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34-127-23804

Well Details

Well ID: 34-127-23804
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Country: United States
State: Ohio
County: Perry
Municipality: Pike Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: FRIEL TJ
License Status: Producing
License Date: 1976-07-12
Spud Date: 1976-07-10
Spud Drilling Contractor:
Final Drill Date: 1976-08-13
Well Total Depth: 3277.00 ft
Configuration: Vertical
Latitude: 39.650000
Longitude: -82.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-07-10
CO 1976-07-12 631 BT ENERGY CORP GeoDate 7/12/76
Completed 1976-08-13
Reached Total Depth 1976-08-13
Change of Owner 2007-10-12 Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO
Record Last Modified 2019-06-04

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 105000 Gal 20000 R.P./ A.F.

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BT ENERGY CORP 2058.00 564.00 365
1985 BT ENERGY CORP 1624.00 390.00 365
1986 BT ENERGY CORP 1788.00 390.00 365
1987 BT ENERGY CORP 1291.00 204.00 365
1988 BT ENERGY CORP 933.00 249.00 365
1990 BT ENERGY CORP 671.00 94.00 365
1991 BT ENERGY CORP 935.00 120.00 365
1993 BT ENERGY CORP 1064.00 106.00 365
1994 BT ENERGY CORP 839.00 0.00 360
1995 BT ENERGY CORP 439.00 68.00 365
1996 BT ENERGY CORP 448.00 46.00 322
1997 BT ENERGY CORP 207.00 0.00 322
1998 STONEBRIDGE OPERATING CO LLC 36.00 0.00 77
2000 STONEBRIDGE OPERATING CO LLC 1149.00 80.00 366
2001 STONEBRIDGE OPERATING CO LLC 439.00 0.00 365
2002 BT ENERGY CORP 22.00 0.00 7
2003 BT ENERGY CORP 122.00 18.00 266
2004 BT ENERGY CORP 174.00 24.00 215
2005 BT ENERGY CORP 53.00 0.00 215
2006 BT ENERGY CORP 64.00 0.00 120
2007 STONEBRIDGE OPERATING CO LLC 17.00 0.00 210
2008 STONEBRIDGE OPERATING CO LLC 0.00 0.00 154
2009 STONEBRIDGE OPERATING CO LLC 33.00 0.00 7
2010 STONEBRIDGE OPERATING CO LLC 49.00 0.00 70
2011 STONEBRIDGE OPERATING CO LLC 111.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 136.00 0.00 308
2013 STONEBRIDGE OPERATING CO LLC 229.00 10.00 224
2014 STONEBRIDGE OPERATING CO LLC 76.00 0.00 217
2015 STONEBRIDGE OPERATING CO LLC 46.00 0.00 210
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 14
2017 STONEBRIDGE OPERATING CO LLC 317.00 0.00 35
2018 STONEBRIDGE OPERATING CO LLC 27.00 0.00 154

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BT ENERGY CORP Brine 0 365
1985 BT ENERGY CORP Brine 315 365
1986 BT ENERGY CORP Brine 275 365
1987 BT ENERGY CORP Brine 0 365
1988 BT ENERGY CORP Brine 0 365
1990 BT ENERGY CORP Brine 70 365
1991 BT ENERGY CORP Brine 135 365
1993 BT ENERGY CORP Brine 175 365
1994 BT ENERGY CORP Brine 0 360
1995 BT ENERGY CORP Brine 127 365
1996 BT ENERGY CORP Brine 0 322
1997 BT ENERGY CORP Brine 0 322
1998 STONEBRIDGE OPERATING CO LLC Brine 0 77
2000 STONEBRIDGE OPERATING CO LLC Brine 23 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 365
2002 BT ENERGY CORP Brine 0 7
2003 BT ENERGY CORP Brine 49 266
2004 BT ENERGY CORP Brine 6 215
2005 BT ENERGY CORP Brine 6 215
2006 BT ENERGY CORP Brine 0 120
2007 STONEBRIDGE OPERATING CO LLC Brine 0 210
2008 STONEBRIDGE OPERATING CO LLC Brine 0 154
2009 STONEBRIDGE OPERATING CO LLC Brine 0 7
2010 STONEBRIDGE OPERATING CO LLC Brine 0 70
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 308
2013 STONEBRIDGE OPERATING CO LLC Brine 0 224
2014 STONEBRIDGE OPERATING CO LLC Brine 0 217
2015 STONEBRIDGE OPERATING CO LLC Brine 0 210
2016 STONEBRIDGE OPERATING CO LLC Brine 0 14
2017 STONEBRIDGE OPERATING CO LLC Brine 0 35
2018 STONEBRIDGE OPERATING CO LLC Brine 0 154

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1311745484 2013-6-3 0:00:0 PW No Violations 1.00
1111799385 2008-07-28 Annular Disposal No Violations No violations.
1311745484 2013-06-03 Production Wells Violations Noted I had a phone call from the land owner on this well. He told me that Stonebridge had a rig on location and tore up his driveway and plugged up the culverts on his right away. The water from the rain is coming right down his drive now and washing away his stone. He is also worried about a tree that fell on the electric line that goes to the well. He is worried for safety issues. He has tried to contact Stonebridge for 2 months but they will not return his call. I contacted Keith from Stonebridge and he is going to have someone get a hold of Mr. Waller and contact me.
1787687053 2013-10-09 Production Wells No Violations The location is now in compliance. The culvert has been fixed and the electric line has been restrung.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1311745484 US-OH-108832 2014-04-23 General Safety

For data sources see[8]

References