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Well ID: 34-119-24758 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Perry Township | |
Operator Name: ECLIPSE RESOURCES-OHIO LLC | |
Well Pad ID: | |
Farm/Lease Name: OXFORD-ALPINE FEE (SWIW #23) | |
License Status: Final Restoration | |
License Date: 2016-04-27 | |
Spud Date: 1984-04-13 | |
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS | |
Final Drill Date: 1984-04-20 | |
Well Total Depth: 4167.00 ft | |
Configuration: Vertical | |
Latitude: 39.970000 | |
Longitude: -81.890000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-07-01 | Issued Date 7/1/82 Expired Date 1/1/83 Acres 0040000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1984-03-23 | 79 OXFORD OIL CO GeoDate 3/23/84 |
Oil and Gas | 1984-03-23 | Issued Date 3/23/84 Expired Date 9/19/84 Acres 0040000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 04167 Proposed Drill Depth 04167 |
Original Spud | 1984-04-13 | P & A PER DAVE BALL INSPECTION |
Completed | 1984-04-20 | P & A PER DAVE BALL INSPECTION |
Reached Total Depth | 1984-04-20 | P & A PER DAVE BALL INSPECTION |
Completion Report Received | 1984-05-09 | P & A PER DAVE BALL INSPECTION |
CO | 1984-05-25 | 79 OXFORD OIL CO GeoDate 7/1/82 |
CO | 1995-02-27 | 79 OXFORD OIL CO GeoDate 2/27/95 |
Conversion to Injector | 1995-02-27 | |
Salt Water Injection Well | 1995-02-27 | Issued Date 2/27/95 Expired Date 2/27/96 Acres 0085000 Tool Type NT Proposed Formation CLINTON Proposed Depth Proposed Drill Depth |
Storage Well | 1995-02-27 | Issued Date 2/27/95 Expired Date 2/27/96 Acres 0085000 Tool Type NT Proposed Formation CLINTON Proposed Depth Proposed Drill Depth |
Annulus Pressure Monitoring Approved | 1995-10-24 | P & A PER DAVE BALL INSPECTION |
First Injection | 1996-03-22 | P & A PER DAVE BALL INSPECTION |
Change of Owner | 2014-02-06 | Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC |
Last Compliance Report | 2014-12-05 | P & A PER DAVE BALL INSPECTION |
APP | 2016-04-27 | Proposed Formations:MEDINA SANDSTONE, Issued Date:4/27/2016, Expired Date:4/27/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:SWIW |
Plugged/Abandoned | 2016-05-12 | P & A PER DAVE BALL INSPECTION |
Record Last Modified | 2017-02-15 | P & A PER DAVE BALL INSPECTION |
Construction Permit Expires | 2018-04-27 | P & A PER DAVE BALL INSPECTION |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3477 | 4085 | 33 |
2014-12-05 | 3977 | 4085 | 33 |
3477 | 4085 | 33 | |
3977 | 4085 | 33 | |
3477 | 4085 | 33 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
FOAM | 0 | 2487 Bbl | 0 | FRAC;H2O,20/40 SAND, ALSO COMPLETED MEDINA SANDSTONE |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OXFORD OIL | 2326.00 | 69.00 | 0 |
1985 | OXFORD OIL | 9496.00 | 305.00 | 365 |
1986 | OXFORD OIL | 2815.00 | 292.00 | 365 |
1987 | OXFORD OIL | 710.00 | 527.00 | 365 |
1988 | OXFORD OIL | 0.00 | 551.00 | 365 |
