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34-119-22839

Well Details

Well ID: 34-119-22839
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Country: United States
State: Ohio
County: Muskingum
Municipality: Salem Township
Operator Name: ECHLEBERRY CHARLES
Well Pad ID:
Farm/Lease Name: KNIPE BRUCE
License Status: Domestic Well
License Date: 1972-07-12
Spud Date: 1972-07-12
Spud Drilling Contractor:
Final Drill Date: 1972-08-10
Well Total Depth: 4122.00 ft
Configuration: Vertical
Latitude: 40.030000
Longitude: -81.860000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1972-07-12 2774 T J'S OIL & GAS INC GeoDate 7/12/72
Original Spud 1972-07-12 NSR. A.F. 3,249 MCFG: 10/05/1972. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KENOIL, INC. #627 TO OWNER ON 12/14/2016 CM.
Completed 1972-08-10 NSR. A.F. 3,249 MCFG: 10/05/1972. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KENOIL, INC. #627 TO OWNER ON 12/14/2016 CM.
Reached Total Depth 1972-08-10 NSR. A.F. 3,249 MCFG: 10/05/1972. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KENOIL, INC. #627 TO OWNER ON 12/14/2016 CM.
Change of Owner 2016-12-14 Operator changed from 627, KENOIL to 9831, ECHLEBERRY CHARLES
Record Last Modified 2019-06-04 NSR. A.F. 3,249 MCFG: 10/05/1972. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM KENOIL, INC. #627 TO OWNER ON 12/14/2016 CM.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 H I SMITH OIL & GAS INC 1803.00 0.00 0
1985 H I SMITH OIL & GAS INC 760.00 66.00 0
1986 H I SMITH OIL & GAS INC 1058.00 35.00 365
1993 T JS OIL & GAS INC 14.00 0.00 30
1996 T JS OIL & GAS INC 0.00 0.00 0
2001 KENOIL LLC 0.00 0.00 365
2002 KENOIL LLC 0.00 0.00 365
2003 KENOIL LLC 110.00 0.00 365
2004 KENOIL LLC 398.00 129.00 365
2005 KENOIL LLC 356.00 35.00 365
2006 KENOIL LLC 571.00 0.00 365
2007 KENOIL LLC 429.00 0.00 365
2008 KENOIL LLC 1037.00 42.00 365
2009 KENOIL LLC 691.00 0.00 365
2010 KENOIL LLC 907.00 32.00 365
2011 KENOIL LLC 986.00 0.00 0
2012 R C POLING CO INC 894.00 29.00 81
2013 KENOIL LLC 962.00 0.00 365
2014 KENOIL LLC 736.00 0.00 365
2015 R C POLING CO INC 1003.00 22.00 365
2016 KENOIL LLC 514.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 H I SMITH OIL & GAS INC Brine 0 0
1985 H I SMITH OIL & GAS INC Brine 0 0
1986 H I SMITH OIL & GAS INC Brine 0 365
1993 T JS OIL & GAS INC Brine 0 30
1996 T JS OIL & GAS INC Brine 0 0
2001 KENOIL LLC Brine 0 365
2002 KENOIL LLC Brine 0 365
2003 KENOIL LLC Brine 25 365
2004 KENOIL LLC Brine 0 365
2005 KENOIL LLC Brine 30 365
2006 KENOIL LLC Brine 0 365
2007 KENOIL LLC Brine 0 365
2008 KENOIL LLC Brine 53 365
2009 KENOIL LLC Brine 37 365
2010 KENOIL LLC Brine 0 365
2011 KENOIL LLC Brine 31
2012 R C POLING CO INC Brine 0 81
2013 R C POLING CO INC Brine 0 81
2014 R C POLING CO INC Brine 0 365
2015 R C POLING CO INC Brine 0 365
2016 R C POLING CO INC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1641628953 2008-3-5 0:00:0 PW No Violations
-1733341663 2016-10-25 0:00 AM No Violations
-96312882 2016-10-25 0:00 EX No Violations 2.00
0096312882 2016-10-25 Exempt Well Pre Transfer No Violations The purpose of the inspection is due to a pre-
0332095619 2005-03-01 Production Wells No Violations Okay
1027701877 2016-10-13 Exempt Well Pre Transfer No Violations The purpose is for a Pre--100 barrel steel tank battery.
1167845772 2007-01-03 Production Wells No Violations Producing
1384545837 2007-11-02 Production Wells No Violations Pump Jack put on well. New separator. Well is producing. No problems noted.
1641628953 2008-03-05 Production Wells No Violations Producing, no problems noted.
1733341663 2016-10-25 Administrative Inspection No Violations The purpose of the inspection is due to the call I made to Reggie on making the well safe for Exempt transfer. Reggie Huber called and stated that the pumping unit is unhooked from the well and the pony rod. I stated that I would be out to make an inspection later in the day.
1783664915 2010-01-07 Production Wells No Violations Producing, no problems noted. House gas off casing.
1796663661 2003-12-12 Production Wells No Violations x-tee on tbg leaking slightly
332095619 2005-3-1 0:00:0 PW No Violations

For data sources see[7]

References