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34-127-27410

Well Details

Well ID: 34-127-27410
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Country: United States
State: Ohio
County: Perry
Municipality: Harrison Township
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name: LEWIS-FRECO UNIT
License Status: Final Restoration
License Date: 2014-07-29
Spud Date: 2014-09-11
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2014-09-30
Well Total Depth: 4125.00 ft
Configuration: Vertical
Latitude: 39.800000
Longitude: -82.120000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-07-29 Proposed Formations:KNOX, Issued Date:7/29/2014, Expired Date:7/28/2016 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2014-09-30

-10/2/2014

Plugged/Abandoned 2014-10-01

-10/2/2014

Construction Permit Expires 2016-07-28

-10/2/2014

Record Last Modified 2017-10-23

-10/2/2014

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-305911437 2015-6-25 0:00: FR No Violations 1.00
-434494346 2014-9-18 0:00: DD No Violations 1.50
-770282378 2014-9-24 0:00: DD No Violations 1.00
0305911437 2015-06-25 Final Restoration No Violations The final restoration of this well meets 1509.072b.
0434494346 2014-09-18 Drill / Deepen / Reopen No Violations I stopped by this well to check on the status of the drilling. They are drilling at a depth of 2,457ft. They said it would be a couple of days before they reached TD.
0770282378 2014-09-24 Drill / Deepen / Reopen No Violations I stopped by to see how the drilling was going on this well. Kilbarger drilling is at a depth of 4085ft during my field inspection. The rig has been overheating making it hard for them to drill.
1822086274 2014-09-30 Plug / Plug Back No Violations While Kilbarger was drilling this hole the drill pipe twisted off. Artex and Kilbarger spent 5 days on trying to retrieve the drill pipe. They were not able to recover the pipe so we had to plug the well. The pipe ripped off at 3,333ft. A 200ft plug was set at 3,333-3133ft. The Lime plug was set at 2704-2504ft. The Berea was covered with 1228-1078ft. The bottom of the surface casing was covered with 783-513ft and a 256ft surface plug was set.
1872105503 2014-09-13 Casing String Witnessed No Violations I was onsite to witness the 8-5/8 surface casing being cemented to surface. Kilbarger drilled to a depth of 646ft. They ran a total of 620ft of 8-5/8, 23lbm/ft casing in the well. Formation Cementing used 205ks of Class A Cement, 400lbs gel, 60lbs L.C.M Cotton seed hulls, 50lbs L.C.M Flake and 350lbs accelerator. We had 6-bbl returns of cement to the surface.

For data sources see[3]

References