1989 | OXFORD OIL | 1307.00 | 338.00 | 365 |
1990 | OXFORD OIL | 2165.00 | 262.00 | 365 |
1991 | OXFORD OIL | 2858.00 | 388.00 | 365 |
1992 | OXFORD OIL | 1954.00 | 191.00 | 365 |
1993 | OXFORD OIL | 2394.00 | 0.00 | 365 |
1994 | OXFORD OIL | 2077.00 | 450.00 | 365 |
1995 | OXFORD OIL | 1322.00 | 502.00 | 365 |
1996 | OXFORD OIL | 0.00 | 473.00 | 366 |
1997 | OXFORD OIL | 0.00 | 286.00 | 365 |
1998 | OXFORD OIL | 0.00 | 219.00 | 365 |
1999 | OXFORD OIL | 2147.00 | 233.00 | 365 |
2000 | OXFORD OIL | 0.00 | 248.00 | 0 |
2001 | OXFORD OIL | 0.00 | 218.00 | 365 |
2002 | OXFORD OIL | 0.00 | 244.00 | 365 |
2003 | OXFORD OIL | 0.00 | 375.00 | 365 |
2004 | OXFORD OIL | 0.00 | 384.00 | 365 |
2005 | OXFORD OIL | 0.00 | 362.00 | 365 |
2006 | OXFORD OIL | 0.00 | 388.00 | 365 |
2007 | OXFORD OIL | 0.00 | 0.00 | 365 |
2008 | OXFORD OIL | 0.00 | 540.00 | 0 |
2009 | OXFORD OIL | 0.00 | 500.00 | 0 |
2010 | OXFORD OIL | 0.00 | 1013.00 | 365 |
2011 | OXFORD OIL | 0.00 | 270.00 | 0 |
2012 | OXFORD OIL | 0.00 | 517.00 | 0 |
2013 | ECLIPSE RESOURCES-OHIO LLC | 0.00 | 219.00 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | 0.00 | 295.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OXFORD OIL | Brine | 0 | 0 |
1985 | OXFORD OIL | Brine | 330 | 365 |
1986 | OXFORD OIL | Brine | 356 | 365 |
1987 | OXFORD OIL | Brine | 434 | 365 |
1988 | OXFORD OIL | Brine | 260 | 365 |
1989 | OXFORD OIL | Brine | 120 | 365 |
1990 | OXFORD OIL | Brine | 275 | 365 |
1991 | OXFORD OIL | Brine | 200 | 365 |
1992 | OXFORD OIL | Brine | 106 | 365 |
1993 | OXFORD OIL | Brine | 100 | 365 |
1994 | OXFORD OIL | Brine | 235 | 365 |
1995 | OXFORD OIL | Brine | 125 | 365 |
1996 | OXFORD OIL | Brine | 2353 | 366 |
1997 | OXFORD OIL | Brine | 850 | 365 |
1998 | OXFORD OIL | Brine | 540 | 365 |
1999 | OXFORD OIL | Brine | 1917 | 365 |
2000 | OXFORD OIL | Brine | 2594 | |
2001 | OXFORD OIL | Brine | 1192 | 365 |
2002 | OXFORD OIL | Brine | 1817 | 365 |
2003 | OXFORD OIL | Brine | 2963 | 365 |
2004 | OXFORD OIL | Brine | 1343 | 365 |
2005 | OXFORD OIL | Brine | 1695 | 365 |
2006 | OXFORD OIL | Brine | 515 | 365 |
2007 | OXFORD OIL | Brine | 1010 | 365 |
2008 | OXFORD OIL | Brine | 998 | |
2009 | OXFORD OIL | Brine | 775 | |
2010 | OXFORD OIL | Brine | 0 | 365 |
2011 | OXFORD OIL | Brine | 595 | |
2012 | OXFORD OIL | Brine | 825 | |
2013 | ECLIPSE RESOURCES-OHIO LLC | Brine | 340 | 365 |
2014 | ECLIPSE RESOURCES-OHIO LLC | Brine | 775 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-108845484 | 2003-6-16 0:00: | SW | No Violations | |
-1161754604 | 2003-4-8 0:00:0 | SW | No Violations | |
-1199957687 | 2014-1-29 0:00: | SW | No Violations | |
-1222855483 | 2006-3-27 0:00: | SW | No Violations | |
-1269881429 | 2012-8-23 0:00: | SW | No Violations | |
-1274478557 | 2011-3-29 0:00: | SW | No Violations | |
-1311104233 | 2014-9-25 0:00: | SW | No Violations | |
-1319432556 | 2016-4-12 0:00: | SW | No Violations | |
