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34-117-22823

Well Details

Well ID: 34-117-22823
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Country: United States
State: Ohio
County: Morrow
Municipality: Cardington Township
Operator Name: FISHBURN PRODUCING INC
Well Pad ID:
Farm/Lease Name: LEE ARTHUR G
License Status: Plugged and Abandoned
License Date: 2019-02-07
Spud Date: 1966-04-05
Spud Drilling Contractor:
Final Drill Date: 1966-04-10
Well Total Depth: 3100.00 ft
Configuration: Vertical
Latitude: 40.540000
Longitude: -82.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 176 ASHLAND EXPLORATION INC
Original Spud 1966-04-05 LOG TYPE=IES, GL=1009.97 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Completed 1966-04-10 LOG TYPE=IES, GL=1009.97 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Reached Total Depth 1966-04-10 LOG TYPE=IES, GL=1009.97 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
CO 1991-08-21 3941 FISHBURN PRODUCING INC GeoDate
APP 2019-02-07 Proposed Formations:TREMPEALEAU, Issued Date:2/7/2019, Expired Date:2/6/2021 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-04-01 LOG TYPE=IES, GL=1009.97 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Construction Permit Expires 2021-02-06 LOG TYPE=IES, GL=1009.97 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2946 2976 0
2946 2976 0
2946 2976 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 5000 Gal 0 NSR

