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34-119-24758

Well Details

Well ID: 34-119-24758
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Country: United States
State: Ohio
County: Muskingum
Municipality: Perry Township
Operator Name: ECLIPSE RESOURCES-OHIO LLC
Well Pad ID:
Farm/Lease Name: OXFORD-ALPINE FEE (SWIW #23)
License Status: Final Restoration
License Date: 2016-04-27
Spud Date: 1984-04-13
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 1984-04-20
Well Total Depth: 4167.00 ft
Configuration: Vertical
Latitude: 39.970000
Longitude: -81.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-07-01 Issued Date 7/1/82 Expired Date 1/1/83 Acres 0040000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-03-23 79 OXFORD OIL CO GeoDate 3/23/84
Oil and Gas 1984-03-23 Issued Date 3/23/84 Expired Date 9/19/84 Acres 0040000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 04167 Proposed Drill Depth 04167
Original Spud 1984-04-13 P & A PER DAVE BALL INSPECTION
Completed 1984-04-20 P & A PER DAVE BALL INSPECTION
Reached Total Depth 1984-04-20 P & A PER DAVE BALL INSPECTION
Completion Report Received 1984-05-09 P & A PER DAVE BALL INSPECTION
CO 1984-05-25 79 OXFORD OIL CO GeoDate 7/1/82
CO 1995-02-27 79 OXFORD OIL CO GeoDate 2/27/95
Conversion to Injector 1995-02-27
Salt Water Injection Well 1995-02-27 Issued Date 2/27/95 Expired Date 2/27/96 Acres 0085000 Tool Type NT Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
Storage Well 1995-02-27 Issued Date 2/27/95 Expired Date 2/27/96 Acres 0085000 Tool Type NT Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
Annulus Pressure Monitoring Approved 1995-10-24 P & A PER DAVE BALL INSPECTION
First Injection 1996-03-22 P & A PER DAVE BALL INSPECTION
Change of Owner 2014-02-06 Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC
Last Compliance Report 2014-12-05 P & A PER DAVE BALL INSPECTION
APP 2016-04-27 Proposed Formations:MEDINA SANDSTONE, Issued Date:4/27/2016, Expired Date:4/27/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:SWIW
Plugged/Abandoned 2016-05-12 P & A PER DAVE BALL INSPECTION
Record Last Modified 2017-02-15 P & A PER DAVE BALL INSPECTION
Construction Permit Expires 2018-04-27 P & A PER DAVE BALL INSPECTION

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3477 4085 33
2014-12-05 3977 4085 33
3477 4085 33
3977 4085 33
3477 4085 33

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
FOAM 0 2487 Bbl 0 FRAC;H2O,20/40 SAND, ALSO COMPLETED MEDINA SANDSTONE