-1325485706 | 2015-9-28 0:00: | SW | No Violations | |
-1342174490 | 2015-4-1 0:00:0 | SW | No Violations | |
-142224653 | 2014-7-9 0:00:0 | SW | No Violations | |
-1594230750 | 2013-5-20 0:00: | SW | No Violations | |
-1662291687 | 2012-1-30 0:00: | SW | No Violations | 1.00 |
-1721506496 | 2009-9-4 0:00:0 | SW | No Violations | |
-1775092436 | 2011-9-23 0:00: | SW | No Violations | 1.00 |
-1782671948 | 2016-6-9 0:00:0 | FR | No Violations | |
-1814164920 | 2011-7-6 0:00:0 | SW | No Violations | 1.00 |
-1888463615 | 2012-10-18 0:00 | SW | No Violations | |
-1918202183 | 2013-2-13 0:00: | SW | No Violations | |
-1932979888 | 2009-9-2 0:00:0 | SW | No Violations | |
-2019655762 | 2012-5-14 0:00: | SW | No Violations | |
-2026899666 | 2014-12-4 0:00: | SW | No Violations | |
-2057915062 | 2014-3-7 0:00:0 | SW | No Violations | |
-256115675 | 2012-10-26 0:00 | SW | No Violations | |
-276972628 | 2003-10-2 0:00: | SW | No Violations | |
-280640592 | 2003-5-21 0:00: | SW | No Violations | |
-346469188 | 2014-11-10 0:00 | SW | No Violations | |
-382873628 | 2005-11-10 0:00 | SW | No Violations | |
-401186765 | 2013-10-28 0:00 | SW | No Violations | |
-414709229 | 2016-3-16 0:00: | SW | No Violations | |
-519931594 | 2008-3-10 0:00: | SW | No Violations | |
-531197317 | 2003-7-25 0:00: | SW | No Violations | |
-545272000 | 2014-11-21 0:00 | SW | No Violations | |
-577796001 | 2009-6-9 0:00:0 | SW | No Violations | |
-63577639 | 2012-3-22 0:00: | SW | No Violations | 2.00 |
-641856128 | 2004-7-29 0:00: | SW | No Violations | 11.00 |
-765483610 | 2011-10-14 0:00 | SW | No Violations | 1.00 |
-833204541 | 2014-12-2 0:00: | SW | No Violations | |
-87188194 | 2015-6-16 0:00: | SW | No Violations | |
-985477987 | 2013-9-23 0:00: | SW | No Violations | |
0063577639 | 2012-03-22 | Salt Water Injection Well | No Violations | On day of inspection Tank Pad was under construction. Oxford brought large crane in and removed 3-210 barrel tanks and replaced with a 500 barrel tank. That work was performed on 3-16-2012.Oxford and I performed a mini test on annulus.40 psi in tubing and 120 psi was held on annulus for 30 minutes. |
0087188194 | 2015-06-16 | Salt Water Injection Well | No Violations | Well not in operation today. |
0108845484 | 2003-06-16 | Salt Water Injection Well | No Violations
-5/8 annulus. ID sign at wellhead will be replaced per Tony. | |
0142224653 | 2014-07-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection. |
0256115675 | 2012-10-26 | Salt Water Injection Well | No Violations | On site to witness new Parmaco Tension packer and used 2.375 tubing run in hole and annulus flushed with fresh water and inhibitor,they ran 3933.45 of tubing plus 2.95 packer element equals 3936.40 is setting depth of packer and it is set in tension12K AND ANNULUS WAS FLUSHED WITH 54 BBL WATER AND 5 GAL OF INHIBITOR AND WE PRESSURED TESTED IT AT 1060 PSI WITH NO DECLINE IN PRESSURE.
