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Well ID: 34-133-23151 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Freedom Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER-WRIGHT UNIT | |
License Status: Producing | |
License Date: 1983-11-22 | |
Spud Date: 1984-03-15 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 1984-03-22 | |
Well Total Depth: 4510.00 ft | |
Configuration: Vertical | |
Latitude: 41.240000 | |
Longitude: -81.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-11-22 | Issued Date 11/22/83 Expired Date 5/20/84 Acres 0050144 Tool Type RTF Proposed Formation CLINTON Proposed Depth 04510 Proposed Drill Depth 04510 |
Original Spud | 1984-03-15 | |
Completed | 1984-03-22 | |
Reached Total Depth | 1984-03-22 | |
Construction Permit Expires | 1984-05-20 | |
CO | 1984-06-07 | 132 NOBLE OIL CORP GeoDate 11/22/83 |
Completion Report Received | 1984-06-15 | |
CO | 1996-06-07 | 4884 EASTERN STATES OIL & GAS GeoDate 11/22/83 |
Change of Owner | 2003-04-09 | Operator changed from 4884, EASTERN STATES OIL & GAS INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4341 | 4481 | 0 |
4341 | 4481 | 0 | |
2006-09-11 | 4378 | 4420 | 18 |
4378 | 4420 | 18 | |
4341 | 4481 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 500 Gal | 0 | FRAC;H2O,SAND,ACID | ||
H2O | 0 | 1800 Bbl | 55000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | NOBLE OIL CORP | 5425.00 | 923.00 | 0 |
1985 | NOBLE OIL CORP | 4174.00 | 917.00 | 300 |
1986 | NOBLE OIL CORP | 2517.00 | 662.00 | 365 |
1987 | NOBLE OIL CORP | 1627.00 | 557.00 | 365 |
1989 | NOBLE OIL CORP | 879.00 | 468.00 | 365 |
1990 | NOBLE OIL CORP | 658.00 | 273.00 | 365 |
1991 | NOBLE OIL CORP | 452.00 | 394.00 | 365 |
1992 | NOBLE OIL CORP | 198.00 | 200.00 | 365 |
1993 | NOBLE OIL CORP | 0.00 | 292.00 | 365 |
1994 | NOBLE OIL CORP | 1068.00 | 255.00 | 365 |
1995 | NOBLE OIL CORP | 435.00 | 357.00 | 365 |
1996 | EASTERN STATES OIL & GAS INC | 191.00 | 299.00 | 365 |
1997 | EASTERN STATES OIL & GAS INC | 49.00 | 313.00 | 365 |
1998 | EASTERN STATES OIL & GAS INC | 2652.00 | 289.00 | 365 |
1999 | EASTERN STATES OIL & GAS INC | 1112.00 | 194.00 | 365 |
2000 | EASTERN STATES OIL & GAS INC | 617.00 | 0.00 | 365 |
2001 | EASTERN STATES OIL & GAS INC | 784.00 | 3106.00 | 365 |
2002 | EASTERN STATES OIL & GAS INC | 1347.00 | 221.00 | 365 |
2003 | EASTERN STATES OIL & GAS INC | 57.00 | 50.00 | 59 |
2004 | RANGE RESOURCES-APPALACHIA LLC | 359.00 | 164.00 | 303 |
2005 | RANGE RESOURCES-APPALACHIA LLC | 906.00 | 253.00 | 365 |
2006 | RANGE RESOURCES-APPALACHIA LLC | 35.00 | 38.00 | 243 |
2007 | RANGE RESOURCES-APPALACHIA LLC | 805.00 | 119.00 | 334 |
2008 | RANGE RESOURCES-APPALACHIA LLC | 11.00 | 0.00 | 30 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 296.00 | 35.00 | 365 |
2015 | ENERVEST OPERATING LLC | 9.00 | 0.00 | 365 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
2017 | ENERVEST OPERATING LLC | 183.00 | 0.00 | 365 |
2018 | ENERVEST OPERATING LLC | 247.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL6136 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0319223626 | 2013-10-09 | Production Wells | No Violations | I inspected this well at the request of the landowner. He was concerned about a possible gas leak and the condition of the tank battery. I inspected the location and found a diked tank battery containing a 100 barrel stock tank and a 30-40 barrel tank. There was a horizontal separator and chart box in the battery as well as 2 domestic meters reading 9psi and 7psi. The chart has not been changed recently and the last commercial production reported from this well was in 2007. The heater tube on the 100 barrel appears to have a leak and there is sludge in the end of the tube. The ID on the tank is badly worn and indicates Great Lakes as the owner of the well. The overall appearance of the battery is overgrown and the equipment requires maintenance. The wellhead consists of a pumping unit that is badly overgrown with weeds and the belt on the motor is broken. I walked the entire location with a PHD6 gas meter looking for leaks in the wellhead, flow lines, and at the tank battery. I detected 0.05ppm of methane near the Big Joe regulator in the tank battery and no LEL. I did not detect methane anywhere else on location. I spoke with Enervest about getting this well back in production and addressing the issues I found on location. I also asked them to test the flow lines to assure that nothing is leaking. I will monitor their progress to see that the issues are fixed. |
319223626 | 2013-10-9 0:00: | PW | No Violations | |
PL6136 | PL | No Violations |
For data sources see[9]