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34-127-26430

Well Details

Well ID: 34-127-26430
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Country: United States
State: Ohio
County: Perry
Municipality: Pike Township
Operator Name: SCHMELZER PLUGGING LLC
Well Pad ID:
Farm/Lease Name: KUNKLER HAROLD
License Status: Final Restoration
License Date: 2013-05-02
Spud Date: 1984-09-04
Spud Drilling Contractor: BILL FINCK DRLG
Final Drill Date: 1984-10-29
Well Total Depth: 3346.00 ft
Configuration: Vertical
Latitude: 39.660000
Longitude: -82.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-09-04 Issued Date 9/4/84 Expired Date 3/3/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03346 Proposed Drill Depth 03346
Original Spud 1984-09-04 FDT/GRAY
Completed 1984-10-29 FDT/GRAY
Reached Total Depth 1984-10-29 FDT/GRAY
CO 1984-11-20 837 METZGERS BOB GeoDate 9/4/84
Completion Report Received 1984-11-29 FDT/GRAY
Change of Owner 2013-04-17 Operator changed from 837, METZGERS BOB to 8565, SCHMELZER PLUGGING LLC
APP 2013-05-02 Proposed Formations:CLINTON, Issued Date:5/2/2013, Expired Date:5/2/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2013-08-07 FDT/GRAY
Construction Permit Expires 2015-05-02 FDT/GRAY
Record Last Modified 2017-02-15 FDT/GRAY

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3300 3328 0
3300 3328 0
3300 3328 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 86000 Gal 20000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 METZGERS BOB 0.00 0.00 0
2010 METZGERS BOB 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 METZGERS BOB Brine 0 0
2010 METZGERS BOB Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1051216680 2013-8-27 0:00: PB No Violations 1.00
-1405248683 2013-7-31 0:00: PB No Violations 7.50
-1769790463 2013-8-12 0:00: PB No Violations 1.00
-1915223195 2013-11-4 0:00: PB No Violations 1.00
-702390515 2013-12-30 0:00 FR No Violations 1.00
0000PL6714 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0223858441 2013-08-07 Plug / Plug Back No Violations I stopped by this well to see if clay had settled. It went down 30ft. Chris Schmelzer was on location topping hole back off while I was there.
0230141764 2013-09-10 Plug / Plug Back No Violations The dirt still needs to be put back and the production tank needs to be removed. Final restoration could not be completed. I talked with Chris to let him know.
0322048437 2013-08-06 Plug / Plug Back No Violations The plug has settled 40 ft. Mark Hines topped the well back off to the surface with the clay and is going to check it the next day.
0702390515 2013-12-30 Final Restoration No Violations The final restoration meets 1509.072.
0979948209 2013-08-02 Plug / Plug Back No Violations Mark Hines rig crew is on location today. They ran the 7 seat down to 1169ft. Then they washed clay in the well up to the bottom of the 8. They got set up to pull on the 8 and began trying to work it free.
1051216680 2013-08-27 Plug / Plug Back No Violations The clay has stopped settling. It can be cut off and reclaimed. Dump truck still on location along with a water tank. The pit has already been filled in.
1376058628 2013-08-05 Plug / Plug Back No Violations Mark Hines rig crew is on location. They pulled out 410ft of 8 out of the hole. Filled the hole the rest of the way with plugging clay. They are going to leave the well open until I give them the ok to close it in. We will check it and make sure it does not settle.
1381488783 2013-10-09 Plug / Plug Back No Violations I went to do the final restoration on this well. The 1-00 barrel tank is still on site and the well has not been covered with dirt. I talked with Chris and he told me he had no excuse for not having it finished. He would get on it right away.
1405248683 2013-07-31 Plug / Plug Back No Violations The rig crew worked on ripping the 4.5. They ended up getting it ripped at 2740ft. They had to pull 200ft to get the pipe to free up. The pipe was hung in the hole. The rig crew then washed in another 500ft of clay. They pulled the 4.5 out after that.
1644459663 2013-07-29 Plug / Plug Back No Violations MH Oilfield Service moved in on the well to plug it. They pulled out rods and tubing then washed in bottom plug. They used plugging clay for the job. A 500ft plug was set.
1769790463 2013-08-12 Plug / Plug Back No Violations The clay has settled down to 15ft. It is solid at that point. Chris Schmelzer will top the well off again.
1915223195 2013-11-04 Plug / Plug Back No Violations I stopped by this location to see if the well had been covered yet. The well has been covered but they have not put down the seed and mulch yet. The 100 barrel tank has been moved to the end of the location and is ready to be loaded.
2064550666 2013-11-19 Plug / Plug Back No Violations The tank is still on location. I was unable to do the FR. I will contact Chris to let him know this.
223858441 2013-8-7 0:00:0 PB No Violations 1.00
230141764 2013-9-10 0:00: PB No Violations 1.00
322048437 2013-8-6 0:00:0 PB No Violations 1.50
979948209 2013-8-2 0:00:0 PB No Violations 5.50
PL6714 PL No Violations

For data sources see[9]

References