Chiefs Order2012-29 has been resolved as of this date. |
0256834619 | 2015-06-02 | Salt Water Injection Well | No Violations | Injection pump was in operation during my inspection. |
0276972628 | 2003-10-02 | Salt Water Injection Well | No Violations | CHECKED SURFACE FACILITY. WELL JUST REWORKED AND PASSED MIT. DID NOT CHECK WELL. |
0280168806 | 2009-09-04 | Salt Water Injection Well | No Violations | Ran tbg and packer and displaced inhibited fresh water into annulus. Tested to 960 psig for 15 minutes w/ no drop in pressure. NOV satisfied. Dave Ball covered for this inspector who was on vacation. |
0280640592 | 2003-05-21 | Salt Water Injection Well | No Violations | |
0346469188 | 2014-11-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that one company owned vacuum truck was unloading at the facility during my inspection. |
0382873628 | 2005-11-10 | Salt Water Injection Well | No Violations | |
0401186765 | 2013-10-28 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
0414709229 | 2016-03-16 | Salt Water Injection Well | Violations Noted | Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15th for 2015, despite a letter that was sent March 1, 2016 with a deadline of March 15, 2016 to submit the reports requested. REPORTS RECEIVED |
0441192414 | 2010-03-18 | Salt Water Injection Well | No Violations | Well was not in operation at time of inspection. Tubing 410 psig, annulus 5 psig. No problems noted at time of inspection. |
0509466414 | 2012-10-19 | Salt Water Injection Well | No Violations | On site to try and locate hole in 4.5 casing rig crew ran test packer in hole @500 intervals and set packer and pressure tested@750 psi at each respected interval it was determined that hole was in the area of 2556-3150 with is cement top on backside of casing,will further pinpoint casing problem on10/21/12. |
0519931594 | 2008-03-10 | Salt Water Injection Well | No Violations | Well was not in operation. No problems noted. |
0531197317 | 2003-07-25 | Salt Water Injection Well | No Violations
-5/8x4-1/2 annulus... going to put rig on well to check it out. | |
0545272000 | 2014-11-21 | Salt Water Injection Well | No Violations | Inspection revealed that Harmon Well Service was trying to release packer and remove it from well bore they plan on getting out of hole today and start new packer and used tubing back into well on 11/24/14. |
0577796001 | 2009-06-09 | Salt Water Injection Well | No Violations | Well was in operation. Sump okay, ID okay, Pad and Impoundment okay. No problems noted. |
0601009704 | 2005-03-04 | Salt Water Injection Well | No Violations | |
0633735980 | 2015-01-08 | Salt Water Injection Well | No Violations | Inspection reveled that injection pump was not in operation today and according to well tender they are not receiving much water this week due to in climate weather. |
0637042921 | 2012-10-22 | Salt Water Injection Well | No Violations | On site to witness operator try and locate hole in production casing and once located we set a composite bridge plug at 3200 and we perforated casing at old cement top@3150 and then we proceeded to pump 200 sacks Class A cement with 2%gel and estimated top of cement should be at 2000 +- Formation Cementing displaced wiper plug down to 2550 and we shut well in for the night they will resume operations tomorrow. |
0641856128 | 2004-07-29 | Salt Water Injection Well | No Violations | No problems noted |
0691334013 | 2011-12-29 | Salt Water Injection Well | No Violations | On day of inspection no violations noted. |
0765483610 | 2011-10-14 | Salt Water Injection Well | No Violations | No violations on day of inspection. |
0767856257 | 2009-03-25 | Salt Water Injection Well | No Violations | All is in order. No problems noted. |
0833204541 | 2014-12-02 | Salt Water Injection Well | No Violations | Harmon Well Service on site drilling out cement plug and once cement was drilled out they stopped and we pressure tested casing at 950 psi to ensure they have good integrity and tomorrow they will drill out bridge plug and clean out wellbore to bottom and come out of hole and then they will start a new packer and tubing in well. |
0925119755 | 2015-07-21 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that one company owned vacuum truck dropped off one load of brine on this day. |
0985477987 | 2013-09-23 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and facility appears to be in satisfactory condition this inspection. |
1001955239 | 2016-05-11 | Plug / Plug Back | No Violations | On site to witness setting of bottom hole plug and lime plug and Berea plug operator will rip 4.5 casing off in the morning and finish plugging operation.