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC 0.00 2661.00 365
1985 ASHLAND EXPLORATION INC 0.00 1172.00 0
1986 ASHLAND EXPLORATION INC 0.00 1597.00 365
1991 FISHBURN PRODUCING INC 0.00 1781.00 150
1992 FISHBURN PRODUCING INC 0.00 1261.00 360
1993 FISHBURN PRODUCING INC 0.00 361.00 120
1994 FISHBURN PRODUCING INC 0.00 1291.00 190
1995 FISHBURN PRODUCING INC 0.00 1619.00 330
1996 FISHBURN PRODUCING INC 0.00 1219.00 200
1997 FISHBURN PRODUCING INC 0.00 1591.00 346
1998 FISHBURN PRODUCING INC 0.00 1226.00 267
1999 FISHBURN PRODUCING INC 0.00 0.00 0
2000 FISHBURN PRODUCING INC 0.00 0.00 0
2001 FISHBURN PRODUCING INC 0.00 0.00 0
2002 FISHBURN PRODUCING INC 0.00 0.00 0
2003 FISHBURN PRODUCING INC 0.00 1019.00 232
2004 FISHBURN PRODUCING INC 0.00 1223.00 353
2005 FISHBURN PRODUCING INC 0.00 1068.00 253
2006 FISHBURN PRODUCING INC 0.00 905.00 211
2007 FISHBURN PRODUCING INC 0.00 886.00 241
2008 FISHBURN PRODUCING INC 0.00 1266.00 183
2009 FISHBURN PRODUCING INC 0.00 1059.00 250
2010 FISHBURN PRODUCING INC 0.00 890.00 259
2011 FISHBURN PRODUCING INC 0.00 1081.00 222
2012 FISHBURN PRODUCING INC 0.00 900.00 236
2013 FISHBURN PRODUCING INC 0.00 538.00 199
2014 FISHBURN PRODUCING INC 0.00 322.00 92
2015 FISHBURN PRODUCING INC 0.00 864.00 277
2016 FISHBURN PRODUCING INC 0.00 0.00 19
2017 FISHBURN PRODUCING INC 0.00 71.00 0
2018 FISHBURN PRODUCING INC 0.00 79.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC Brine 0 365
1985 ASHLAND EXPLORATION INC Brine 29389 0
1986 ASHLAND EXPLORATION INC Brine 11928 365
1991 FISHBURN PRODUCING INC Brine 1695 150
1992 FISHBURN PRODUCING INC Brine 2740 360
1993 FISHBURN PRODUCING INC Brine 1000 120
1994 FISHBURN PRODUCING INC Brine 2975 190
1995 FISHBURN PRODUCING INC Brine 2920 330
1996 FISHBURN PRODUCING INC Brine 2260 200
1997 FISHBURN PRODUCING INC Brine 2630 346
1998 FISHBURN PRODUCING INC Brine 1970 267
1999 FISHBURN PRODUCING INC Brine 0 0
2000 FISHBURN PRODUCING INC Brine 0 0
2001 FISHBURN PRODUCING INC Brine 0 0
2002 FISHBURN PRODUCING INC Brine 0 0
2003 FISHBURN PRODUCING INC Brine 17025 232
2004 FISHBURN PRODUCING INC Brine 10215 353
2005 FISHBURN PRODUCING INC Brine 7505 253
2006 FISHBURN PRODUCING INC Brine 3620 211
2007 FISHBURN PRODUCING INC Brine 3590 241
2008 FISHBURN PRODUCING INC Brine 4160 183
2009 FISHBURN PRODUCING INC Brine 3470 250
2010 FISHBURN PRODUCING INC Brine 4285 259
2011 FISHBURN PRODUCING INC Brine 3735 222
2012 FISHBURN PRODUCING INC Brine 3435 236
2013 FISHBURN PRODUCING INC Brine 2130 199
2014 FISHBURN PRODUCING INC Brine 1620 92
2015 FISHBURN PRODUCING INC Brine 2180 277
2016 FISHBURN PRODUCING INC Brine 160 19
2017 FISHBURN PRODUCING INC Brine 0 0
2018 FISHBURN PRODUCING INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1563303738 2015-12-2 0:00: WR No Violations
-1718991800 2015-10-19 0:00 PW No Violations
-1809293701 2018-1-5 0:00:0 PW No Violations
-282108975 2019-10-2 0:00: PB No Violations
-426220275 2012-9-6 0:00:0 PW No Violations
-529815314 2019-10-1 0:00: PB No Violations
-687656097 2019-9-23 0:00: PB No Violations
-901454893 2003-4-23 0:00: PW No Violations
0000PL9126 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0121724852 2006-01-05 Production Wells No Violations Chk well and storage, Ok.
0179308525 2015-01-30 Production Wells No Violations Inspected the Lee #3 (#2823) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
0368903061 2007-02-20 Production Wells No Violations Inspect well. Pump jack is not running. Oil staining at well head. Wood shavings at wellhead to control oil spill. ID illegible.
0426220275 2012-09-06 Production Wells No Violations Fishburn Producing is currently repairing the separator on the Lee #3 as a bucket truck is on location. No one is working at this time and some oil has drained from the separator piping and is contained within the dike. Clean-up appears is in progress as straw is on location.
0575689386 2015-01-30 Production Wells No Violations Location Information for the Lee #3 (#2823). WELL HEAD: Lat. 40.54375 Long. -82.90314 / CENTER-OF-STORAGE: Lat. 40.54587 Long. -82.90031 / ENTRANCE: Lat. 40.54285 Long. -82.90388.
0580464002 2009-08-28 Production Wells No Violations Chk well and storage, Ok.
0785070796 2013-04-04 Production Wells No Violations Fishburn Production has placed the well back into production after steaming the tubing. Paraffin residual on the ground waiting on clean-up. Made phone call to Fishburn, will continue to monitor.
0901454893 2003-04-23 Production Wells No Violations Chk well and storage, pumping unit running at this time. Shows signs of recent service, has stains on the ground around the well head and has a small pit that shoulk be closed.
1004929600 2019-2-14 0:00: PB No Violations
1055989725 2012-05-29 Production Wells Violations Noted Inspected the Lee #3 (#2823) as part of a standard status check. There is no well identification at the well or tanks.
1128418492 2012-09-06 Production Wells No Violations Inspected the Lee #3 (#2823) as a compliance notice follow-up. The well identification is now clearly marked at the well and storage Status OK.
121724852 2006-1-5 0:00:0 PW No Violations
1242786261 2019-01-07 Plug / Plug Back No Violations Check well after alternate plugging plan meeting with the operator the previous day. Status: 2.875 inch tubing set with a casing hanger on the 8 inch surface casing-covered with a plastic bucket. Alternate plugging plan approved-relayed information to the owner/operator.
1295285143 2017-08-22 Production Wells No Violations Inspected the Lee #3 (#2823) as part of a standard production well status check. Inspect well, storage and identification. Status: the well is currently out-of-service after recent work over. Rods and tubing removed and stacked on racks, lined work over pit open. Added directions.
1355416120 2012-12-13 Work Over Reconditioning No Violations The Lee #3 is currently being worked over as the tubing and rods have been pulled. The well identification, emergency contact information and No Trespassing signs are posted at the well and the storage.
1464996379 2019-9-26 0:00: PB No Violations
1486993297 2017-02-09 Work Over Reconditioning No Violations Berry Well Service Rig #6 is on the well attempting to fish tubing from the well.
1563303738 2015-12-02 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
1569606181 2019-9-27 0:00: PB No Violations
1571684393 2019-9-30 0:00: PB No Violations
1718991800 2015-10-19 Production Wells No Violations Inspected the Lee #3 (#2823) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
179308525 2015-1-30 0:00: PW No Violations
1809293701 2018-01-05 Production Wells No Violations Inspect well, storage and identification. Status: no change in status from previous inspection, out-of-service, no leaks or odor noted.
1824802241 2019-9-30 0:00: PB No Violations
1867294435 2019-10-4 0:00: PB No Violations
2067960485 2013-02-11 Work Over Reconditioning No Violations The Lee #3 (#2823) is currently in a state of being worked-over. Fishburn producing has pulled the rods and tubing and they are stacked near the well.
219901698 2019-9-24 0:00: PB No Violations
368903061 2007-2-20 0:00: PW No Violations
427412071 2019-10-3 0:00: PB No Violations
575689386 2015-1-30 0:00: PW No Violations
580464002 2009-8-28 0:00: PW No Violations
785070796 2013-4-4 0:00:0 PW No Violations
PL9126 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1055989725 US-OH-101030 2012-05-29 Failure to legibly identify well

For data sources see[9]

References