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34-127-22283

Well Details

Well ID: 34-127-22283
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Country: United States
State: Ohio
County: Perry
Municipality: Hopewell Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: SHELLY FRANK V
License Status: Producing
License Date: 1963-06-21
Spud Date: 1963-06-20
Spud Drilling Contractor:
Final Drill Date: 1963-07-17
Well Total Depth: 2735.00 ft
Configuration: Vertical
Latitude: 39.880000
Longitude: -82.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 79 OXFORD OIL CO
Oil and Gas 1802-01-01
Original Spud 1963-06-20
Completed 1963-07-17
Reached Total Depth 1963-07-17
Change of Owner 2014-02-06 Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC
Change of Owner 2016-08-02 Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2016-08-04

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 820 Bbl 12000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OXFORD OIL 0.00 305.00 0
1985 OXFORD OIL 0.00 289.00 365
1986 OXFORD OIL 0.00 230.00 365
1987 OXFORD OIL 0.00 290.00 365
1988 OXFORD OIL 0.00 225.00 365
1989 OXFORD OIL 0.00 137.00 365
1990 OXFORD OIL 0.00 235.00 365
1991 OXFORD OIL 0.00 147.00 365
1992 OXFORD OIL 0.00 244.00 365
1993 OXFORD OIL 0.00 159.00 365
1994 OXFORD OIL 0.00 204.00 365
1995 OXFORD OIL 0.00 146.00 365
1996 OXFORD OIL 0.00 232.00 366
1997 OXFORD OIL 0.00 231.00 365
1998 OXFORD OIL 0.00 148.00 365
1999 OXFORD OIL 0.00 224.00 365
2000 OXFORD OIL 0.00 229.00 0
2001 OXFORD OIL 0.00 152.00 365
2002 OXFORD OIL 0.00 153.00 365
2003 OXFORD OIL 0.00 192.00 365
2004 OXFORD OIL 0.00 176.00 365
2005 OXFORD OIL 0.00 129.00 365
2006 OXFORD OIL 0.00 225.00 365
2007 OXFORD OIL 0.00 143.00 365
2008 OXFORD OIL 0.00 140.00 0
2009 OXFORD OIL 0.00 156.00 0
2010 OXFORD OIL 0.00 159.00 365
2011 OXFORD OIL 0.00 150.00 0
2012 OXFORD OIL 0.00 155.00 0
2013 ECLIPSE RESOURCES-OHIO LLC 0.00 159.00 365
2014 ECLIPSE RESOURCES-OHIO LLC 0.00 223.00 365
2015 ECLIPSE RESOURCES-OHIO LLC 0.00 154.00 365
2016 M & R INVESTMENTS OHIO LLC 0.00 100.00 365
2017 M & R INVESTMENTS OHIO LLC 0.00 230.00 365
2018 M & R INVESTMENTS OHIO LLC 0.00 157.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OXFORD OIL Brine 0 0
1985 OXFORD OIL Brine 30 365
1986 OXFORD OIL Brine 25 365
1987 OXFORD OIL Brine 20 365
1988 OXFORD OIL Brine 100 365
1989 OXFORD OIL Brine 40 365
1990 OXFORD OIL Brine 35 365
1991 OXFORD OIL Brine 40 365
1992 OXFORD OIL Brine 30 365
1993 OXFORD OIL Brine 20 365
1994 OXFORD OIL Brine 40 365
1995 OXFORD OIL Brine 30 365
1996 OXFORD OIL Brine 30 366
1997 OXFORD OIL Brine 30 365
1998 OXFORD OIL Brine 70 365
1999 OXFORD OIL Brine 51 365
2000 OXFORD OIL Brine 36
2001 OXFORD OIL Brine 28 365
2002 OXFORD OIL Brine 34 365
2003 OXFORD OIL Brine 28 365
2004 OXFORD OIL Brine 24 365
2005 OXFORD OIL Brine 26 365
2006 OXFORD OIL Brine 47 365
2007 OXFORD OIL Brine 10 365
2008 OXFORD OIL Brine 16
2009 OXFORD OIL Brine 15
2010 OXFORD OIL Brine 36 365
2011 OXFORD OIL Brine 27
2012 OXFORD OIL Brine 20
2013 ECLIPSE RESOURCES-OHIO LLC Brine 25 365
2014 ECLIPSE RESOURCES-OHIO LLC Brine 25 365
2015 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2016 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2017 M & R INVESTMENTS OHIO LLC Brine 30 365
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1283373749 2007-2-21 0:00: PW No Violations
-1570471757 2017-7-17 0:00: PW No Violations 3.00
-1755116777 2017-8-18 0:00: PW No Violations
-248084712 2017-7-17 0:00: PW No Violations 1.00
-469598085 2008-11-19 0:00 PW No Violations
-807849128 2020-7-14 0:00: PW No Violations 0.50
-8475176 2013-8-7 0:00:0 PW No Violations 1.00
0008475176 2013-08-07 Production Wells No Violations This well is capable of production. It has a pumping unit on it with rods and 2 tubing. The identification for the well is on the tank. The valve coming off the well to the production tank is open. No violations at this time.
0095448660 2017-08-07 Production Wells No Violations I returned to this well today to do a follow-up inspection on it. While I was on location today Rusty and Kevin from M&R Investments were on site working on building the fence around the tank pad. The production tank has been reset, the dike has been rebuilt and they are working on finishing the rest. I will stop back in a couple of days to see if everything is finished.
0248084712 2017-07-17 Production Wells No Violations I returned to this well today to do a follow-up inspection on it. The company has put down an absorbent material to soak up any oil inside the contained area. They will continue to clean up and remove any contamination until it is clean.
0309632011 2015-04-02 Production Wells No Violations Inspection on 4/2/2015 the well and tank were identified properly. Well is capable of producing. Tank battery consisted of two 100 barrel tanks with knockout. Upon inspection of the well there was found to be a small leak with escaping gas around the 4 1/2 well head.. A call was placed to Mike Hartshorn to have Jerry Love the pumper correct the situation.
0340457603 2018-12-19 Production Wells No Violations I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time.
0469598085 2008-11-19 Production Wells No Violations No violations.