Note: Formation cementing was cement contractor and they used a total of 77 sacks of Class A cement today along with gel spacers in between required plugs. |
1032140345 | 2004-12-07 | Salt Water Injection Well | No Violations | Okay |
1065094683 | 2003-09-16 | Salt Water Injection Well | No Violations | Ran Howco R-4 packer on seal lock tubing to 3928. Displaced 43 bbls of inhibited (with Treat-O-Lite R- |
1074004974 | 2004-01-13 | Salt Water Injection Well | No Violations | Looks good. |
1080672006 | 2004-03-30 | Salt Water Injection Well | No Violations | Injection pump had just shut down. No problems noted. |
1097070434 | 2004-10-06 | Salt Water Injection Well | No Violations | Looks good |
1152204532 | 2006-07-06 | Salt Water Injection Well | No Violations | |
1161754604 | 2003-04-08 | Salt Water Injection Well | No Violations | Not injecting at time of inspection. Oil around well head. |
1161797525 | 2006-10-25 | Surface Facility Construction | No Violations | |
1168007066 | 2007-01-05 | Salt Water Injection Well | Violations Noted | Looks like packer or tubing has failed. Tubing and casing equalized (differential between fresh water and salt water ~200psi) 275 tbg vs 480 csg |
1169035625 | 2007-01-16 | Work Over Reconditioning | No Violations | Ran R-4 packer on 2-3/8 used tubing. Packer to be set at 3902.9. Will displace inhibited fresh water, set packer and test on 1/17/2007. |
1169147572 | 2007-01-17 | Salt Water Injection Well | No Violations | Ran packer and tubing to 3903. Displaced 41 bbls of inhibited fresh water into annulus and tested annulus to 940 for 15 minutes. Test held. |
1185383190 | 2007-07-25 | Salt Water Injection Well | No Violations | Looks good. No problems noted |
1197615195 | 2014-11-20 | Salt Water Injection Well | No Violations | Inspection revealed that Harmon Well Service has moved there service rig on site to change out tubing and packer in well, on this day they released packer and started it out of hole and they plan on starting new packer back into well tomorrow if weather permits. |
1199957687 | 2014-01-29 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it appears that well is not being used much at this time due to extreme cold weather conditions. |
1210i20544 | 2001-11-14 | Salt Water Injection Well | No Violations | Accompanied by Tom Tomastik, and Dave Hodges. Well and facility in good shape. Need well head ID remarked , 1501:9-3-06 (H). Informed Toni of this and left a copy of report with him. |
1210i2054497 | 2001-11-14 0:00 | SW | No Violations | |
1216827512 | 2008-06-30 | Salt Water Injection Well | No Violations | Well was not in operation. Need new ID on well. (told Tony). No other problems noted. |
1221670754 | 2008-09-17 | Salt Water Injection Well | No Violations | Need new ID on well. Told Tony again. He will comply this time. No other problems noted. |
1222855483 | 2006-03-27 | Salt Water Injection Well | No Violations | Okay, not in operation. All looks good. |
1228846172 | 2008-12-09 | Salt Water Injection Well | No Violations | Not injecting when checked. ID replaced as requested last time. No problems noted. Tubing 135 psig. Annulus 10psig. |
1254372560 | 2013-07-05 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not operating during my inspection.
