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Well ID: 34-119-27905 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Perry Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: ANDERSON ANDY | |
License Status: Producing | |
License Date: 2016-02-22 | |
Spud Date: 1994-08-10 | |
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]] | |
Final Drill Date: 1994-08-26 | |
Well Total Depth: 6565.00 ft | |
Configuration: Vertical | |
Latitude: 39.980000 | |
Longitude: -81.830000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1994-08-08 | Issued Date 8/8/94 Expired Date 8/8/95 Acres 0040000 Tool Type RTAF Proposed Formation ORSK/BKMN Proposed Depth 06565 Proposed Drill Depth 06565 |
Original Spud | 1994-08-12 | |
Completed | 1994-08-26 | |
Reached Total Depth | 1994-08-26 | |
CO | 1994-09-22 | 214 LIGHTHIZER CHARLES O GeoDate 8/8/94 |
Completion Report Received | 1994-09-28 | |
Change of Owner | 1999-03-08 | Operator changed from 214, LIGHTHIZER CHARLES O to 6405, H & H ENERGY OF OHIO |
APP | 2002-08-12 | Proposed Formations:CLINTON, Issued Date:8/12/2002, Expired Date:8/12/2003 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Change of Owner | 2007-12-24 | Operator changed from 6405, H & H ENERGY OF OHIO to 001, HOPEWELL OIL & GAS DEVELOPMENT |
APP | 2011-04-04 | Proposed Formations:BEEKMANTOWN, Issued Date:4/4/2011, Expired Date:4/3/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2015-05-29 | Operator changed from 1, HOPEWELL OIL & GAS DEVELOPMENT to 9488, SIBERIAN SOLSTICE ENERGY LLC |
APP | 2016-02-22 | Proposed Formations:ROSE RUN, Issued Date:2/22/2016, Expired Date:2/21/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2017-10-04 | Operator changed from 9488, SIBERIAN SOLSTICE ENERGY LLC to 1634, NORTHWOOD ENERGY CORP |
Record Last Modified | 2017-10-04 | |
Construction Permit Expires | 2018-02-21 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6436 | 6446 | 2 |
6430 | 6499 | 0 | |
1997-06-29 | 6430 | 6499 | 0 |
6436 | 6446 | 2 | |
6430 | 6499 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 28 | 2000 Gal | 0 | NONE |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1240535024 | 2009-12-11 0:00 | PW | No Violations | |
-1398834847 | 2018-4-12 0:00: | PW | No Violations | 1.00 |
-575312606 | 2009-12-11 0:00 | PW | No Violations | |
-690228089 | 2019-5-2 0:00:0 | PW | No Violations | 0.20 |
0000016551 | Final Restoration | No Violations | PASSED Y WITNESSED 11/28/95 INSPECTOR MIKE PHELPS DATE 11/2819/95 DATA FROM OLD VAX INFO | |
0455391011 | 2016-04-14 | Administrative Inspection | No Violations | Anthony Moore the land owner and complainant called on the status of the well plugging. I stated that there was a 90 day extension given to the company per approval of Deputy Chief. |
0575312606 | 2009-12-11 | Production Wells | No Violations | FOLLOW UP TO NOV # -1240535024 Well is shut in. Status of well should be PR as this well has been plugged back. |
1240535024 | 2009-12-11 | Production Wells | Violations Noted | Well is shut in. Status of well should be PR as this well has been plugged back. |
1245435250 | 2015-10-05 | Production Wells | Violations Noted | I met with landowner named Tony Moore on idle well. The complaint is filed under complaint #5139. The well is equipped with a tubing head and rods and tubing and stuffing box left in place. The rod annulus and the tubing annulus is shut in. There is 2.375upset 8 round tubing present. There is 2.375upset tubing that is laying on ground. There is a 210 barrel steel tank battery with a small dike and no identification present. There is large Bremco horizontal separator that is not hooked up. There is a vertical separator that is hooked up to tank battery. It may be coming from another well. The well owner /operator shall submit a written plugging schedule to Patrick Shreve at 5880 Memory Rd. Zanesville, Ohio 43701 within 30 days per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1260820561 | 2009-12-14 | Administrative Inspection | No Violations | |
1398834847 | 2018-04-12 | Production Wells | No Violations | The day of the inspection is a follow-up to Compliance Follow-up numbers 1245435250, -1240535024 respectively and complaint number 5139. The day of inspection revealed that Corp Oil field services is fixing the road into the well with a dozer. The bridge has been repaired to mobilize the equipment. The well is equipped with no pumping unit on the well head. The rods and tubing and packing glands were in place. The production manifold shows that the rod and tubing annulus were still shut. There is a horizontal separator and a vertical separator. They are both shut in. The 1-210- |
1468954308 | 2016-07-19 | Production Wells | No Violations | On day of inspection as a follow-up to Compliance Follow-up numbers 1245435250,-1240535024 respectively the following was revealed that there was no pumping unit on the well head. The rods and tubing and packing glands were in place. The production manifold shows that the rod and tubing annulus were still shut. There is a horizontal separator and a vertical separator. They are both shut in. The 1- |
1547059052 | 2019-01-09 | Production Wells | No Violations | The inspection is conducted as a follow up to the prior Compliance Notices. R & B Drilling is rigged up over the well and has pulled the rods and 2 3/8--1-94 and showed the top of the 2--2983 feet. The Oriskany sandstone is at top of that cement plug. The top of the Big Lime is at 2870 feet. The Clinton perforations are 4200-4256 with 11 shots. Company will perform a squeeze job and place cement 600 feet above the Oriskany later this year. |
16551 | FR | No Violations | ||
455391011 | 2016-4-14 0:00: | AM | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1240535024 | US-OH-106409 | 2009-12-14 | Well shall be plugged | |
1245435250 | US-OH-106550 | 2015-11-24 | Failure to legibly identify well | |
1245435250 | US-OH-106551 | 2015-11-24 | Well shall be plugged |
For data sources see[9]