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Well ID: 34-127-26437 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Thorn Township | |
Operator Name: MH OILFIELD SERVICE LLC | |
Well Pad ID: | |
Farm/Lease Name: WALSER RUSSELL | |
License Status: Producing | |
License Date: 1985-11-19 | |
Spud Date: 1984-10-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1984-11-10 | |
Well Total Depth: 2700.00 ft | |
Configuration: Vertical | |
Latitude: 39.910000 | |
Longitude: -82.370000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-09-12 | Issued Date 9/12/84 Expired Date 3/11/85 Acres 0020000 Tool Type CRA Proposed Formation CLINTON Proposed Depth 02700 Proposed Drill Depth 02700 |
Original Spud | 1984-10-26 | |
Completed | 1984-11-10 | |
Reached Total Depth | 1984-11-10 | |
CO | 1984-11-21 | 526 MID-CON PETROLEUM CO INC GeoDate 9/12/84 |
CO | 1985-11-19 | 75 BARCLAY PETROLEUM INC GeoDate 11/19/85 |
Unknown | 1985-11-19 | Issued Date 11/19/85 Expired Date 11/19/86 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Completion Report Received | 1986-02-13 | |
Construction Permit Expires | 1986-11-19 | |
Change of Owner | 2017-11-27 | Operator changed from 75, BARCLAY PETROLEUM INC to 8277, MH OILFIELD SERVICE LLC |
Record Last Modified | 2017-11-27 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2601 | 2620 | 19 |
2601 | 2620 | 19 | |
2601 | 2620 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
GEL | 0 | 2000 Lbs | 0 | |||
H2O | 0 | 1500 Bbl | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MID-CON PETROLEUM CO INC | 9229.00 | 0.00 | 365 |
1986 | MID-CON PETROLEUM CO INC | 5085.00 | 71.00 | 365 |
1987 | MID-CON PETROLEUM CO INC | 2720.00 | 53.00 | 365 |
1988 | MID-CON PETROLEUM CO INC | 2101.00 | 25.00 | 365 |
1989 | BARCLAY PETROLEUM INC | 265.00 | 0.00 | 365 |
1990 | BARCLAY PETROLEUM INC | 1180.00 | 0.00 | 365 |
1991 | BARCLAY PETROLEUM INC | 900.00 | 0.00 | 340 |
1992 | BASS ENERGY CO INC | 848.00 | 0.00 | 365 |
1993 | BARCLAY PETROLEUM INC | 1166.00 | 50.00 | 365 |
1994 | BARCLAY PETROLEUM INC | 998.00 | 0.00 | 300 |
1995 | BARCLAY PETROLEUM INC | 913.00 | 0.00 | 300 |
1996 | BARCLAY PETROLEUM INC | 614.00 | 0.00 | 366 |
1997 | BARCLAY PETROLEUM INC | 319.00 | 0.00 | 365 |
1998 | BARCLAY PETROLEUM INC | 153.00 | 0.00 | 365 |
1999 | BARCLAY PETROLEUM INC | 655.00 | 0.00 | 365 |
2000 | BARCLAY PETROLEUM INC | 573.00 | 0.00 | 365 |
2001 | BARCLAY PETROLEUM INC | 537.00 | 0.00 | 365 |
2002 | BARCLAY PETROLEUM INC | 648.00 | 0.00 | 365 |
2003 | BARCLAY PETROLEUM INC | 276.00 | 0.00 | 180 |
2004 | BARCLAY PETROLEUM INC | 251.00 | 0.00 | 105 |
2005 | BARCLAY PETROLEUM INC | 225.00 | 0.00 | 365 |
2006 | BARCLAY PETROLEUM INC | 249.00 | 0.00 | 365 |
2007 | BARCLAY PETROLEUM INC | 273.00 | 0.00 | 365 |
2008 | BARCLAY PETROLEUM INC | 294.00 | 0.00 | 365 |
2009 | BARCLAY PETROLEUM INC | 321.00 | 0.00 | 365 |
2010 | BARCLAY PETROLEUM INC | 303.00 | 0.00 | 365 |
2011 | BARCLAY PETROLEUM INC | 223.00 | 0.00 | 365 |
2012 | BARCLAY PETROLEUM INC | 207.00 | 0.00 | 366 |
2013 | BARCLAY PETROLEUM INC | 106.00 | 0.00 | 365 |
2014 | BARCLAY PETROLEUM INC | 145.00 | 0.00 | 365 |
2015 | BARCLAY PETROLEUM INC | 270.00 | 0.00 | 365 |
2016 | BARCLAY PETROLEUM INC | 233.00 | 0.00 | 365 |
2017 | BARCLAY PETROLEUM INC | 121.00 | 0.00 | 180 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1068818849 | 2015-2-24 0:00: | PW | No Violations | 1.50 |
-1310798335 | 2017-3-24 0:00: | PW | No Violations | 1.00 |
-872989872 | 2015-2-20 0:00: | PW | No Violations | 1.50 |
0000PL6711 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0484820446 | 2009-05-11 | Production Wells | No Violations | Follow-up on NOV, Non-Compliance, will send company a letter about violations. |