Note: Unloading pad is in need of a good cleaning. |
1260896518 | 2009-12-15 | Salt Water Injection Well | No Violations | Well in operation at the time of the inspection. Tanks and unloading pad in good repair. ID in place, no problems noted. Well ID in place. Tubing 540 psig. Annulus 825 psig. |
1269881429 | 2012-08-23 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that annulus pressure has fallen to zero and I talked to company rep requesting that they perform mini MIT test on annulus and he stated that they would set one up for next week. |
1274478557 | 2011-03-29 | Salt Water Injection Well | No Violations | Ran Parmaco tension packer and 132 jts of 2-3/8 EUE tubing to 3916.4 Pumped inhibited fresh water down tubing and up the annulus to surface. Set packer in tension with 10,000#. Pressure tested the annulus to 1100psig with 40 psi drop (due to leaking stem on 1/4 valve) for 15 minutes. Test passed. Well will be put back in operation as soon as it can be plumbed in. |
1277818524 | 2010-06-17 | Salt Water Injection Well | No Violations | Well in operation at time of inspection. Both tank battery and well in good repair, no problems noted. Annulus 10 psig, tubing 560 psig. |
1284637495 | 2010-09-15 | Salt Water Injection Well | No Violations | Well was in operation when inspected. Packing was leaking on pump and drip pan was full. No other problems noted. |
1300970756 | 2011-03-24 | Salt Water Injection Well | Violations Noted | Tubing 720 psig. Annulus 660 psig. Well was operating when inspected but was then shut down. Contacted Tony Blizzard. No other problems noted. A rig will move on the well on 3/28/2011. |
1311104233 | 2014-09-25 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that one company owned vacuum truck was unloading at the facility during my inspection. |
1313665755 | 2011-08-17 | Salt Water Injection Well | No Violations | Checked well pressures and the facility. No violations noted. |
1319432556 | 2016-04-12 | Salt Water Injection Well | No Violations | Inspection today revealed that well is still incapable of injection due to fact that it equalized and according to owner they are evaluating well cost to repair said well. |
1325485706 | 2015-09-28 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that one company owned vacuum truck was unloading at the facility on this day of my inspections. |
1342174490 | 2015-04-01 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and I stopped at the company office and talked to Tony Blizzard and told him to have positive pressure applied to annulus of tubing in the near future. |
1349993175 | 2012-10-11 | Salt Water Injection Well | No Violations | Upon performing mini test on well it was determined that 4.5 casing has lost integrity we pressure tested annulus @500 psi and they loss pressure within 10 seconds ,told well owner to shut well down until repairs can be made to casing and too submit repair plan to UIC Dept in Central Office. |
1351250633 | 2012-10-23 | Salt Water Injection Well | No Violations | Tagged cement plug @2540 operator will drill cement from inside of casing and then we will perform integrity test on casing before drilling out bridge plug. |
1353871187 | 2007-09-20 | Salt Water Injection Well | No Violations | No problems noted. |
1357159464 | 2013-01-02 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today due to extreme cold weather. |
1363898474 | 2013-03-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and according to well tender there has not been much activity at site recently due to weather conditions. |
1366290572 | 2013-04-16 | Salt Water Injection Well | No Violations | Onsite to witness pressure testing of annulus of tubing after valve froze and busted during recent cold spell, replaced valve and applied 470 pounds of pressure to annulus of tubing and we monitored pressure for 15 minutes with no decline in pressure. |
1367536032 | 2013-05-02 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was just being started when I arrived on site for my inspection and I stopped and talked to Jack Greene about getting seed&mulch on area of old working pit to help bind the soils and to prevent any erosion issues that may arise. |
1368055102 | 2010-12-07 | Salt Water Injection Well | No Violations | Well was in operation. Tubing injection pressure 690 psig. Annulus 0 psig. No problems noted at time of inspection. |
1374417115 | 2013-07-19 | Salt Water Injection Well | No Violations | Injection pump not in operation today, unloading pad recently cleaned and facility appears to be in satisfactory condition this inspection. |
1376947639 | 2013-08-19 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and in conversation with well tender requesting that they replace there gauge on tubing it appears to be faulty. |
1386113841 | 2013-12-03 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and we discussed what was needed to place brine storage facility within there yard, contacted central office and had them send info to there office pertaining to approved brine storage sites. |
1409784399 | 2013-04-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Pressure needs to be applied to annulus of tubing to ensure that we have casing integrity. |
