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34-117-22058

Well Details

Well ID: 34-117-22058
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Country: United States
State: Ohio
County: Morrow
Municipality: Canaan Township
Operator Name: FISHBURN PRODUCING INC
Well Pad ID:
Farm/Lease Name: GILLSON R & J
License Status: Producing
License Date: 1964-09-11
Spud Date: 1964-09-17
Spud Drilling Contractor:
Final Drill Date: 1964-09-24
Well Total Depth: 3056.00 ft
Configuration: Vertical
Latitude: 40.580000
Longitude: -82.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 176 ASHLAND EXPLORATION INC
Original Spud 1964-09-17
Completed 1964-09-24
Reached Total Depth 1964-09-24
CO 1991-08-21 3941 FISHBURN PRODUCING INC GeoDate
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-02-15 1970 1972 7
2006-09-11 2916 2950 0
2916 2950 0
1970 1972 7
1970 1972 7

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 5000 Gal 0 & 300# MOTH BALLS

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC 0.00 1756.00 365
1985 ASHLAND EXPLORATION INC 0.00 1654.00 0
1986 ASHLAND EXPLORATION INC 0.00 1522.00 365
1991 FISHBURN PRODUCING INC 0.00 1335.00 132
1992 FISHBURN PRODUCING INC 0.00 1431.00 345
1993 FISHBURN PRODUCING INC 0.00 1047.00 350
1994 FISHBURN PRODUCING INC 0.00 889.00 300
1995 FISHBURN PRODUCING INC 0.00 895.00 260
1996 FISHBURN PRODUCING INC 0.00 1340.00 330
1997 FISHBURN PRODUCING INC 0.00 1172.00 320
1998 FISHBURN PRODUCING INC 0.00 1028.00 260
1999 FISHBURN PRODUCING INC 0.00 0.00 0
2000 FISHBURN PRODUCING INC 0.00 0.00 5
2001 FISHBURN PRODUCING INC 0.00 1148.00 210
2002 FISHBURN PRODUCING INC 0.00 1075.00 220
2003 FISHBURN PRODUCING INC 0.00 940.00 200
2004 FISHBURN PRODUCING INC 0.00 1134.00 220
2005 FISHBURN PRODUCING INC 0.00 1049.00 200
2006 FISHBURN PRODUCING INC 0.00 1035.00 270
2007 FISHBURN PRODUCING INC 0.00 662.00 235
2008 FISHBURN PRODUCING INC 0.00 173.00 110
2009 FISHBURN PRODUCING INC 0.00 520.00 270
2010 FISHBURN PRODUCING INC 0.00 863.00 320
2011 FISHBURN PRODUCING INC 0.00 0.00 18
2012 FISHBURN PRODUCING INC 0.00 0.00 110
2013 FISHBURN PRODUCING INC 0.00 45.00 260
2014 FISHBURN PRODUCING INC 0.00 335.00 310
2015 FISHBURN PRODUCING INC 0.00 512.00 265
2016 FISHBURN PRODUCING INC 0.00 357.00 235
2017 FISHBURN PRODUCING INC 0.00 350.00 265
2018 FISHBURN PRODUCING INC 0.00 352.00 139

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC Brine 0 365
1985 ASHLAND EXPLORATION INC Brine 3202 0
1986 ASHLAND EXPLORATION INC Brine 4176 365
1991 FISHBURN PRODUCING INC Brine 1945 132
1992 FISHBURN PRODUCING INC Brine 6130 345
1993 FISHBURN PRODUCING INC Brine 4635 350
1994 FISHBURN PRODUCING INC Brine 3915 300
1995 FISHBURN PRODUCING INC Brine 4275 260
1996 FISHBURN PRODUCING INC Brine 5665 330
1997 FISHBURN PRODUCING INC Brine 4970 320
1998 FISHBURN PRODUCING INC Brine 5305 260
1999 FISHBURN PRODUCING INC Brine 0 0
2000 FISHBURN PRODUCING INC Brine 90 5
2001 FISHBURN PRODUCING INC Brine 9190 210
2002 FISHBURN PRODUCING INC Brine 8710 220
2003 FISHBURN PRODUCING INC Brine 9050 200
2004 FISHBURN PRODUCING INC Brine 11805 220
2005 FISHBURN PRODUCING INC Brine 9245 200
2006 FISHBURN PRODUCING INC Brine 6105 270
2007 FISHBURN PRODUCING INC Brine 4140 235
2008 FISHBURN PRODUCING INC Brine 4095 110
2009 FISHBURN PRODUCING INC Brine 5065 270
2010 FISHBURN PRODUCING INC Brine 7975 320
2011 FISHBURN PRODUCING INC Brine 300 18
2012 FISHBURN PRODUCING INC Brine 8370 110
2013 FISHBURN PRODUCING INC Brine 11070 260
2014 FISHBURN PRODUCING INC Brine 14415 310
2015 FISHBURN PRODUCING INC Brine 15010 265
2016 FISHBURN PRODUCING INC Brine 10155 235
2017 FISHBURN PRODUCING INC Brine 10385 265
2018 FISHBURN PRODUCING INC Brine 4755 139

