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34-121-23193

Well Details

Well ID: 34-121-23193
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Country: United States
State: Ohio
County: Noble
Municipality: Jackson Township
Operator Name: GENESIS RESOURCES LLC
Well Pad ID:
Farm/Lease Name: MARIETTA COAL
License Status: Producing
License Date: 1984-05-31
Spud Date: 1984-06-09
Spud Drilling Contractor: J & B DRILLING
Final Drill Date: 1984-06-17
Well Total Depth: 6217.00 ft
Configuration: Vertical
Latitude: 39.600000
Longitude: -81.500000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-05-31 6 BENATTY CORP GeoDate 5/31/84
Oil and Gas 1984-05-31 Issued Date 5/31/84 Expired Date 11/27/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06217 Proposed Drill Depth 06217
Original Spud 1984-06-09
Completed 1984-06-17
Reached Total Depth 1984-06-17
Completion Report Received 1984-07-24
Construction Permit Expires 1984-11-27
CO 1995-01-20 182 BELDEN & BLAKE CO GeoDate 5/31/84
Change of Owner 2003-05-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 5352, ARTEX OIL COMPANY
Change of Owner 2003-05-07 Operator changed from 5352, ARTEX OIL COMPANY to 952, G-R CONTRACTING INC
Last Compliance Report 2014-04-15
Change of Owner 2019-01-22 Operator changed from 952, G-R CONTRACTING INC to 9086, GENESIS RESOURCES LLC
Record Last Modified 2019-01-22