1416956801 | 2014-11-24 | Salt Water Injection Well | No Violations | On site to witness Harmon Well Service run new R-4 Halliburton packer and used 2.375 tubing in well and they set packer at 3934 and we tried to pressure test the integrity of casing and test failed and they unset packer and moved it up the hole too 3924 and tried to pressure test it again and test failed again we then put pressure gauge on 8 and we noticed a pressure increase when they applied pressure which indicated that 4.5 has a hole in it and then we shut down for the night and we intend to perform further testing tomorrow to try and pinpoint hole in casing. |
1417088723 | 2014-11-26 | Salt Water Injection Well | No Violations | On site to witness Timco Wireline Services set drillable bridge plug and Formation Cementing pump 395 sacks of cement for squeeze job to repair hole in casing, cement did not circulate to surface as calculated and company is going to run bond log on 12/1/14 to confirm cement top. |
1417468959 | 2014-12-01 | Salt Water Injection Well | No Violations | Inspection revealed that Timco Wireline bond logged well and cement top was noted at 650 on annulus of casing and owner is planning on drilling cement out from inside of casing and then pressure test casing and if it OK they will drill out bridge plug and go to bottom. |
1423684814 | 2015-02-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and both storage tank and well head were properly identified. |
1441138413 | 2015-08-31 | Salt Water Injection Well | No Violations | Inspection on this day indicated that injection pump was not in operation on the day of my inspection and it was noted that one company owned vacuum truck was unloading at the facility on the day of my inspection. |
1448541759 | 2015-11-23 | Salt Water Injection Well | No Violations | Inspection revealed that well is equalized and I contacted company rep to inform him of problem he stated they would get service rig on the well site as soon as possible to replace tubing and packer and they will submit plan to the division on there plan to repair well. |
1452884476 | 2016-01-15 | Salt Water Injection Well | No Violations | Inspection on this day indicated that well is still down waiting on service rig to repair problem with tubing/packer assembly. |
1456343431 | 2016-02-23 | Salt Water Injection Well | No Violations | Inspection revealed that well is still down waiting on owner to secure service rig contract to repair said well. |
1457980661 | 2016-03-11 | Salt Water Injection Well | No Violations | Inspection today revealed that well is still incapable of injection due to tubing/packer failure owner claims they are going to repair well when the economics are right for there operation. |
1463000062 | 2016-05-10 | Salt Water Injection Well | No Violations | On site to witness releasing of packer and pulling it from well in preparation for plugging operation. |
1463076669 | 2016-05-12 | Plug / Plug Back | No Violations | I am onsite to witness the plugging operations. Wrights Well Service attempted to rip the casing at 704, 450, and 238. After ripping each time an attempt to pull the casing and circulate was made. The casing moved a few inches, while pulling 60,000 pounds, after ripping at 238. Circulation could not be established. The determination to back off casing was made after attempts to pull the casing were unsuccessful. The casing was backed off at 98 and recovered from the same point. 125 of 2.375 tubing were placed in the well and a 65 sack class A plug was circulated to surface. |
1546848860 | 2011-03-28 | Salt Water Injection Well | No Violations | Parted tubing trying to get packer loose. Ran in hole with overshot and sat down on fish. POOH with tubing to overshot. Shut down for night. |
1553469494 | 2005-06-23 | Salt Water Injection Well | No Violations | Okay . |
1559380656 | 2001-11-14 | Salt Water Injection Well | Violations Noted | FOLLOW UP TO NOV # 1210i20 Accompanied by Tom Tomastik, and Dave Hodges. Well and facility in good shape. Need well head ID remarked , 1501:9-3-06 (H). Informed Toni of this and left a copy of report with him. |
1582801666 | 2015-03-06 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that one company owned truck was setting on unloading pad today. |
1594230750 | 2013-05-20 | Salt Water Injection Well | No Violations | Well not in operation today and containment was in good repair and it was noted that in area of old working pit had been graded and I stopped at office and told them to apply seed and mulch to exposed area and company rep stated that they would perform task later today. |
1636435764 | 2012-10-25 | Salt Water Injection Well | No Violations | Well cleaned out to 4020 then they went on to bottom and circulated well and once hole cleaned up we pressured testing casing to 1000 psi to ensure we had regained integrity with casing and once test passed we removed tubing from well and then Timco Wireline Services bond logged well to determine new cement top on backside of casing it was located @2305 shut down for the night will run new packer and used tubing back into well tomorrow. |
1662291687 | 2012-01-30 | Salt Water Injection Well | No Violations | On day of inspection the well was not pumping and there were no violations.Met with Oxford on replacing tanks and reworking dike. |
1721506496 | 2009-09-04 | Salt Water Injection Well | No Violations | On site to witness operator run Packer and tubing back into well and pressure casing.