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OXFORD OIL 2326.00 69.00 0
1985 OXFORD OIL 9496.00 305.00 365
1986 OXFORD OIL 2815.00 292.00 365
1987 OXFORD OIL 710.00 527.00 365
1988 OXFORD OIL 0.00 551.00 365
1989 OXFORD OIL 1307.00 338.00 365
1990 OXFORD OIL 2165.00 262.00 365
1991 OXFORD OIL 2858.00 388.00 365
1992 OXFORD OIL 1954.00 191.00 365
1993 OXFORD OIL 2394.00 0.00 365
1994 OXFORD OIL 2077.00 450.00 365
1995 OXFORD OIL 1322.00 502.00 365
1996 OXFORD OIL 0.00 473.00 366
1997 OXFORD OIL 0.00 286.00 365
1998 OXFORD OIL 0.00 219.00 365
1999 OXFORD OIL 2147.00 233.00 365
2000 OXFORD OIL 0.00 248.00 0
2001 OXFORD OIL 0.00 218.00 365
2002 OXFORD OIL 0.00 244.00 365
2003 OXFORD OIL 0.00 375.00 365
2004 OXFORD OIL 0.00 384.00 365
2005 OXFORD OIL 0.00 362.00 365
2006 OXFORD OIL 0.00 388.00 365
2007 OXFORD OIL 0.00 0.00 365
2008 OXFORD OIL 0.00 540.00 0
2009 OXFORD OIL 0.00 500.00 0
2010 OXFORD OIL 0.00 1013.00 365
2011 OXFORD OIL 0.00 270.00 0
2012 OXFORD OIL 0.00 517.00 0
2013 ECLIPSE RESOURCES-OHIO LLC 0.00 219.00 365
2014 ECLIPSE RESOURCES-OHIO LLC 0.00 295.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OXFORD OIL Brine 0 0
1985 OXFORD OIL Brine 330 365
1986 OXFORD OIL Brine 356 365
1987 OXFORD OIL Brine 434 365
1988 OXFORD OIL Brine 260 365
1989 OXFORD OIL Brine 120 365
1990 OXFORD OIL Brine 275 365
1991 OXFORD OIL Brine 200 365
1992 OXFORD OIL Brine 106 365
1993 OXFORD OIL Brine 100 365
1994 OXFORD OIL Brine 235 365
1995 OXFORD OIL Brine 125 365
1996 OXFORD OIL Brine 2353 366
1997 OXFORD OIL Brine 850 365
1998 OXFORD OIL Brine 540 365
1999 OXFORD OIL Brine 1917 365
2000 OXFORD OIL Brine 2594
2001 OXFORD OIL Brine 1192 365
2002 OXFORD OIL Brine 1817 365
2003 OXFORD OIL Brine 2963 365
2004 OXFORD OIL Brine 1343 365
2005 OXFORD OIL Brine 1695 365
2006 OXFORD OIL Brine 515 365
2007 OXFORD OIL Brine 1010 365
2008 OXFORD OIL Brine 998
2009 OXFORD OIL Brine 775
2010 OXFORD OIL Brine 0 365
2011 OXFORD OIL Brine 595
2012 OXFORD OIL Brine 825
2013 ECLIPSE RESOURCES-OHIO LLC Brine 340 365
2014 ECLIPSE RESOURCES-OHIO LLC Brine 775 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-108845484 2003-6-16 0:00: SW No Violations
-1161754604 2003-4-8 0:00:0 SW No Violations
-1199957687 2014-1-29 0:00: SW No Violations
-1222855483 2006-3-27 0:00: SW No Violations
-1269881429 2012-8-23 0:00: SW No Violations
-1274478557 2011-3-29 0:00: SW No Violations
-1311104233 2014-9-25 0:00: SW No Violations
-1319432556 2016-4-12 0:00: SW No Violations
-1325485706 2015-9-28 0:00: SW No Violations
-1342174490 2015-4-1 0:00:0 SW No Violations
-142224653 2014-7-9 0:00:0 SW No Violations
-1594230750 2013-5-20 0:00: SW No Violations
-1662291687 2012-1-30 0:00: SW No Violations 1.00
-1721506496 2009-9-4 0:00:0 SW No Violations
-1775092436 2011-9-23 0:00: SW No Violations 1.00
-1782671948 2016-6-9 0:00:0 FR No Violations
-1814164920 2011-7-6 0:00:0 SW No Violations 1.00
-1888463615 2012-10-18 0:00 SW No Violations
-1918202183 2013-2-13 0:00: SW No Violations
-1932979888 2009-9-2 0:00:0 SW No Violations
-2019655762 2012-5-14 0:00: SW No Violations
-2026899666 2014-12-4 0:00: SW No Violations
-2057915062 2014-3-7 0:00:0 SW No Violations
-256115675 2012-10-26 0:00 SW No Violations
-276972628 2003-10-2 0:00: SW No Violations
-280640592 2003-5-21 0:00: SW No Violations
-346469188 2014-11-10 0:00 SW No Violations
-382873628 2005-11-10 0:00 SW No Violations
-401186765 2013-10-28 0:00 SW No Violations
-414709229 2016-3-16 0:00: SW No Violations
-519931594 2008-3-10 0:00: SW No Violations
-531197317 2003-7-25 0:00: SW No Violations
-545272000 2014-11-21 0:00 SW No Violations
-577796001 2009-6-9 0:00:0 SW No Violations
-63577639 2012-3-22 0:00: SW No Violations 2.00
-641856128 2004-7-29 0:00: SW No Violations 11.00
-765483610 2011-10-14 0:00 SW No Violations 1.00
-833204541 2014-12-2 0:00: SW No Violations
-87188194 2015-6-16 0:00: SW No Violations
-985477987 2013-9-23 0:00: SW No Violations
0063577639 2012-03-22 Salt Water Injection Well No Violations On day of inspection Tank Pad was under construction. Oxford brought large crane in and removed 3-210 barrel tanks and replaced with a 500 barrel tank. That work was performed on 3-16-2012.Oxford and I performed a mini test on annulus.40 psi in tubing and 120 psi was held on annulus for 30 minutes.
0087188194 2015-06-16 Salt Water Injection Well No Violations Well not in operation today.
0108845484 2003-06-16 Salt Water Injection Well No Violations

