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34-121-20411

Well Details

Well ID: 34-121-20411
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Country: United States
State: Ohio
County: Noble
Municipality: Seneca Township
Operator Name: CLEARY JON C
Well Pad ID:
Farm/Lease Name: JOHNSON
License Status: Final Restoration
License Date: 2014-01-24
Spud Date: 1944-03-06
Spud Drilling Contractor:
Final Drill Date: 1944-03-30
Well Total Depth: 1550.00 ft
Configuration: Vertical
Latitude: 39.840000
Longitude: -81.360000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1944-03-06
Completed 1944-03-30
Reached Total Depth 1944-03-30
APP 2014-01-24 Proposed Formations:BEREA, Issued Date:1/24/2014, Expired Date:1/24/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-05-22
Construction Permit Expires 2016-01-24
Record Last Modified 2017-02-15

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 CLEARY JON C 2.00 0.00 0
1986 CLEARY JON C 436.00 0.00 365
1987 CLEARY JON C 475.00 0.00 365
1988 CLEARY JON C 824.00 0.00 365
1989 CLEARY JON C 626.00 0.00 248
1997 CLEARY JON C 0.00 0.00 365
1999 CLEARY JON C 1096.00 0.00 365
2000 CLEARY JON C 1018.00 0.00 365
2001 CLEARY JON C 994.00 0.00 365
2002 CLEARY JON C 926.00 0.00 365
2003 CLEARY JON C 998.00 0.00 365
2004 CLEARY JON C 829.00 0.00 365
2005 CLEARY JON C 755.00 0.00 365
2006 CLEARY JON C 629.00 0.00 365
2007 CLEARY JON C 635.00 0.00 365
2008 CLEARY JON C 532.00 0.00 365
2009 CLEARY JON C 617.00 0.00 365
2010 CLEARY JON C 895.00 0.00 365
2011 CLEARY JON C 788.00 0.00 365
2012 CLEARY JON C 768.00 0.00 366
2013 CLEARY JON C 529.00 0.00 273

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 CLEARY JON C Brine 0 0
1986 CLEARY JON C Brine 0 365
1987 CLEARY JON C Brine 0 365
1988 CLEARY JON C Brine 0 365
1989 CLEARY JON C Brine 0 248
1997 CLEARY JON C Brine 0 365
1999 CLEARY JON C Brine 0 365
2000 CLEARY JON C Brine 0 365
2001 CLEARY JON C Brine 0 365
2002 CLEARY JON C Brine 0 365
2003 CLEARY JON C Brine 0 365
2004 CLEARY JON C Brine 0 365
2005 CLEARY JON C Brine 0 365
2006 CLEARY JON C Brine 0 365
2007 CLEARY JON C Brine 0 365
2008 CLEARY JON C Brine 0 365
2009 CLEARY JON C Brine 0 365
2010 CLEARY JON C Brine 0 365
2011 CLEARY JON C Brine 0 365
2012 CLEARY JON C Brine 0 366
2013 CLEARY JON C Brine 0 273

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1022666192 2014-1-9 0:00:0 AM No Violations 1.00
-1113908308 2014-5-21 0:00: PB No Violations 4.00
-1643479730 2014-2-21 0:00: AM No Violations
-537218397 2013-10-24 0:00 PW No Violations 4.00
0537218397 2013-10-24 Production Wells Violations Noted I met the complainant Mr. Havran and he accompanied me on the inspection. My inspection found the well was equipped with 2 tubing with 1 tubing inside of it. There is no pressure on the well and it does not appear capable of producing in its current state. The operator is back feeding gas for the land owner from another well. I spoke to the well owner, Mr. Cleary, at 11:58am on Friday 10-25-13 and informed him of the violation. Make well capable of commercial production within 90 days; or plugging is required within 90 days.

Failure to comply may result in Forfeiture of Bond.

0867782381 2013-11-20 Production Wells No Violations My inspection today finds the owner has a service rig on site. The 1 tubing is parted at 260 from surface. The rig crew ran a center spear and grabbed the pipe. They are waiting for the packer to release.
1022666192 2014-01-09 Administrative Inspection No Violations I mailed three permit applications to Mr. Cleary as he requested in a Jan. 7 conversation.
1042310461 2014-05-22 Plug / Plug Back No Violations My inspection today finds FMS Drilling ran one inch tubing to 1550. Cemenco pumped 45 sks of class A cement in three 500 lifts. Once the tubing was removed an additional 25 sks of cement was pumped through the perforations and out the back side of the pipe. I instructed the well owner to reclaim the site in accordance with 1509.072. The well has been plugged resolving the outstanding violation.
1113908308 2014-05-21 Plug / Plug Back No Violations My inspection finds FMS Drilling pulled the one inch tubing and packer out of the well. Appalachian ran a bond log on the well to determine if there are any voids behind the 2 tubing that was mudded in 1946. A void was located and three perforations were shot from 1378 to 1390. The rig crew will run the tubing back to bottom.
1243897974 2014-03-24 Administrative Inspection No Violations I received a phone message from Jon Cleary at 11:40 AM stating that he has tentatively set up contractors to plug the well around the last week of May.
1333405178 2012-04-02 Production Wells No Violations Inspection revealed that well is equipped with 2 casing and 1 tubing set on packer well is supplying gas only.
1389907056 2014-01-16 Administrative Inspection No Violations I received a call from Jon Cleary at 2:41 pm. Mr. Cleary asked for an extension to his compliance notice. He recently applied for a plugging permit and it will not be issued before Jan. 25. Mr. Cleary has made a good faith effort to gain compliance so I agreed to extend the compliance date to Feb. 25, 2014.
1408782453 2014-08-06 Final Restoration No Violations My inspection today finds the well site has been reclaimed in accordance with 1509.072B. A land owner waiver has been signed by the land owner for the above ground steel gas line to remain in place for their benefit.
1643479730 2014-02-21 Administrative Inspection No Violations I received a call from the well owner Mr. Cleary. He stated that in order to minimize the impact to local roads and the land owners property he needed an extension. Since his efforts to return the well to production failed he stated that he would plug the well. Mr. Cleary agreed to send me a letter agreeing to plug the well by June 15, 2014.
867782381 2013-11-20 0:00 PW No Violations 3.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0537218397 US-OH-125875 2013-10-28 Inadequate pipeline strength
0537218397 US-OH-125876 2013-10-28 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[7]

References