Operator ran 3897 of used 2.375 tubing and a rebuilt Parmaco packer in well bore setting depth of packer is 3901.30,Producers Services flushed annulus of tubing with 60 bbl of fresh water with anhib and pressured tested at 960 psi with no decline in pressure(TEST PASSED) owner will place well back into operation 9/9/09. |
1775092436 | 2011-09-23 | Salt Water Injection Well | No Violations | On day of inspection well was in production and no violations were noted. Oxford will change a tank out soon. |
1782671948 | 2016-06-09 | Final Restoration | No Violations | Inspection revealed that well has been properly plugged and owner has the pit filled in and site restored and vegetation has been established. |
1814164920 | 2011-07-06 | Salt Water Injection Well | No Violations | Checked facility and pressures at well head. No violations noted. |
1831450649 | 2012-11-26 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Stopped and talked to company rep regarding closing of open pit that was used when owner pulled packer and replaced tubing on said well he stated that he would get started on it later today. |
1863706635 | 2011-11-18 | Salt Water Injection Well | No Violations | No violations on day of inspection. May need to replace tank in the near future. Well was not pumping at time of inspection. |
1888463615 | 2012-10-18 | Salt Water Injection Well | No Violations | Inspection revealed that Chipco Well Services was on site to release packer and pull tubing and then go in hole with test packer to try and locate hole in 4.5 production casing.
Note: Packer was released and tubing started out of hole on this date. |
1908882015 | 2012-02-23 | Salt Water Injection Well | No Violations | On day of inspection well was not being pumped into. I met with John Straker of Oxford and talked about the tank needing replaced. They will place a 500bbl tank in the dike and repair the dike. We plan to do a mini test on the annulus as soon as the solvent truck is repaired. |
1918202183 | 2013-02-13 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and facility is in satisfactory condition this inspection. |
1932979888 | 2009-09-02 | Salt Water Injection Well | No Violations | Found that well had equalized across tubing and annulus. Spoke with John Staker who said they would repair the well ASAP. Replace faulty tubing or packer, put new inhibitor in annulus and test to at least maximum injsction pressure for 15 minutes. |
1955861573 | 2004-12-29 | Salt Water Injection Well | No Violations | NO problems noted. Injection pump has been removed |
1976194475 | 2015-06-30 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
2019655762 | 2012-05-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection.
Note: Housekeeping needed in unloading pad area. |
2026899666 | 2014-12-04 | Salt Water Injection Well | No Violations | On site to witness tubing and packer run in well and fresh water and inhibitor pumped too check annulus of tubing for integrity.
Note: Packer set at 3934 and good used 2.375 tubing and we pressure tested annulus at 1020 psi for 15 min. with no decline in pressure and owner is going to replumb the top of tubing and place new 1/4 valves on tubing head. |
2057915062 | 2014-03-07 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: It appears that company is planning on constructing brine storage facility near this injection well facility. |
2065543546 | 2007-12-26 | Salt Water Injection Well | No Violations | No problems noted. Well in operation |
256834619 | 2015-6-2 0:00:0 | SW | No Violations | |
280168806 | 2009-9-4 0:00:0 | SW | No Violations | |
441192414 | 2010-3-18 0:00: | SW | No Violations | |
509466414 | 2012-10-19 0:00 | SW | No Violations | 8.00 |
601009704 | 2005-3-4 0:00:0 | SW | No Violations | |
633735980 | 2015-1-8 0:00:0 | SW | No Violations | |
637042921 | 2012-10-22 0:00 | SW | No Violations | |
691334013 | 2011-12-29 0:00 | SW | No Violations | 1.00 |
767856257 | 2009-3-25 0:00: | SW | No Violations | |
925119755 | 2015-7-21 0:00: | SW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0414709229 | US-OH-124412 | 2016-04-04 | Failure to file salt water injection annual report | |
1168007066 | US-OH-104449 | 2007-01-05 | Mechanical failure/contamination | |
1300970756 | US-OH-108493 | 2011-03-29 | Mechanical failure/contamination | |
1559380656 | US-OH-115228 | 2002-07-11 | Well shall be plugged |
For data sources see[9]