-5/8 annulus. ID sign at wellhead will be replaced per Tony.

0142224653 2014-07-09 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation during my inspection.
0256115675 2012-10-26 Salt Water Injection Well No Violations On site to witness new Parmaco Tension packer and used 2.375 tubing run in hole and annulus flushed with fresh water and inhibitor,they ran 3933.45 of tubing plus 2.95 packer element equals 3936.40 is setting depth of packer and it is set in tension12K AND ANNULUS WAS FLUSHED WITH 54 BBL WATER AND 5 GAL OF INHIBITOR AND WE PRESSURED TESTED IT AT 1060 PSI WITH NO DECLINE IN PRESSURE.

Chiefs Order2012-29 has been resolved as of this date.

0256834619 2015-06-02 Salt Water Injection Well No Violations Injection pump was in operation during my inspection.
0276972628 2003-10-02 Salt Water Injection Well No Violations CHECKED SURFACE FACILITY. WELL JUST REWORKED AND PASSED MIT. DID NOT CHECK WELL.
0280168806 2009-09-04 Salt Water Injection Well No Violations Ran tbg and packer and displaced inhibited fresh water into annulus. Tested to 960 psig for 15 minutes w/ no drop in pressure. NOV satisfied. Dave Ball covered for this inspector who was on vacation.
0280640592 2003-05-21 Salt Water Injection Well No Violations
0346469188 2014-11-10 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation today and it was noted that one company owned vacuum truck was unloading at the facility during my inspection.
0382873628 2005-11-10 Salt Water Injection Well No Violations
0401186765 2013-10-28 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection.
0414709229 2016-03-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15th for 2015, despite a letter that was sent March 1, 2016 with a deadline of March 15, 2016 to submit the reports requested. REPORTS RECEIVED
0441192414 2010-03-18 Salt Water Injection Well No Violations Well was not in operation at time of inspection. Tubing 410 psig, annulus 5 psig. No problems noted at time of inspection.
0509466414 2012-10-19 Salt Water Injection Well No Violations On site to try and locate hole in 4.5 casing rig crew ran test packer in hole @500 intervals and set packer and pressure tested@750 psi at each respected interval it was determined that hole was in the area of 2556-3150 with is cement top on backside of casing,will further pinpoint casing problem on10/21/12.
0519931594 2008-03-10 Salt Water Injection Well No Violations Well was not in operation. No problems noted.
0531197317 2003-07-25 Salt Water Injection Well No Violations

-5/8x4-1/2 annulus... going to put rig on well to check it out.

0545272000 2014-11-21 Salt Water Injection Well No Violations Inspection revealed that Harmon Well Service was trying to release packer and remove it from well bore they plan on getting out of hole today and start new packer and used tubing back into well on 11/24/14.
0577796001 2009-06-09 Salt Water Injection Well No Violations Well was in operation. Sump okay, ID okay, Pad and Impoundment okay. No problems noted.
0601009704 2005-03-04 Salt Water Injection Well No Violations
0633735980 2015-01-08 Salt Water Injection Well No Violations Inspection reveled that injection pump was not in operation today and according to well tender they are not receiving much water this week due to in climate weather.
0637042921 2012-10-22 Salt Water Injection Well No Violations On site to witness operator try and locate hole in production casing and once located we set a composite bridge plug at 3200 and we perforated casing at old cement top@3150 and then we proceeded to pump 200 sacks Class A cement with 2%gel and estimated top of cement should be at 2000 +- Formation Cementing displaced wiper plug down to 2550 and we shut well in for the night they will resume operations tomorrow.
0641856128 2004-07-29 Salt Water Injection Well No Violations No problems noted
0691334013 2011-12-29 Salt Water Injection Well No Violations On day of inspection no violations noted.
0765483610 2011-10-14 Salt Water Injection Well No Violations No violations on day of inspection.
0767856257 2009-03-25 Salt Water Injection Well No Violations All is in order. No problems noted.
0833204541 2014-12-02 Salt Water Injection Well No Violations Harmon Well Service on site drilling out cement plug and once cement was drilled out they stopped and we pressure tested casing at 950 psi to ensure they have good integrity and tomorrow they will drill out bridge plug and clean out wellbore to bottom and come out of hole and then they will start a new packer and tubing in well.
0925119755 2015-07-21 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection and it was noted that one company owned vacuum truck dropped off one load of brine on this day.
0985477987 2013-09-23 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and facility appears to be in satisfactory condition this inspection.
1001955239 2016-05-11 Plug / Plug Back No Violations On site to witness setting of bottom hole plug and lime plug and Berea plug operator will rip 4.5 casing off in the morning and finish plugging operation.