0484732709 2017-07-20 Production Wells No Violations I returned back to this location today to check on the clean-up around the tank pad. It looks like the company has been back here and put down more absorbent on the contaminated areas. I tried to contact Jody Jasper from M&R Investments during the time of my inspection to see when they would be setting the production tank back up but I did not reach him. His phone did not go to voicemail so I will try to call him again later in the day. Jody Jasper returned my phone call while I was still on location. He stated at this time he is trying to reach the township and has left them a message to see if they could relocate the production tank on there property so it does not flood again. He stated that they have not got back with him yet so he would try again and let me know what they said.
0628991585 2016-06-30 Production Wells No Violations I was on location today to do a field inspection on this well. The well appears to be capable of production. It has a pumping unit on it with rods and 2 tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time.
1062453921 2018-01-22 Production Wells No Violations I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. It has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the wellhead to the tank pad. The identification is located on the production tank. There are no violations at this time.
1250281015 2018-09-07 Production Wells No Violations I stopped by this well to check on the production tank. We are suppose to get a bunch of rain over the next couple of days so I contacted Matt the supervisor for M&R Investments to see if he can find out how much fluid is in the tank and make sure it is secured so it does not float away again from the heavy rain. He is currently working on it now.
1283373749 2007-02-21 Production Wells No Violations No violations.
1500315053 2017-07-13 Production Wells Violations Noted This inspection was conducted as a status check. I received a phone call regarding a 100 barrel tank flipping on its side due to a flood where high water reached the tank battery. I arrived to the location at 7:30 PM and was accompanied by Southwest Region Supervisor Dan Goins. Ohio EPA OSC Trevor Irwin was on location during inspection. The inspection revealed that water depth at the tank battery location was approximately 6 feet and was responsible for floating the tank and tipping it on its side. The tank stayed within the dike area. Oil was observed on top of the water. A Diversified Resources vac truck arrived at approximately 8:30 PM to cacuum up oil from around the tank. The company was advised to clean up contamination. This was regarded as a verbal compliance notice.
1500551734 2017-07-20 Production Wells No Violations This inspection was conducted as a compliance notice follow-up. No personnel were present during inspection. The oil contamination has been cleaned up. The company has indicated that they are planning on setting the tank battery on higher ground. Time of inspection: 7:55 AM. Weather: 70*F, Partly cloudy
1559775174 2019-05-30 Production Wells No Violations I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The valves are open from the well to the tank pad. The identification is located on the production tank. There are no violations at this time.
1570471757 2017-07-17 Production Wells No Violations I was on location today to check on the clean-up of this location. All the rain we got caused a 100 barrel production tank to lift up and break off from the water knockout. This caused some contamination around the tank pad. The company responded fast and got the production tank emptied and pulled up out of the flooded area. After discussing it with Jody Jasper from M&R Investments and Aaron Wolfe from the EPA they believe they lost less then 20 gallons from what they had in the production tank and what they recovered. The company stated that they had around 2 feet in the tank and they recovered right at 2 feet. The company is working on setting the production tank in a different spot so this does not happen again.
1755116777 2017-08-18 Production Wells No Violations I returned to this well today to check the status of the clean-up. At this point the well is no longer in violation. All of the contamination has been removed, the production tank has been reset, the contamination dike has been rebuilt and a new fence has been put around the production tank. There are no violations at this time.
1850869098 2017-07-14 Production Wells No Violations This inspection was conducted as a follow-up. Inspector Justin Smith was on location when I arrived. Ohio EPA OSC Aaron Wolfe was on location during inspection as well as Perry County Wildlife Officer Eric Lane. Cleanup was in progress during the inspection. The water had receded approximately 8 feet since the previous night. The 100 barrel tank was pulled up onto higher ground. Photos were taken of the cleanup. Time of inspection: 8:40 AM.
309632011 2015-4-2 0:00:0 PW No Violations 1.00
340457603 2018-12-19 0:00 PW No Violations 0.50
484732709 2017-7-20 0:00: PW No Violations 1.00
628991585 2016-6-30 0:00: PW No Violations 1.00
95448660 2017-8-7 0:00:0 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1500315053 US-OH-114113 2017-12-27 9-1-07 Well operation causing pollution and contamination

For data sources see[8]

References