If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-127-27410 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.8,"lon":-82.12,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Harrison Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: LEWIS-FRECO UNIT | |
License Status: Final Restoration | |
License Date: 2014-07-29 | |
Spud Date: 2014-09-11 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2014-09-30 | |
Well Total Depth: 4125.00 ft | |
Configuration: Vertical | |
Latitude: 39.800000 | |
Longitude: -82.120000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-07-29 | Proposed Formations:KNOX, Issued Date:7/29/2014, Expired Date:7/28/2016 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2014-09-30
-10/2/2014 | |
Plugged/Abandoned | 2014-10-01
-10/2/2014 | |
Construction Permit Expires | 2016-07-28
-10/2/2014 | |
Record Last Modified | 2017-10-23
-10/2/2014 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-305911437 | 2015-6-25 0:00: | FR | No Violations | 1.00 |
-434494346 | 2014-9-18 0:00: | DD | No Violations | 1.50 |
-770282378 | 2014-9-24 0:00: | DD | No Violations | 1.00 |
0305911437 | 2015-06-25 | Final Restoration | No Violations | The final restoration of this well meets 1509.072b. |
0434494346 | 2014-09-18 | Drill / Deepen / Reopen | No Violations | I stopped by this well to check on the status of the drilling. They are drilling at a depth of 2,457ft. They said it would be a couple of days before they reached TD. |
0770282378 | 2014-09-24 | Drill / Deepen / Reopen | No Violations | I stopped by to see how the drilling was going on this well. Kilbarger drilling is at a depth of 4085ft during my field inspection. The rig has been overheating making it hard for them to drill. |
1822086274 | 2014-09-30 | Plug / Plug Back | No Violations | While Kilbarger was drilling this hole the drill pipe twisted off. Artex and Kilbarger spent 5 days on trying to retrieve the drill pipe. They were not able to recover the pipe so we had to plug the well. The pipe ripped off at 3,333ft. A 200ft plug was set at 3,333-3133ft. The Lime plug was set at 2704-2504ft. The Berea was covered with 1228-1078ft. The bottom of the surface casing was covered with 783-513ft and a 256ft surface plug was set. |
1872105503 | 2014-09-13 | Casing String Witnessed | No Violations | I was onsite to witness the 8-5/8 surface casing being cemented to surface. Kilbarger drilled to a depth of 646ft. They ran a total of 620ft of 8-5/8, 23lbm/ft casing in the well. Formation Cementing used 205ks of Class A Cement, 400lbs gel, 60lbs L.C.M Cotton seed hulls, 50lbs L.C.M Flake and 350lbs accelerator. We had 6-bbl returns of cement to the surface. |
For data sources see[3]