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Well ID: 34-121-23904 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Brookfield Township | |
Operator Name: ATLAS NOBLE LLC | |
Well Pad ID: | |
Farm/Lease Name: OHIO POWER | |
License Status: Final Restoration | |
License Date: 2013-02-06 | |
Spud Date: 1996-10-30 | |
Spud Drilling Contractor: MATTMARK DRILLING | |
Final Drill Date: 1996-11-21 | |
Well Total Depth: 5360.00 ft | |
Configuration: Vertical | |
Latitude: 39.780000 | |
Longitude: -81.670000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1996-08-06 | 3071 KINGSTON OIL CORP GeoDate 8/6/96 |
Oil and Gas | 1996-08-06 | Issued Date 8/6/96 Expired Date 8/6/97 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05360 Proposed Drill Depth 05360 |
Original Spud | 1996-10-31 | |
Completed | 1996-11-21 | |
Reached Total Depth | 1996-11-21 | |
Completion Report Received | 1996-12-16 | |
Change of Owner | 2001-01-12 | Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC |
Change of Owner | 2004-03-23 | Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC |
APP | 2013-02-06 | Proposed Formations:CLINTON, Issued Date:2/6/2013, Expired Date:2/6/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-12-29 | |
Construction Permit Expires | 2015-02-06 | |
Record Last Modified | 2015-08-11 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5015 | 5126 | 0 |
5015 | 5126 | 0 | |
2006-09-11 | 5053 | 5124 | 35 |
5030 | 5035 | 5 | |
5015 | 5126 | 0 | |
2006-09-11 | 5171 | 5177 | 6 |
2006-09-11 | 5030 | 5035 | 5 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 400 Gal | 0 | FRAC W/2700 BW & 400 SX SAND | ||
H2O | 0 | 2700 Bbl | 40000 | TREAT 44 BPM, SHUT IN PRESS 400 PSI. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | KINGSTON OIL CORP | 12004.00 | 67.00 | 350 |
1998 | KINGSTON OIL CORP | 5476.00 | 0.00 | 350 |
1999 | KINGSTON OIL CORP | 7464.00 | 0.00 | 0 |
2000 | KINGSTON OIL CORP | 5960.00 | 0.00 | 0 |
2001 | CHEVRON APPALACHIA LLC | 4135.00 | 110.00 | 365 |
2002 | CHEVRON APPALACHIA LLC | 4666.00 | 0.00 | 365 |
2003 | ATLAS NOBLE LLC | 5418.00 | 65.00 | 365 |
2004 | ATLAS NOBLE LLC | 4421.00 | 31.00 | 365 |
2005 | ATLAS NOBLE LLC | 3558.00 | 0.00 | 365 |
2006 | ATLAS NOBLE LLC | 2958.00 | 0.00 | 365 |
2007 | ATLAS NOBLE LLC | 2656.00 | 17.00 | 365 |
2008 | ATLAS NOBLE LLC | 2143.00 | 0.00 | 366 |
2009 | ATLAS NOBLE LLC | 896.00 | 0.00 | 365 |
2010 | ATLAS NOBLE LLC | 39.00 | 0.00 | 365 |
2011 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2012 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2013 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2014 | ATLAS NOBLE LLC | 0.00 | 0.00 | 182 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | KINGSTON OIL CORP | Brine | 340 | 350 |
1998 | KINGSTON OIL CORP | Brine | 1041 | 350 |
1999 | KINGSTON OIL CORP | Brine | 510 | |
2000 | KINGSTON OIL CORP | Brine | 351 | |
2001 | CHEVRON APPALACHIA LLC | Brine | 25 | 365 |
2002 | CHEVRON APPALACHIA LLC | Brine | 602 | 365 |
2003 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2004 | ATLAS NOBLE LLC | Brine | 80 | 365 |
2005 | ATLAS NOBLE LLC | Brine | 52 | 365 |
2006 | ATLAS NOBLE LLC | Brine | 39 | 365 |
2007 | ATLAS NOBLE LLC | Brine | 28 | 365 |
2008 | ATLAS NOBLE LLC | Brine | 29 | 366 |
2009 | ATLAS NOBLE LLC | Brine | 28 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2011 | ATLAS NOBLE LLC | Brine | 0 | |
2012 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2013 | ATLAS NOBLE LLC | Brine | 23 | 0 |
2014 | ATLAS NOBLE LLC | Brine | 5 | 182 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1791618898 | 2015-6-2 0:00:0 | FR | No Violations | |
-1890588134 | 2014-7-3 0:00:0 | AM | No Violations | |
-232406927 | 2015-6-30 0:00: | FR | No Violations | 1.00 |
-747975322 | 2015-8-3 0:00:0 | FR | No Violations | 1.50 |
-891300297 | 2014-1-13 0:00: | AM | No Violations | 0.30 |
-913289203 | 2014-12-29 0:00 | PB | No Violations | 5.00 |
0232406927 | 2015-06-30 | Final Restoration | No Violations | My inspection today finds the well site has been graded, but lacks vegetation. Further work is needed to comply with 1509.072(B). |