Note: Formation cementing was cement contractor and they used a total of 77 sacks of Class A cement today along with gel spacers in between required plugs.

1032140345 2004-12-07 Salt Water Injection Well No Violations Okay
1065094683 2003-09-16 Salt Water Injection Well No Violations Ran Howco R-4 packer on seal lock tubing to 3928. Displaced 43 bbls of inhibited (with Treat-O-Lite R-
1074004974 2004-01-13 Salt Water Injection Well No Violations Looks good.
1080672006 2004-03-30 Salt Water Injection Well No Violations Injection pump had just shut down. No problems noted.
1097070434 2004-10-06 Salt Water Injection Well No Violations Looks good
1152204532 2006-07-06 Salt Water Injection Well No Violations
1161754604 2003-04-08 Salt Water Injection Well No Violations Not injecting at time of inspection. Oil around well head.
1161797525 2006-10-25 Surface Facility Construction No Violations
1168007066 2007-01-05 Salt Water Injection Well Violations Noted Looks like packer or tubing has failed. Tubing and casing equalized (differential between fresh water and salt water ~200psi) 275 tbg vs 480 csg
1169035625 2007-01-16 Work Over Reconditioning No Violations Ran R-4 packer on 2-3/8 used tubing. Packer to be set at 3902.9. Will displace inhibited fresh water, set packer and test on 1/17/2007.
1169147572 2007-01-17 Salt Water Injection Well No Violations Ran packer and tubing to 3903. Displaced 41 bbls of inhibited fresh water into annulus and tested annulus to 940 for 15 minutes. Test held.
1185383190 2007-07-25 Salt Water Injection Well No Violations Looks good. No problems noted
1197615195 2014-11-20 Salt Water Injection Well No Violations Inspection revealed that Harmon Well Service has moved there service rig on site to change out tubing and packer in well, on this day they released packer and started it out of hole and they plan on starting new packer back into well tomorrow if weather permits.
1199957687 2014-01-29 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection and it appears that well is not being used much at this time due to extreme cold weather conditions.
1210i20544 2001-11-14 Salt Water Injection Well No Violations Accompanied by Tom Tomastik, and Dave Hodges. Well and facility in good shape. Need well head ID remarked , 1501:9-3-06 (H). Informed Toni of this and left a copy of report with him.
1210i2054497 2001-11-14 0:00 SW No Violations
1216827512 2008-06-30 Salt Water Injection Well No Violations Well was not in operation. Need new ID on well. (told Tony). No other problems noted.
1221670754 2008-09-17 Salt Water Injection Well No Violations Need new ID on well. Told Tony again. He will comply this time. No other problems noted.
1222855483 2006-03-27 Salt Water Injection Well No Violations Okay, not in operation. All looks good.
1228846172 2008-12-09 Salt Water Injection Well No Violations Not injecting when checked. ID replaced as requested last time. No problems noted. Tubing 135 psig. Annulus 10psig.
1254372560 2013-07-05 Salt Water Injection Well No Violations Inspection revealed that injection pump was not operating during my inspection.

Note: Unloading pad is in need of a good cleaning.

