If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-121-22260 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.68,"lon":-81.29,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Elk Township | |
Operator Name: BECK ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: ROGERS BERNADINE & MICHAEL | |
License Status: Producing | |
License Date: 1980-03-03 | |
Spud Date: 1980-03-01 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 1980-03-09 | |
Well Total Depth: 2550.00 ft | |
Configuration: Vertical | |
Latitude: 39.680000 | |
Longitude: -81.290000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1980-03-01 | |
CO | 1980-03-03 | 3927 WILMAR OIL & GAS GeoDate 3/3/80 |
Completed | 1980-03-09 | |
Reached Total Depth | 1980-03-09 | |
Completion Report Received | 1980-03-18 | |
Change of Owner | 2003-08-07 | Operator changed from 3927, WILMAR OIL & GAS to 1888, BECK ENERGY CORP |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-08-26 | 2204 | 2213 | 18 |
2006-09-11 | 2213 | 2362 | 28 |
2204 | 2213 | 18 | |
2362 | 2366 | 10 | |
2213 | 2362 | 28 | |
2204 | 2213 | 18 | |
2003-08-26 | 2362 | 2366 | 10 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 500 Bbl | 60000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | BECK ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2015 | BECK ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2016 | BECK ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2017 | BECK ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2018 | BECK ENERGY CORPORATION | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | BECK ENERGY CORPORATION | Brine | 0 | 0 |
2015 | BECK ENERGY CORPORATION | Brine | 0 | 0 |
2016 | BECK ENERGY CORPORATION | Brine | 0 | 0 |
2017 | BECK ENERGY CORPORATION | Brine | 0 | 0 |
2018 | BECK ENERGY CORPORATION | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1115975962 | 2016-4-8 0:00:0 | PW | No Violations | 2.00 |
1115975962 | 2016-04-08 | Production Wells | No Violations | My inspection today finds the well is equipped with 4.5 casing reduced to 2 pipe thread by a casing swage. The casing is hanging on a clamp resting on the 8.625 surface casing. A brass ball valve at the top of the casing swage is in the open position. The only pipeline attached to the wellhead is fitted with a Little Joe regulator. The two inch pipeline then runs to a earthen dike. The dike contains only an eight inch diameter drip which is attached to the pipeline emanating from the wellhead. A valve on top of the drip is open to atmosphere and the outlet line is severed two feet from the drip. No gas can be detected leaking from drip. |
2083774451 | 2012-04-12 | Production Wells | No Violations | Inspection of the well head found 8.625 surface casing-4.5 production casing -with reducing swage -and inline valve down to 2- valve is open and sales line hooked up but gas is venting at the old tank battery from open valve on drip tank and gas line is disconnected at this point from sales line , production tanks have been removed -no separator or gas meter present --nothing in database on reported production . |
For data sources see[9]