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34-133-24414

Well Details

Well ID: 34-133-24414
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Country: United States
State: Ohio
County: Portage
Municipality: Suffield Township
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID: US-OH-000600
Farm/Lease Name: HOSEY POR
License Status: Final Restoration
License Date: 2011-06-13
Spud Date: 2011-08-08
Spud Drilling Contractor:
Final Drill Date: 2011-08-15
Well Total Depth: 67.00 ft
Configuration: Vertical
Latitude: 40.990000
Longitude: -81.330000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-06-13 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:6/13/2011, Expired Date:6/12/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
Reached Total Depth 2011-08-15
Plugged/Abandoned 2011-08-16
Construction Permit Expires 2012-06-12
Completion Report Received 2012-09-13
Record Last Modified 2015-09-24

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1282268950 2011-8-16 0:00: FR No Violations
-1502062296 2011-8-16 0:00: PL No Violations
-448685047 2011-8-16 0:00: FR No Violations
0046269731 2011-08-16 Plug / Plug Back No Violations I witnessed the plugging of the 30 conductor down 67 by Medina Ready mix company. The Medina Ready mix used 3500mix cement(10 yards) to dump down the conductor. The cement came to the top of the 30 conductor. There were no violations at this time.
0448685047 2011-08-16 Final Restoration No Violations The old well down to 67 has been plugged. This well has PASSED FINAL RESTORATION.
1136431785 2011-08-01 Surface Facility Construction No Violations I performed a status check on this well. The lease road had rocks part way into the drilling location. The drilling location had dirt only. There were no violations at this time.
1282268950 2011-08-16 Final Restoration No Violations The old well down to 67 has been plugged. This well has PASSED FINAL RESTORATION.
1312310479 2011-08-02 Surface Facility Construction No Violations The lease road into the drilling pad is complete. There are no rocks on the drilling pad yet. There were no violations at this time.
1312825278 2011-08-08 Drill / Deepen / Reopen No Violations The Rat Hole rig KOD has spud in drilling a 30 hole. The rig is mounted on a track hole. It is a ogger machine. The rig drilled to a depth of 67. Ran 2 joints of 30, 116# conductor. Set at 67. Tex OK started to pumped fresh water to brake circulation. There were two pen holes in the conductor above the ground. Pumping stopped. A welder came out to weld pen holes. It started a HEAVY RAIN. This caused the ground around the cellar to fall in. Operations stopped. Chesapeake will address the situation at day light. The area around the cellar was fenced off. There were no violations at this time.
1312911162 2011-08-09 Drill / Deepen / Reopen No Violations This conductor operation continued from 8/8/11. There were no violations at this time.
1313598425 2011-08-15 Drill / Deepen / Reopen No Violations BJ cementing tried to pump into the 30 conductor to brake circulation. BJ pressured up to 40psi. The top of the conductor started to bow out. BJ shut down. Chesapeake will regroup and try to find out what to do next. Rick Been called me and told me that they would plug the 30 conductor down to 67. I agreed. I called Rick Simmers let him know what was going on with the operations. He agreed with plugging the well. The plugging would occur tomorrow. There were no violationsa at this time.
1313748781 2011-08-16 Preliminary Restoration No Violations The new well will be restacked 10 feet to the south. This well has PASSED PRELIMINARY RESTORATION.
1502062296 2011-08-16 Preliminary Restoration No Violations The new well will be restacked 10 feet to the south. This well has PASSED PRELIMINARY RESTORATION.
1920822054 2011-08-16 Plug / Plug Back No Violations I witnessed the plugging of the 30 conductor down 67 by Medina Ready mix company. The Medina Ready mix used 3500mix cement(10 yards) to dump down the conductor. The cement came to the top of the 30 conductor. There were no violations at this time.
46269731 2011-8-16 0:00: PB No Violations

For data sources see[3]

References