1260896518 2009-12-15 Salt Water Injection Well No Violations Well in operation at the time of the inspection. Tanks and unloading pad in good repair. ID in place, no problems noted. Well ID in place. Tubing 540 psig. Annulus 825 psig.
1269881429 2012-08-23 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation during my inspection and it was noted that annulus pressure has fallen to zero and I talked to company rep requesting that they perform mini MIT test on annulus and he stated that they would set one up for next week.
1274478557 2011-03-29 Salt Water Injection Well No Violations Ran Parmaco tension packer and 132 jts of 2-3/8 EUE tubing to 3916.4 Pumped inhibited fresh water down tubing and up the annulus to surface. Set packer in tension with 10,000#. Pressure tested the annulus to 1100psig with 40 psi drop (due to leaking stem on 1/4 valve) for 15 minutes. Test passed. Well will be put back in operation as soon as it can be plumbed in.
1277818524 2010-06-17 Salt Water Injection Well No Violations Well in operation at time of inspection. Both tank battery and well in good repair, no problems noted. Annulus 10 psig, tubing 560 psig.
1284637495 2010-09-15 Salt Water Injection Well No Violations Well was in operation when inspected. Packing was leaking on pump and drip pan was full. No other problems noted.
1300970756 2011-03-24 Salt Water Injection Well Violations Noted Tubing 720 psig. Annulus 660 psig. Well was operating when inspected but was then shut down. Contacted Tony Blizzard. No other problems noted. A rig will move on the well on 3/28/2011.
1311104233 2014-09-25 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and it was noted that one company owned vacuum truck was unloading at the facility during my inspection.
1313665755 2011-08-17 Salt Water Injection Well No Violations Checked well pressures and the facility. No violations noted.
1319432556 2016-04-12 Salt Water Injection Well No Violations Inspection today revealed that well is still incapable of injection due to fact that it equalized and according to owner they are evaluating well cost to repair said well.
1325485706 2015-09-28 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and it was noted that one company owned vacuum truck was unloading at the facility on this day of my inspections.
1342174490 2015-04-01 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and I stopped at the company office and talked to Tony Blizzard and told him to have positive pressure applied to annulus of tubing in the near future.
1349993175 2012-10-11 Salt Water Injection Well No Violations Upon performing mini test on well it was determined that 4.5 casing has lost integrity we pressure tested annulus @500 psi and they loss pressure within 10 seconds ,told well owner to shut well down until repairs can be made to casing and too submit repair plan to UIC Dept in Central Office.
1351250633 2012-10-23 Salt Water Injection Well No Violations Tagged cement plug @2540 operator will drill cement from inside of casing and then we will perform integrity test on casing before drilling out bridge plug.
1353871187 2007-09-20 Salt Water Injection Well No Violations No problems noted.
1357159464 2013-01-02 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation today due to extreme cold weather.
1363898474 2013-03-20 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection and according to well tender there has not been much activity at site recently due to weather conditions.
1366290572 2013-04-16 Salt Water Injection Well No Violations Onsite to witness pressure testing of annulus of tubing after valve froze and busted during recent cold spell, replaced valve and applied 470 pounds of pressure to annulus of tubing and we monitored pressure for 15 minutes with no decline in pressure.
1367536032 2013-05-02 Salt Water Injection Well No Violations Inspection revealed that injection pump was just being started when I arrived on site for my inspection and I stopped and talked to Jack Greene about getting seed&mulch on area of old working pit to help bind the soils and to prevent any erosion issues that may arise.
1368055102 2010-12-07 Salt Water Injection Well No Violations Well was in operation. Tubing injection pressure 690 psig. Annulus 0 psig. No problems noted at time of inspection.
1374417115 2013-07-19 Salt Water Injection Well No Violations Injection pump not in operation today, unloading pad recently cleaned and facility appears to be in satisfactory condition this inspection.
1376947639 2013-08-19 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection and in conversation with well tender requesting that they replace there gauge on tubing it appears to be faulty.
1386113841 2013-12-03 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation during my inspection and we discussed what was needed to place brine storage facility within there yard, contacted central office and had them send info to there office pertaining to approved brine storage sites.
1409784399 2013-04-09 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection.

Note: Pressure needs to be applied to annulus of tubing to ensure that we have casing integrity.