0491781023 | 2019-01-03 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well appears to be in production. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the wellhead to the production tank. There is 1-100 barrel storage tank located at the end of the lease road. The well looks like it is providing domestic gas. There are no violations at this time. |
0845614018 | 2006-04-27 | Production Wells | Violations Noted | An inspection of the well revealed no ID at the well head. |
0872989872 | 2015-02-20 | Production Wells | No Violations | I returned to this well to see if the oil around the well had been cleaned up. The oil was still on location but was frozen. I contacted Bruce Kelley and he said he was at the well yesterday afternoon to see what he needed to clean it up and to grab the broken belts. He will be out at the well today to clean it up and put the new belts on. |
0884967777 | 2009-03-12 | Production Wells | Violations Noted | An inspection of the well revealed ID needs rewrote at well and tank battery. Oily material around tanks and in dike at tank battery. Production tank bottom starting to leak. |
1068818849 | 2015-02-24 | Production Wells | No Violations | I returned to the well to make sure the contamination was removed. The well is in-compliance and was pumping during my follow-up. |
1116433931 | 2020-7-9 0:00:0 | PW | No Violations | 0.50 |
1244117879 | 2009-06-02 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
1310798335 | 2017-03-24 | Production Wells | No Violations | The purpose of my visit today on this location was to conduct a field inspection on this well. The state of the well at this current time appears to be in production. The well currently has a pumping unit on it with rods and tubing down hole. The valves coming from the wellhead to the tank battery are open at this time. This will allow for the production of this well to reach the sales line making the well capable of production. The identification for this well is located at the production tank. There are no violations at this time. |
1461129907 | 2015-02-19 | Production Wells | Violations Noted | During the e field inspection of this well I found the stuffing box has started to leak. I contacted Bruce Kelly to let him know there is oil around the well. He said he would be out to clean it up. He is going to remove the contamination around the well. There is approximately 4-5gal around the well. The belts broke on the pulley and the motor was running so I asked him if he wanted me to shut it down. I shut the well off and he will fix the belts. I will return to this well tomorrow to check it. |
1881690066 | 2016-04-21 | Production Wells | No Violations | This well was pumping during the time of my inspection. The well has a pumping unit on it with rods and 2 tubing in it. The identification for the well was located on the tank pad. There are no violations to report at tis time. |
2080301577 | 2006-08-01 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
484820446 | 2009-5-11 0:00: | PW | No Violations | |
491781023 | 2019-1-3 0:00:0 | PW | No Violations | 0.40 |
845614018 | 2006-4-27 0:00: | PW | No Violations | |
884967777 | 2009-3-12 0:00: | PW | No Violations | |
PL6711 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0845614018 | US-OH-129629 | 2006-05-01 | Failure to legibly identify well | |
0884967777 | US-OH-130072 | 2009-03-13 | Well operation causing pollution and contamination | |
0884967777 | US-OH-130073 | 2009-03-13 | Well insufficiently equipped to prevent escape of oil and gas | |
0884967777 | US-OH-130074 | 2009-03-13 | Failure to legibly identify well | |
0884967777 | US-OH-130075 | 2009-03-13 | Equipment pressure rated below operating pressure | |
0884967777 | US-OH-130076 | 2009-03-13 | No SPCC dike/or failure to keep dike free of water or oil | |
1461129907 | US-OH-113210 | 2015-03-02 | Well operation causing pollution and contamination |
For data sources see[9]