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Well ID: 34-133-24414 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Suffield Township | |
Operator Name: CHESAPEAKE EXPLORATION LLC | |
Well Pad ID: US-OH-000600 | |
Farm/Lease Name: HOSEY POR | |
License Status: Final Restoration | |
License Date: 2011-06-13 | |
Spud Date: 2011-08-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 2011-08-15 | |
Well Total Depth: 67.00 ft | |
Configuration: Vertical | |
Latitude: 40.990000 | |
Longitude: -81.330000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-06-13 | Proposed Formations:TRENTON-BLACK RIVER, Issued Date:6/13/2011, Expired Date:6/12/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Reached Total Depth | 2011-08-15 | |
Plugged/Abandoned | 2011-08-16 | |
Construction Permit Expires | 2012-06-12 | |
Completion Report Received | 2012-09-13 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1282268950 | 2011-8-16 0:00: | FR | No Violations | |
-1502062296 | 2011-8-16 0:00: | PL | No Violations | |
-448685047 | 2011-8-16 0:00: | FR | No Violations | |
0046269731 | 2011-08-16 | Plug / Plug Back | No Violations | I witnessed the plugging of the 30 conductor down 67 by Medina Ready mix company. The Medina Ready mix used 3500mix cement(10 yards) to dump down the conductor. The cement came to the top of the 30 conductor. There were no violations at this time. |
0448685047 | 2011-08-16 | Final Restoration | No Violations | The old well down to 67 has been plugged. This well has PASSED FINAL RESTORATION. |
1136431785 | 2011-08-01 | Surface Facility Construction | No Violations | I performed a status check on this well. The lease road had rocks part way into the drilling location. The drilling location had dirt only. There were no violations at this time. |
1282268950 | 2011-08-16 | Final Restoration | No Violations | The old well down to 67 has been plugged. This well has PASSED FINAL RESTORATION. |
1312310479 | 2011-08-02 | Surface Facility Construction | No Violations | The lease road into the drilling pad is complete. There are no rocks on the drilling pad yet. There were no violations at this time. |
1312825278 | 2011-08-08 | Drill / Deepen / Reopen | No Violations | The Rat Hole rig KOD has spud in drilling a 30 hole. The rig is mounted on a track hole. It is a ogger machine. The rig drilled to a depth of 67. Ran 2 joints of 30, 116# conductor. Set at 67. Tex OK started to pumped fresh water to brake circulation. There were two pen holes in the conductor above the ground. Pumping stopped. A welder came out to weld pen holes. It started a HEAVY RAIN. This caused the ground around the cellar to fall in. Operations stopped. Chesapeake will address the situation at day light. The area around the cellar was fenced off. There were no violations at this time. |
1312911162 | 2011-08-09 | Drill / Deepen / Reopen | No Violations | This conductor operation continued from 8/8/11. There were no violations at this time. |
1313598425 | 2011-08-15 | Drill / Deepen / Reopen | No Violations | BJ cementing tried to pump into the 30 conductor to brake circulation. BJ pressured up to 40psi. The top of the conductor started to bow out. BJ shut down. Chesapeake will regroup and try to find out what to do next. Rick Been called me and told me that they would plug the 30 conductor down to 67. I agreed. I called Rick Simmers let him know what was going on with the operations. He agreed with plugging the well. The plugging would occur tomorrow. There were no violationsa at this time. |
1313748781 | 2011-08-16 | Preliminary Restoration | No Violations | The new well will be restacked 10 feet to the south. This well has PASSED PRELIMINARY RESTORATION. |
1502062296 | 2011-08-16 | Preliminary Restoration | No Violations | The new well will be restacked 10 feet to the south. This well has PASSED PRELIMINARY RESTORATION. |
1920822054 | 2011-08-16 | Plug / Plug Back | No Violations | I witnessed the plugging of the 30 conductor down 67 by Medina Ready mix company. The Medina Ready mix used 3500mix cement(10 yards) to dump down the conductor. The cement came to the top of the 30 conductor. There were no violations at this time. |
46269731 | 2011-8-16 0:00: | PB | No Violations |
For data sources see[3]