X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-121-24105

Well Details

Well ID: 34-121-24105
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Center Township
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name: SCHNEEBERGER UNIT
License Status: Final Restoration
License Date: 2004-10-20
Spud Date: 2004-10-25
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 2004-11-12
Well Total Depth: 9030.00 ft
Configuration: Vertical
Latitude: 39.790000
Longitude: -81.470000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2004-10-20 Proposed Formations:ROSE RUN, Issued Date:10/20/2004, Expired Date:10/20/2005 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 2004-10-25 RBDMS Rec
Completed 2004-11-12 RBDMS Rec
Reached Total Depth 2004-11-12 RBDMS Rec
Plugged/Abandoned 2004-11-14 RBDMS Rec
Completion Report Received 2005-01-03 RBDMS Rec
Construction Permit Expires 2005-10-20 RBDMS Rec
Record Last Modified 2013-03-14 RBDMS Rec

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2004 ARTEX OIL COMPANY 0.00 0.00 365
2005 ARTEX OIL COMPANY 0.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2004 ARTEX OIL COMPANY Brine 3993 365
2005 ARTEX OIL COMPANY Brine 3486 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1566920732 2004-11-8 0:00: DD No Violations
1099144801 2004-10-26 Drill / Deepen / Reopen No Violations On site to check on drilling rig moving in,rig crew was receiving surface pipe,awaiting air package to enable crew to get started drilling operation.

Received 1639 of 8.625 casing-23#

1099219064 2004-10-28 Drill / Deepen / Reopen No Violations On site to witness testing of BOP system,tested Blind rams@950psi for 15 min test passed,tested pipe rams @900psi for 15min test passed,and tested annular system for an additional 15 min @975psi and it also passed with no decline in pressure.
1099923768 2004-11-08 Drill / Deepen / Reopen No Violations Stopped by drilling rig for update they were 7334 fishing drill string uot of hole pipe parted 1525+- down hole operator trying to get back on string with overshot.
1133645709 2005-12-02 Final Restoration No Violations Well site has been restored restoration work at site satisfactory.
1566920732 2004-11-08 Drill / Deepen / Reopen No Violations Stopped by drilling operation to check on rig they were twisted off at 7334 they were attempting too hook back onto drill string with overshot&grapple three attempts were made before making hookup with drillstring operator removed drillstring from wellbore and changed out faulty pipe and drill bit before resuming drilling operation.

For data sources see[7]

References