1416956801 2014-11-24 Salt Water Injection Well No Violations On site to witness Harmon Well Service run new R-4 Halliburton packer and used 2.375 tubing in well and they set packer at 3934 and we tried to pressure test the integrity of casing and test failed and they unset packer and moved it up the hole too 3924 and tried to pressure test it again and test failed again we then put pressure gauge on 8 and we noticed a pressure increase when they applied pressure which indicated that 4.5 has a hole in it and then we shut down for the night and we intend to perform further testing tomorrow to try and pinpoint hole in casing.
1417088723 2014-11-26 Salt Water Injection Well No Violations On site to witness Timco Wireline Services set drillable bridge plug and Formation Cementing pump 395 sacks of cement for squeeze job to repair hole in casing, cement did not circulate to surface as calculated and company is going to run bond log on 12/1/14 to confirm cement top.
1417468959 2014-12-01 Salt Water Injection Well No Violations Inspection revealed that Timco Wireline bond logged well and cement top was noted at 650 on annulus of casing and owner is planning on drilling cement out from inside of casing and then pressure test casing and if it OK they will drill out bridge plug and go to bottom.
1423684814 2015-02-11 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and both storage tank and well head were properly identified.
1441138413 2015-08-31 Salt Water Injection Well No Violations Inspection on this day indicated that injection pump was not in operation on the day of my inspection and it was noted that one company owned vacuum truck was unloading at the facility on the day of my inspection.
1448541759 2015-11-23 Salt Water Injection Well No Violations Inspection revealed that well is equalized and I contacted company rep to inform him of problem he stated they would get service rig on the well site as soon as possible to replace tubing and packer and they will submit plan to the division on there plan to repair well.
1452884476 2016-01-15 Salt Water Injection Well No Violations Inspection on this day indicated that well is still down waiting on service rig to repair problem with tubing/packer assembly.
1456343431 2016-02-23 Salt Water Injection Well No Violations Inspection revealed that well is still down waiting on owner to secure service rig contract to repair said well.
1457980661 2016-03-11 Salt Water Injection Well No Violations Inspection today revealed that well is still incapable of injection due to tubing/packer failure owner claims they are going to repair well when the economics are right for there operation.
1463000062 2016-05-10 Salt Water Injection Well No Violations On site to witness releasing of packer and pulling it from well in preparation for plugging operation.
1463076669 2016-05-12 Plug / Plug Back No Violations I am onsite to witness the plugging operations. Wrights Well Service attempted to rip the casing at 704, 450, and 238. After ripping each time an attempt to pull the casing and circulate was made. The casing moved a few inches, while pulling 60,000 pounds, after ripping at 238. Circulation could not be established. The determination to back off casing was made after attempts to pull the casing were unsuccessful. The casing was backed off at 98 and recovered from the same point. 125 of 2.375 tubing were placed in the well and a 65 sack class A plug was circulated to surface.
1546848860 2011-03-28 Salt Water Injection Well No Violations Parted tubing trying to get packer loose. Ran in hole with overshot and sat down on fish. POOH with tubing to overshot. Shut down for night.
1553469494 2005-06-23 Salt Water Injection Well No Violations Okay .
1559380656 2001-11-14 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 1210i20 Accompanied by Tom Tomastik, and Dave Hodges. Well and facility in good shape. Need well head ID remarked , 1501:9-3-06 (H). Informed Toni of this and left a copy of report with him.
1582801666 2015-03-06 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation today and it was noted that one company owned truck was setting on unloading pad today.
1594230750 2013-05-20 Salt Water Injection Well No Violations Well not in operation today and containment was in good repair and it was noted that in area of old working pit had been graded and I stopped at office and told them to apply seed and mulch to exposed area and company rep stated that they would perform task later today.
1636435764 2012-10-25 Salt Water Injection Well No Violations Well cleaned out to 4020 then they went on to bottom and circulated well and once hole cleaned up we pressured testing casing to 1000 psi to ensure we had regained integrity with casing and once test passed we removed tubing from well and then Timco Wireline Services bond logged well to determine new cement top on backside of casing it was located @2305 shut down for the night will run new packer and used tubing back into well tomorrow.
1662291687 2012-01-30 Salt Water Injection Well No Violations On day of inspection the well was not pumping and there were no violations.Met with Oxford on replacing tanks and reworking dike.
1721506496 2009-09-04 Salt Water Injection Well No Violations On site to witness operator run Packer and tubing back into well and pressure casing.

