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34-121-23136

Well Details

Well ID: 34-121-23136
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Country: United States
State: Ohio
County: Noble
Municipality: Jackson Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: ATHERTON CLARK
License Status: Final Restoration
License Date: 2014-03-14
Spud Date: 1984-05-29
Spud Drilling Contractor: MID ATLANTC DRLG
Final Drill Date: 1984-06-16
Well Total Depth: 6332.00 ft
Configuration: Vertical
Latitude: 39.600000
Longitude: -81.490000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-02-08 3443 MALVERN GROUP INC GeoDate 2/8/84
Oil and Gas 1984-02-08 Issued Date 2/8/84 Expired Date 8/6/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06332 Proposed Drill Depth 06332
Original Spud 1984-05-29
Completed 1984-06-16
Reached Total Depth 1984-06-16
Completion Report Received 1984-07-12
APP 1999-03-17 Proposed Formations:CLINTON, Issued Date:3/17/99, Expired Date:3/16/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2000-02-14 Operator changed from 3443, MALVERN GROUP INC to 6351, T & C OIL & GAS COMPANY
Change of Owner 2000-04-05 Operator changed from 6351, T & C OIL & GAS COMPANY to 6733, C & M GAS & OIL
Change of Owner 2001-04-18 Operator changed from 6733, C & M GAS & OIL to 4431, VALLEY ENTERPRISES
APP 2008-04-22 Proposed Formations:CLINTON, Issued Date:4/22/2008, Expired Date:4/22/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:HAD, Proposed Well Class:
Change of Owner 2008-10-21 Operator changed from 4431, VALLEY ENTERPRISES to 1634, NORTHWOOD ENERGY CORP
APP 2010-07-01 Proposed Formations:DEVONIAN SHALE THRU ORISKANY, Issued Date:7/1/2010, Expired Date:7/1/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:ENPW
APP 2014-03-14 Proposed Formations:ORISKANY, Issued Date:3/14/2014, Expired Date:3/13/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2014-05-05
Construction Permit Expires 2016-03-13
Record Last Modified 2017-10-13

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 0 0
0 0
2006-09-11 6081 6214 40
6081 6214 40
0 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 52750 Gal 50000 FRAC;H2O,SAND
H2O 0 36500 Gal 40000 MED.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DERBY OIL & GAS CORP 10522.00 0.00 0
1985 DERBY OIL & GAS CORP 16495.00 0.00 353
1986 DERBY OIL & GAS CORP 2141.00 0.00 357
1987 CHRISTA OIL CO 5854.00 0.00 361
1988 BAUGHMAN ELEANOR 2091.00 0.00 356
1989 BAUGHMAN ELEANOR 994.00 0.00 334
1990 MALVERN GROUP INC 2865.00 6.00 365
1991 MALVERN GROUP INC 2127.00 0.00 363
1992 MALVERN GROUP INC 2477.00 0.00 365
1993 MALVERN GROUP INC 2372.00 0.00 365
1994 MALVERN GROUP INC 2452.00 0.00 365
1995 MALVERN GROUP INC 2458.00 0.00 365
1996 MALVERN GROUP INC 2364.00 0.00 365
1997 MALVERN GROUP INC 2272.00 0.00 365
1998 MALVERN GROUP INC 1053.00 0.00 365
1999 MALVERN GROUP INC 120.00 0.00 60
2000 MALVERN GROUP INC 0.00 0.00 0
2001 VALLEY ENTERPRISES 0.00 0.00 0
2008 NORTHWOOD ENERGY CORP 0.00 0.00 0
2009 NORTHWOOD ENERGY CORP 0.00 0.00 0
2010 NORTHWOOD ENERGY CORP 0.00 0.00 0
2011 NORTHWOOD ENERGY CORP 121.00 0.00 0
2012 NORTHWOOD ENERGY CORP 0.00 0.00 0
2013 NORTHWOOD ENERGY CORP 0.00 59.00 365
2014 NORTHWOOD ENERGY CORP 0.00 91.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DERBY OIL & GAS CORP Brine 472 0
1985 DERBY OIL & GAS CORP Brine 450 353
1986 DERBY OIL & GAS CORP Brine 142 357
1987 CHRISTA OIL CO Brine 150 361
1988 BAUGHMAN ELEANOR Brine 142 356
1989 BAUGHMAN ELEANOR Brine 100 334
1990 MALVERN GROUP INC Brine 72 365
1991 MALVERN GROUP INC Brine 0 363
1992 MALVERN GROUP INC Brine 0 365
1993 MALVERN GROUP INC Brine 0 365
1994 MALVERN GROUP INC Brine 0 365
1995 MALVERN GROUP INC Brine 0 365
1996 MALVERN GROUP INC Brine 0 365
1997 MALVERN GROUP INC Brine 365
1998 MALVERN GROUP INC Brine 365
1999 MALVERN GROUP INC Brine 60
2000 MALVERN GROUP INC Brine 0
2001 VALLEY ENTERPRISES Brine 0 0
2008 NORTHWOOD ENERGY CORP Brine 0 0
2009 NORTHWOOD ENERGY CORP Brine 0 0
2010 NORTHWOOD ENERGY CORP Brine 0 0
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 75 0
2013 NORTHWOOD ENERGY CORP Brine 107 365
2014 NORTHWOOD ENERGY CORP Brine 340 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-126321449 2004-3-23 0:00: PW No Violations
0000PL7609 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0126321449 2004-03-23 Production Wells No Violations Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phots indicate

H2S gas odor present.

1362360061 2014-05-02 Plug / Plug Back No Violations My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe. The cement crew was sent back.
1399049324 2014-05-01 Plug / Plug Back No Violations My inspection today finds Davis Well Service moved a rig onto the location. The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042.
1399309060 2014-05-05 Plug / Plug Back No Violations My inspection today finds the casing was ripped at 3660. Cemenco circulated a 38 sk class A 2% gel plug. The casing was pulled up to 1950. Cemenco circulated a 52 sk 2% gel plug into place. A 200 54 sk plug was placed from 200 to surface. I instructed the company to reclaim the site in accordance with 1509.072.
1668780202 2014-07-02 Final Restoration No Violations Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
PL7609 PL No Violations

For data sources see[9]

References