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| Well ID: 34-149-20075 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Shelby | |
| Municipality: Van Buren Township | |
| Operator Name: EGBERT DAVID A | |
| Well Pad ID: | |
| Farm/Lease Name: EGBERT ALVIN & BARBARA | |
| License Status: Final Restoration | |
| License Date: 2012-11-30 | |
| Spud Date: | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1980-11-15 | |
| Well Total Depth: 1204.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.470000 | |
| Longitude: -84.300000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Completed | 1980-11-15 | |
| Reached Total Depth | 1980-11-15 | |
| Completion Report Received | 1982-06-11 | |
| Change of Owner | 2012-11-20 | Operator changed from 9998, HISTORIC OWNER to 9064, EGBERT DAVID A |
| APP | 2012-11-30 | Proposed Formations:TRENTON, Issued Date:11/30/2012, Expired Date:11/30/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2013-01-25 | |
| Construction Permit Expires | 2014-11-30 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| N2 | 0 | 90 Qts | 0 |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1986 | LARRY H WRIGHT INC | 0.00 | 298.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1986 | LARRY H WRIGHT INC | Brine | 110 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1529269070 | 2012-12-3 0:00: | PW | No Violations | 1.00 |
| -1588218405 | 2013-1-31 0:00: | FR | No Violations | 1.00 |
| 0516317132 | 2013-01-29 | Plug / Plug Back | No Violations | Reinspection of this well that was plugged with cement on 01/25/2013. The plug fell back 26, Knox Energy is topping off the plug with sack crete. 15 bags of concrete was used to top off the plug. |
| 1500823490 | 2013-01-25 | Plug / Plug Back | No Violations | Knox energy has made a attempt to remove the 6 casing before plugging. They were able to unscrew two joints of pipe. Cement plugs are in place, plugs did circulate. |
| 1529269070 | 2012-12-03 | Production Wells | No Violations | I received a plug permit for this historic production well, the well is not capable of production, there is a pumping unit and one 100 barrel tank. |
| 1588218405 | 2013-01-31 | Final Restoration | No Violations | I have received a landowner waiver for this site, the waiver is for seeding and mulching. All production equipment has been removed from the site, the well is plugged. |
| 516317132 | 2013-1-29 0:00: | PB | No Violations | 1.00 |
For data sources see[8]