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5924 6014 0
5924 6014 0
2006-09-11 5950 5958 2
5950 5958 2
5924 6014 0
2006-09-11 6062 6078 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 155 Mscf 0 CL.
N2 0 134 Mscf 0 MED.
H2O 0 36500 Gal 40000 FRAC: H2O,SAND,N2
H2O 0 45750 Gal 40000 CL.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BENATTY CORP 13576.00 0.00 0
1985 BENATTY CORP 34348.00 0.00 0
1986 BENATTY CORP 15431.00 0.00 365
1987 BENATTY CORP 11381.00 0.00 365
1988 BENATTY CORP 7915.00 0.00 365
1989 BENATTY CORP 6036.00 0.00 365
1990 BENATTY CORP 4841.00 0.00 365
1991 BENATTY CORP 3153.00 0.00 365
1992 BENATTY CORP 3482.00 0.00 365
1993 BENATTY CORP 3150.00 0.00 365
1994 BELDEN & BLAKE CORPORATION 782.00 0.00 366
1995 BELDEN & BLAKE CORPORATION 950.00 41.00 249
1996 BELDEN & BLAKE CORPORATION 184.00 0.00 141
1999 ARTEX OIL COMPANY 1880.00 0.00 0
2000 ARTEX OIL COMPANY 1632.00 0.00 365
2001 ARTEX OIL COMPANY 2191.00 0.00 365
2002 G-R CONTRACTING INC 0.00 0.00 365
2003 G-R CONTRACTING INC 0.00 0.00 365
2004 G-R CONTRACTING INC 249.00 0.00 365
2005 G-R CONTRACTING INC 0.00 0.00 365
2006 G-R CONTRACTING INC 0.00 0.00 365
2007 G-R CONTRACTING INC 0.00 0.00 365
2008 G-R CONTRACTING INC 0.00 0.00 365
2009 G-R CONTRACTING INC 42.00 0.00 365
2010 G-R CONTRACTING INC 0.00 0.00 365
2011 G-R CONTRACTING INC 0.00 0.00 365
2012 G-R CONTRACTING INC 0.00 0.00 366
2013 G-R CONTRACTING INC 0.00 0.00 365
2014 G-R CONTRACTING INC 0.00 0.00 365
2015 G-R CONTRACTING INC 0.00 0.00 365
2016 G-R CONTRACTING INC 0.00 0.00 365
2017 G-R CONTRACTING INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BENATTY CORP Brine 0 0
1985 BENATTY CORP Brine 420 0
1986 BENATTY CORP Brine 320 365
1987 BENATTY CORP Brine 325 365
1988 BENATTY CORP Brine 140 365
1989 BENATTY CORP Brine 101 365
1990 BENATTY CORP Brine 135 365
1991 BENATTY CORP Brine 100 365
1992 BENATTY CORP Brine 0 365
1993 BENATTY CORP Brine 60 365
1994 BELDEN & BLAKE CORPORATION Brine 0 366
1995 BELDEN & BLAKE CORPORATION Brine 0 249
1996 BELDEN & BLAKE CORPORATION Brine 0 141
1999 ARTEX OIL COMPANY Brine
2000 ARTEX OIL COMPANY Brine 0 365
2001 ARTEX OIL COMPANY Brine 0 365
2002 G-R CONTRACTING INC Brine 0 365
2003 G-R CONTRACTING INC Brine 0 365
2004 G-R CONTRACTING INC Brine 0 365
2005 G-R CONTRACTING INC Brine 0 365
2006 G-R CONTRACTING INC Brine 0 365
2007 G-R CONTRACTING INC Brine 0 365
2008 G-R CONTRACTING INC Brine 0 365
2009 G-R CONTRACTING INC Brine 0 365
2010 G-R CONTRACTING INC Brine 0 365
2011 G-R CONTRACTING INC Brine 0 365
2012 G-R CONTRACTING INC Brine 0 366
2013 G-R CONTRACTING INC Brine 0 365
2014 G-R CONTRACTING INC Brine 0 365
2015 G-R CONTRACTING INC Brine 0 365
2016 G-R CONTRACTING INC Brine 0 365
2017 G-R CONTRACTING INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2121904182 2014-3-27 0:00: PW No Violations 1.50
-81323815 2014-2-25 0:00: PW No Violations 4.50
0000PL7568 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0081323815 2014-02-25 Production Wells No Violations The company sent a dozer to repair the lease road. Once accessing the location we determined that the 4.5 casing has no pressure and the tubing has over 600 psi. The pressures indicate the tubing may be set on a packer. The 8.625 casing has over 150 psi and the gas has traces of H2S. I instructed the company representative to flare the gas off of the 8.625 casing and load the hole with fluid to stop the flow of gas.
0152812929 2008-09-02 Annular Disposal No Violations A.D.not hooked up well is shut in at present time, it is equipped with tubing&production casing&8 surface casing and 1-100 bbl tank in need of dike work preformed will call company and discuss future plans on placing well into production or file for plugging permit/
0169267478 2014-01-31 Annular Disposal No Violations The annular disposal is not in use. The well is equipped with 4.5 casing and 1.5 tubing. All the valves are shut. The well has a significant lean. It appears the casing has failed at the surface. There is a strong odor of sulfur at the well. I will return on Monday to test the area for H2S. The lease road is impassible.
0523912195 2014-02-06 Production Wells Violations Noted My inspection finds the well is equipped to be produced by a plunger lift system. All valves are shut in at the well. A test of the area around the 8.625 casing, with a Honeywell PhD6 gas meter, indicated that H2S gas was present in amounts of 80 ppm. I contacted Mr. Shulzberger with G-R Contracting and made him aware of the issue. Mr. Shulzberger was directed to immediately cordon off the area around the well and post signage notifying people of the danger. I also directed Mr. Shulzberger to submit a plan in writing that outlines the company plan to kill the well to prevent the flow of H2S. Additionally I asked for a plan to remedy the well long term with a specific time frame. IMMEDIATELY STOP THE FLOW OF H2S. IMMEDIATELY REPAIR THE CASING, CORRECT THE CONSTRUCTION INADEQUACIES, OR PLUG AND ABANDON THE WELL. SUBMIT, IN WRITING, A PLAN WITH TIME LINES TO ACHIEVE THESE REQUIREMENTS WITHIN 72 HOURS.
0942950055 2014-02-05 Administrative Inspection No Violations I called Jordan with G-R Contracting at 1:06 pm. I spoke to him about the condition of the well. He stated that a truck had struck the well sometime ago and caused the well to lean. I informed him that I detected a strong odor, that may be H2S, on my 1/31/14 inspection and that I would return to test the well as soon as the weather permitted. I also told him that if the well was leaking H2S the company would be required to take immediate action.
1224540657 2008-10-20 Annular Disposal No Violations Upon inspecting site again found well is still shut in contacted owner and he stated they would apply for plugging permit over the winter months and plug said well in the spring of 09.
1393017683 2014-02-21 Administrative Inspection No Violations I called Jordan Jones of G-R Contracting at 11:15 am. I asked him when he was going to move a dozer and water truck to the site to kill the flow of sour gas. He stated that the county roads were too soft and he did not want to tear them up with the heavy trucks. I agreed to allow them to wait until next Tuesday for the road conditions to improve.
152812929 2008-9-2 0:00:0 AD No Violations
1586784220 2020-4-2 0:00:0 TD No Violations 0.10
1638373737 2020-4-6 0:00:0 AM No Violations 0.30
169267478 2014-1-31 0:00: AD No Violations 1.00
2121904182 2014-03-27 Production Wells No Violations My inspection finds the well has been returned to production. The previous violations have been corrected. The flow of H2S has been stopped. The well is equipped with 1.5 tubing on a packer and is being produced through an intermittent timer. A meter is set on location and it has a current chart.
266917430 2020-4-22 0:00: PW No Violations 1.00
50833373 2020-4-2 0:00:0 PW No Violations 1.50
523912195 2014-2-6 0:00:0 PW No Violations
942950055 2014-2-5 0:00:0 AM No Violations 0.20
PL7568 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0523912195 US-OH-125726 2014-04-10 General Safety
0523912195 US-OH-125727 2014-04-10 Well shall be plugged

For data sources see[9]

References