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34-121-62909

Well Details

Well ID: 34-121-62909
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Country: United States
State: Ohio
County: Noble
Municipality: Marion Township
Operator Name: GEORGETOWN OIL CO
Well Pad ID:
Farm/Lease Name: GROVES J F
License Status: Final Restoration
License Date: 2004-09-14
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 1752.00 ft
Configuration: Vertical
Latitude: 39.830000
Longitude: -81.380000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2004-09-14 Proposed Formations:BEREA, Issued Date:9/14/2004, Expired Date:9/14/2005 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2004-10-12
Construction Permit Expires 2005-09-14
Record Last Modified 2017-02-15

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 COLUMBIA GAS TRANSMISSION LLC 1161.00 0.00 365
1992 CHESAPEAKE APPALACHIA LLC 863.00 0.00 365
1994 CHESAPEAKE APPALACHIA LLC 0.00 0.00 0
1995 CHESAPEAKE APPALACHIA LLC 0.00 0.00 0
1996 CHESAPEAKE APPALACHIA LLC 0.00 0.00 0
1997 CHESAPEAKE APPALACHIA LLC 0.00 0.00 0
1998 CHESAPEAKE APPALACHIA LLC 0.00 0.00 0
1999 GEORGETOWN OIL 1090.00 0.00 365
2000 GEORGETOWN OIL 120.00 0.00 150

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 COLUMBIA GAS TRANSMISSION LLC Brine 0 365
1992 CHESAPEAKE APPALACHIA LLC Brine 0 365
1994 CHESAPEAKE APPALACHIA LLC Brine 0 0
1995 CHESAPEAKE APPALACHIA LLC Brine 0 0
1996 CHESAPEAKE APPALACHIA LLC Brine 0 0
1997 CHESAPEAKE APPALACHIA LLC Brine 0 0
1998 CHESAPEAKE APPALACHIA LLC Brine 0 0
1999 GEORGETOWN OIL Brine 0 365
2000 GEORGETOWN OIL Brine 0 150

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1750665066 2004-9-29 0:00: PB No Violations
1097357677 2004-10-04 Plug / Plug Back No Violations On site to witness cleaning out of well bore in attempt to plug well.
1097489878 2004-10-07 Plug / Plug Back No Violations On site to witness operator attempting to free up 1 tubing in efforts to plug said well,Timco wireline services located Packer @1660 set inside of 2 tubing,operator instructed Mr. Brown to perf 1 at 1600 in attempts to free up tubing (failed)then Earl Barnes instructed rig operator to pull on 1 and it parted attempts were made to get back on 1 with no avail, decision was made to run 5 casing down hole to where 2 is parted and reattempt to get back on 1 to set bottom hole plug
1750000857 2005-01-19 Final Restoration No Violations Restoration work at site satisfactory,,well was plugged by Davis Well Service 10-12-04.
1750665066 2004-09-29 Plug / Plug Back No Violations On site to witness attempts being made to clean out tubing so operator can plug well.

Earl Barnes is acting agent for Georgetown Oil,Davis Well Service is the contractor.

For data sources see[7]

References