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34-121-21936

Well Details

Well ID: 34-121-21936
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Country: United States
State: Ohio
County: Noble
Municipality: Seneca Township
Operator Name: ZILKHA ENERGY INC
Well Pad ID:
Farm/Lease Name: BATES W
License Status: Producing
License Date: 1976-12-09
Spud Date: 1976-12-31
Spud Drilling Contractor:
Final Drill Date: 1977-01-05
Well Total Depth: 6280.00 ft
Configuration: Vertical
Latitude: 39.870000
Longitude: -81.360000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-12-09 34 ZILKHA ENERGY INC GeoDate 12/9/76
Original Spud 1976-12-31
Completed 1977-01-05
Reached Total Depth 1977-01-05
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 6102 6138 13
6102 6138 13
6102 6138 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1810 Bbl 60400

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1336796584 2019-11-1 0:00: PW No Violations 0.50
-1394147607 2019-10-22 0:00 PW No Violations 0.50
-1802823813 2015-12-30 0:00 PW No Violations
-286758056 2020-10-21 0:00 PW No Violations 1.00
-345113657 2019-10-15 0:00 PW No Violations
-491357419 2019-9-18 0:00: PW No Violations 3.00
-573810533 2019-10-15 0:00 PW No Violations 1.50
-769991279 2019-12-23 0:00 PW No Violations 0.80
-874172237 2015-12-30 0:00 PW No Violations
-884235616 2015-12-30 0:00 PW No Violations 1.00
-984701630 2019-10-11 0:00 PW No Violations 3.00
0874172237 2015-12-30 Production Wells No Violations Inspection revealed that well is being used for domestic purposes and it is equipped with 8.625 surface casing and 4.5 production casing and 1.5 tubing and there is a 20 bbl tank on site but not being used at this time and it was noted that wellhead and plumbing was painted yellow and it was also noted that 1 valve on wellhead had a small leak.
0884235616 2015-12-30 Production Wells No Violations I am accompanied today by Inspector Ball. Our inspection today finds the well is equipped with 4.5 casing and 1.5 tubing. The valves on the casing head and the tubing are steel and rated for 1500 psi. A domestic gas hook up is attached to the 4.5 casing; however the valve is closed at the casing head. Gas can be heard leaking at the surface casing head due to a partially open valve.
1001211588 2020-3-10 0:00: PW No Violations
1149712313 2019-11-18 0:00 PW No Violations 0.80
1183873676 2019-12-4 0:00: PW No Violations 0.80
1193635535 2020-5-13 0:00: PW No Violations 1.00
1234178896 2020-7-23 0:00: PW No Violations 1.00
1241854297 2020-3-10 0:00: PW No Violations 1.00
145009807 2019-12-11 0:00 PW No Violations 0.80
1451941303 2016-01-04 Production Wells No Violations At 4:00 pm I attempted to contact Zilkha Energy at the phone number listed in the RBDMS system. The phone number is no longer a working number. None of the aliases listed in RBDMS yielded any contact information.
1568751695 2019-9-17 0:00: PW No Violations 4.00
1569162823 2019-9-18 0:00: PW No Violations
1572377473 2019-10-29 0:00 PW No Violations 0.50
1572538955 2019-10-31 0:00 PW No Violations 1.00
1575472302 2019-11-13 0:00 PW No Violations 1.00
1579290209 2020-1-17 0:00: PW No Violations 0.80
1581700115 2020-2-14 0:00: PW No Violations 0.50
1585058876 2020-3-23 0:00: PW No Violations 1.00
1601891874 2020-10-3 0:00: PW No Violations 1.00
16757525 2019-11-5 0:00: PW No Violations 1.00
1802823813 2015-12-30 Production Wells No Violations At 12:55 pm, I received a telephone call from Doug Stebbins, Production Manager with Antero, stating that Antero received a complaint from Merrick Bates indicating his well was gaining pressure and he believed it was due to activities at the Bond well pad. Antero has been monitoring the well and the current pressure on the well was 1080 psi on the tubing and 420 psi on the casing. I requested information including the bond logs for the wells on the pad.
1872907723 2020-3-2 0:00:0 PW No Violations 1.00
2006775555 2020-3-17 0:00: PW No Violations 1.50
537993507 2020-10-6 0:00: PW No Violations 1.00
770425489 2020-5-5 0:00:0 PW No Violations 1.00

For data sources see[5]

References