOLVED.
1475515510 2016-09-23 Production Wells No Violations I conducted a status check inspection on this well after receiving a phone call from the landowner. The landowners concern was that the well was leaking into her pond. I contacted PDL Services and they advised me they had sent someone to clean-up the site and to make sure it was not leaking beyond the well dike. When I arrived on location a worker was cleaning up the area around the wellhead. There is evidence that the well was leaking from the stuffing box. The contminated area is located in an area approximately 2ft. x 4ft. area aorund the wellhead. My investigation found no evidence of the well leaking to the pond which is located downhill ~ 300 ft. Northwest of the well which is diked. I met with the landowners and advised them of my findings and gave them my business card. The following ODNR personnel were contacted: Rick Anderson (District Supervisor), Tom Hill (Regional Supervisor), Terry White (emergency response), and a message was left on the duty line.
1592063110 2004-03-10 Production Wells Violations Noted Stuffing box is leaking. Remove oil and paraffin from around the wellhead and remove any stained soil. GPS WH & TB (1-210, 1 brine vault).

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1592063110 US-OH-115572 2004-03-11 Well operation causing pollution and contamination

For data sources see[9]

References