0338539749 | 2014-12-23 | Plug / Plug Back | No Violations | My inspection today finds Appalachian Well Surveys perforated the 4.5 casing at 3810 with ten shots. The service rig ran tubing to the top of the Clinton plug and set an additional 30 sack plug to ensure isolation. The rig crew then pulled the tubing up to 3810 and a 58 sack class A plug was placed. |
0643010160 | 2014-10-15 | Production Wells | No Violations | My inspection today finds the well is shut in and has been disconnected from any pipeline. The pumping unit has been removed. A 210 barrel tank is still located in a dike; however, the 100 barrel tank and the production unit has been removed. |
0747975322 | 2015-08-03 | Final Restoration | No Violations | My inspection today finds the well site meets the final restoration requirements of 1509.072(B). |
0891300297 | 2014-01-13 | Administrative Inspection | No Violations | Mark Warehime returned my call at 2:14pm we discussed the outstanding compliance notice on this well. He will review the notice with his supervisors again. I reminded him of the H2S condition of the well. |
0913289203 | 2014-12-29 | Plug / Plug Back | No Violations | I am onsite to witness the well plugging operations. A 200 58 sack class A plug was circulated into place over the Berea from 1682 to 1482. The service rig then pulled the casing up to the base of the surface casing and placed a 60 sack class A plug from 1321 to 1121. A 62 sack class A plug was placed at surface. The company was instructed to reclaim the site in accordance with 1509:072(B). The previous violation has been resolved. |
1265171514 | 2003-05-19 | Salt Water Injection Well | No Violations | well in production,no violations noted on the day of my inspection. |
1331516308 | 2014-03-27 | Administrative Inspection | No Violations | At 1:38 pm Mark Warehime called to inform me that the company has approved the plugging of the well, though an exact date has not been set. |
1355324752 | 2012-12-12 | Production Wells | Violations Noted | My inspection today finds that upon entering the lease road there is a DANGER HYDROGEN SULFIDE sign. The well has not reported any production since 2008. The well is equipped with 4.5 casing, 2.375, tubing, rods, and a pump jack. All valves are shut. The tank battery consists of one 210 bbl tank, a 100 bbl tank, and a production unit. THE WELL SHALL BE PLUGGED DUE TO H2S CONDITIONS. FILE PRODUCTION STATEMENTS FROM 2009 TO CURRENT. FAILURE TO COMPLY MAY RESULT IN FORFIETURE OF BOND. |
1381856072 | 2013-10-11 | Production Wells | No Violations | The status of the well has not changed. The well is still shut in. A danger hydrogen sulfide sign is posted at the tank battery. |
1620344509 | 2015-10-27 | Final Restoration | No Violations | The well site is fully vegetated and all equipment has been removed. |
1791618898 | 2015-06-02 | Final Restoration | No Violations | My inspection today finds the well head has been cut off and the pit closed; however, the site has not been seeded and the road has not been graded. |
1890588134 | 2014-07-03 | Administrative Inspection | No Violations | I called and spoke to Mark Warehime Field Supervisor for Atlas Noble LLC at 7:22 AM. Mr. Warehime said that Nicks Plugging will be bringing a rig to begin plugging operations within the next few of weeks. |
1905318644 | 2014-12-19 | Plug / Plug Back | No Violations | Nicks Well Plugging used their pump truck to kill the gas flow from the well due to H2S. Specialized Safety Services is onsite to provide monitoring of H2S. A class A 30 sack bottom plug was placed through 2.375 tubing at 5177. The service rig then pulled out all of the tubing. |
338539749 | 2014-12-23 0:00 | PB | No Violations | 9.00 |
643010160 | 2014-10-15 0:00 | PW | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1355324752 | US-OH-110280 | 2015-01-14 | General Safety | |
1355324752 | US-OH-110281 | 2015-01-14 | Well shall be plugged | |
1355324752 | US-OH-110282 | 2015-01-14 | Statement of annual production not filed |
For data sources see[9]