Operator ran 3897 of used 2.375 tubing and a rebuilt Parmaco packer in well bore setting depth of packer is 3901.30,Producers Services flushed annulus of tubing with 60 bbl of fresh water with anhib and pressured tested at 960 psi with no decline in pressure(TEST PASSED) owner will place well back into operation 9/9/09.

1775092436 2011-09-23 Salt Water Injection Well No Violations On day of inspection well was in production and no violations were noted. Oxford will change a tank out soon.
1782671948 2016-06-09 Final Restoration No Violations Inspection revealed that well has been properly plugged and owner has the pit filled in and site restored and vegetation has been established.
1814164920 2011-07-06 Salt Water Injection Well No Violations Checked facility and pressures at well head. No violations noted.
1831450649 2012-11-26 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection.

Note: Stopped and talked to company rep regarding closing of open pit that was used when owner pulled packer and replaced tubing on said well he stated that he would get started on it later today.

1863706635 2011-11-18 Salt Water Injection Well No Violations No violations on day of inspection. May need to replace tank in the near future. Well was not pumping at time of inspection.
1888463615 2012-10-18 Salt Water Injection Well No Violations Inspection revealed that Chipco Well Services was on site to release packer and pull tubing and then go in hole with test packer to try and locate hole in 4.5 production casing.

Note: Packer was released and tubing started out of hole on this date.

1908882015 2012-02-23 Salt Water Injection Well No Violations On day of inspection well was not being pumped into. I met with John Straker of Oxford and talked about the tank needing replaced. They will place a 500bbl tank in the dike and repair the dike. We plan to do a mini test on the annulus as soon as the solvent truck is repaired.
1918202183 2013-02-13 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation today and facility is in satisfactory condition this inspection.
1932979888 2009-09-02 Salt Water Injection Well No Violations Found that well had equalized across tubing and annulus. Spoke with John Staker who said they would repair the well ASAP. Replace faulty tubing or packer, put new inhibitor in annulus and test to at least maximum injsction pressure for 15 minutes.
1955861573 2004-12-29 Salt Water Injection Well No Violations NO problems noted. Injection pump has been removed
1976194475 2015-06-30 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection.
2019655762 2012-05-14 Salt Water Injection Well No Violations Inspection revealed that injection pump was in operation during my inspection.

Note: Housekeeping needed in unloading pad area.

2026899666 2014-12-04 Salt Water Injection Well No Violations On site to witness tubing and packer run in well and fresh water and inhibitor pumped too check annulus of tubing for integrity.

Note: Packer set at 3934 and good used 2.375 tubing and we pressure tested annulus at 1020 psi for 15 min. with no decline in pressure and owner is going to replumb the top of tubing and place new 1/4 valves on tubing head.

2057915062 2014-03-07 Salt Water Injection Well No Violations Inspection revealed that injection pump was not in operation during my inspection.

Note: It appears that company is planning on constructing brine storage facility near this injection well facility.

2065543546 2007-12-26 Salt Water Injection Well No Violations No problems noted. Well in operation
256834619 2015-6-2 0:00:0 SW No Violations
280168806 2009-9-4 0:00:0 SW No Violations
441192414 2010-3-18 0:00: SW No Violations
509466414 2012-10-19 0:00 SW No Violations 8.00
601009704 2005-3-4 0:00:0 SW No Violations
633735980 2015-1-8 0:00:0 SW No Violations
637042921 2012-10-22 0:00 SW No Violations
691334013 2011-12-29 0:00 SW No Violations 1.00
767856257 2009-3-25 0:00: SW No Violations
925119755 2015-7-21 0:00: SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0414709229 US-OH-124412 2016-04-04 Failure to file salt water injection annual report
1168007066 US-OH-104449 2007-01-05 Mechanical failure/contamination
1300970756 US-OH-108493 2011-03-29 Mechanical failure/contamination
1559380656 US-OH-115228 2002-07-11 Well shall be plugged

For data sources see[9]

References