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34-145-20230

Well Details

Well ID: 34-145-20230
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Country: United States
State: Ohio
County: Scioto
Municipality: Harrison Township
Operator Name: ODOT DISTRICT 9
Well Pad ID:
Farm/Lease Name: GAHM ROY
License Status: Final Restoration
License Date: 1973-09-19
Spud Date: 1973-11-07
Spud Drilling Contractor:
Final Drill Date: 1973-12-08
Well Total Depth: 397.00 ft
Configuration: Vertical
Latitude: 38.860000
Longitude: -82.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1973-11-07
Completed 1973-12-08
Reached Total Depth 1973-12-08
Change of Owner 2015-08-13 CHANGE OF OWNER FROM HISTORIC OWNER (#9998) TO ODOT DISTRICT 9 (#9518). OPERATOR APPLIED FOR PLUGGING PERMIT FOR THE WRONG WELL.
Plugged/Abandoned 2015-08-20
Record Last Modified 2017-02-10

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1278208377 2015-4-1 0:00:0 PW No Violations 3.50
-1500110614 2014-8-6 0:00:0 PW No Violations 1.00
-1867966681 2015-10-6 0:00: PB No Violations 4.00
-298149366 2015-8-12 0:00: PB No Violations 0.70
0091652164 2014-08-14 Production Wells No Violations Well site has 5 foot vegetation growing in the field. Located well for ODOT plugging contractor. Well site is now marked with orange tape attached to 9 foot stick that was attached to the 4.5 casing with tape.
0298149366 2015-08-12 Plug / Plug Back No Violations ODOT applied for the incorrect API number to plug this well and I met with the ODOT rep at the well to correct the issue. There appears to be cement concrete between the 4 1/2 casing and the 6 5/8 casing.
0463657471 2015-08-13 Plug / Plug Back No Violations After the correct application had been received and verified in Columbus a VDL log was ran inside the 4 1/2 production casing to TD at 392 feet.
0646420579 2015-10-08 Plug / Plug Back No Violations The sleeve of 40 mil plastic liner was sealed around the riser pipe today for the gas collection system.
0731597098 2015-10-07 Plug / Plug Back No Violations Witnessed construction of the gas collection apparatus and the vent stack being placed at well. during previous inspections at the well it was noted the grade has been brought up around the site and water and silt has covered the cut off casing. Nothing out of the ordinary was noted during these inspections. An area around the well was dug out today and during this process I noted a few small sporadic bubbles coming to surface in the casing. Work was stopped and I used a trowel to remove debris and some gravel from inside the casing. As the debris was loosened more bubbles were noted escaping, my gas meter read zero for LEL, and after the debris was removed the bubbles stopped. I notified our plugging specialist and my supervisor of the occurrence, it was determined it was small pockets of trapped air associated with the debris.
0919761552 2011-03-16 Production Wells No Violations ODOT well no change since last inspection.
1172079974 2007-02-15 Production Wells No Violations Well is located in a field. Flat land, no trees. 4.5 casing sticking up in the air 2 Well has a plug in the top with a .5 hole in it. Can smell natural gas coming from the well. Well is approximatly 100 behind the barn. This inspection was requested by ODOT they have purchased the land and are going to plug the well.
1206970086 2008-03-04 Production Wells No Violations Well is disconnected. This well is to be plugged by ODOT. The well is not leaking. I painted the well orange.
1263561810 2010-01-14 Production Wells No Violations Well is to be plugged by ODOT. Robert Stonerock accompanied me on the inspection. Well is idle with no id. Well is not connected to production lines or equipment. No production equipment is on location.
1278208377 2015-04-01 Production Wells No Violations Met with Pat Shreve to discuss plugging of well.
1427301682 2015-03-24 Production Wells No Violations Met with company representative and DOT representative to discuss plugging options for the well as part of a package to put in Portsmouth Bi-pass. Well is equipped with 57 of 6 5/8 surface casing and 210 of 4 1/2 production casing.
1429634388 2015-04-01 Production Wells No Violations Josh Garland and I looked at the well that will be bidded out and plugged by ODOT and revealed the following: The old 4.5casing had a bull plug at the top with a.75tap. The 4.5casing is inside of 6.625casing.
1440436891 2015-08-20 Plug / Plug Back No Violations Witnessed plug job. Ran 1 tubing to a depth of 380 feet, cleaned out the hole with 10 Bbl fresh water, and circulated 50 sacks Class A cement to surface.
1500110614 2014-08-06 Production Wells No Violations Production well inspection. I received a request from Joe Senita. Joe is with AMEC engineering. He wanted to know the well location and condition. He is working on a road widening plan for ODOT. The well was not located due to 5 tall vegetation. I spent one hour looking. I will return when the vegetation is down.
1545295095 2015-08-19 Plug / Plug Back No Violations Witnessed plug job. Rigged up and pulled on the 4 1/2 line pipe, no stretch. There appears to be cement between the 4 1/2 casing and the 6 5/8 at the surface. The VDL shows a possible area of bond from 125 to surface and good bond from TD to 210. I had the crew dig down four feet and cut a hole into the surface casing at 36 inches to verify wether of not there was cement in the annulus. The hole shows there was cement inside at three feet. Kilbargers placed shots through out the 4 1/2 casing at 15, 30, 55, 70, 90, 110, 140, 160, 180, 200, 220, 240, 260, 310, 326, 340, 360, 370, and 380 feet.
1609501214 2016-03-10 Final Restoration No Violations On my inspection I found that the location had been restored according to 1509.072. I passed the final restoration at this time.
1656704506 2015-09-24 Plug / Plug Back No Violations The grade has been brought up about 15 feet above the well head. Water around well, unable to see casing.
1867966681 2015-10-06 Plug / Plug Back No Violations Arrived on site to witness installation of Vault and Vent system, the job was delayed and canceled for the day.
463657471 2015-8-13 0:00: PB No Violations 1.30
646420579 2015-10-8 0:00: PB No Violations 4.00
731597098 2015-10-7 0:00: PB No Violations 8.50
91652164 2014-8-14 0:00: PW No Violations 2.00
919761552 2011-3-16 0:00: PW No Violations

For data sources see[3]

References