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1010088977 2019-6-17 0:00: PW No Violations
-1212295915 2020-5-19 0:00: BH No Violations
-1299351095 2019-6-26 0:00: WR No Violations
-1311501917 2019-10-8 0:00: PW No Violations
-1403296645 2016-4-27 0:00: PW No Violations
-1486199363 2018-6-4 0:00:0 PW No Violations
-1648549023 2018-12-6 0:00: PW No Violations
-1871245849 2018-9-13 0:00: PW No Violations
-1900031581 2013-10-2 0:00: WR No Violations
-2142877212 2020-5-19 0:00: PW No Violations
-22737302 2014-10-23 0:00 WR No Violations
-425168584 2018-1-16 0:00: PW No Violations
-700774384 2017-7-27 0:00: PW No Violations
-750286635 2016-10-12 0:00 WR No Violations
-81998105 2015-6-18 0:00: WR No Violations
-863415226 2017-9-20 0:00: PW No Violations
-955464639 2014-9-4 0:00:0 WR No Violations
-972446567 2017-6-12 0:00: PW No Violations
0000PL9164 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0022737302 2014-10-23 Work Over Reconditioning No Violations Fishburn service rig is on location for work over. Status: ok.
0081998105 2015-06-18 Work Over Reconditioning No Violations Fishburn service rig is on location for workover.
0208346919 2017-12-01 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection. Tubing from recent work over stacked next to the well.
0226087017 2018-04-02 Production Wells No Violations The operator has repaired the flowline and placed the well back into production.
0424135638 2017-05-31 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
0425168584 2018-01-16 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok
0431433582 2015-02-26 Production Wells No Violations Inspected the Gilson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
0700774384 2017-07-27 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage, separator and identification. Status: the well was shut-in the previous week as the horizontal tank developed a leak at the nipple valve. Inspection revealed the tank leaking at the nipple valve with brine pooled in the storage dike in a low spot by the separator. Contacted the operator who responded and temporarily patched the hole. Fishburn Services brine truck #112 responded and emptied the tank and vacuumed residual product from the dike and spread absorbent material. The tank is slated for replacement as well as secondary containment reconstruction.
0750286635 2016-10-12 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
0863415226 2017-09-20 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok, the operator has replaced the laydown tank with a recondition one and partially constructed a earthen dike around the storage.
0955464639 2014-09-04 Work Over Reconditioning No Violations Fishburn service rig is on location for work over.
0972446567 2017-06-12 Production Wells No Violations Inspect well after recent work over. Status: ok, the operator has placed the well back into production.
0973297691 2018-03-26 Production Wells No Violations Fishburn hot oil truck is flushing the flowline with hot water (fresh) to unclog a paraffin build-up. Met with the operator and discussed production operations.
1209975383 2015-02-26 Production Wells No Violations Location Information for the Gilson #1 (#2058). WELL HEAD: Lat. 40.58885 Long. -82.93057 / CENTER-OF-STORAGE: Lat. 40.58796 Long. -82.92837 / ENTRANCE: Lat. 40.58699 Long. -82.92825.
1246263429 2003-03-19 Production Wells No Violations Chk well and storage, Ok.
1354728451 2012-12-05 Work Over Reconditioning No Violations Fishburn has finished work over and placed the well back into production. The well pad is free of excess contamination and the well identification and emergency contact information is displayed at the pump jack. Status: OK.
1403296645 2016-04-27 Production Wells No Violations Inspect well and storage. Status: ok.
1414164416 2014-10-24 Production Wells No Violations Fishburn has placed the well back into production. Status: ok.
1418830389 2014-12-15 Work Over Reconditioning No Violations Fishburn Services is on location for work over.
1429753754 2014-09-04 Work Over Reconditioning No Violations With Inspector Eric Daugstrup. Fishburn work over rig on location. See Erics report for details.
1465568247 2016-06-07 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
1486199363 2018-06-04 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection.
1501261814 2017-07-27 Brine Hauler No Violations Inspect Fishburn Services brine truck #112 (PJS-7626) on location. Brine, UIC number and other identification clearly and properly displayed. Status: ok.
1503987864 2012-11-21 Work Over Reconditioning No Violations Fishburn service rig has moved on location for work over. Shut down for Thanksgiving. Authorized personnel only signs are posted. Status: work in progress.
1506899199 2016-01-20 Work Over Reconditioning No Violations Fishburn service rig is on the well for workover.
1540614893 2008-07-01 Production Wells No Violations Chk well and storage, Ok.
1648549023 2018-12-06 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1684133452 2019-02-14 Surface Facility Construction No Violations The operator replaced the separator (heater treater) with the treater from the Redmond #2 (#4230) which is slated for plugging. Their hot oil truck was on location attempting to clean/unclog the separator and place in back into production.
1871245849 2018-09-13 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1900031581 2013-10-02 Work Over Reconditioning No Violations Fishburn service rig is on location performing work over. No Trespassing signs posted. Status: ok.
1924106348 2018-04-20 Production Wells No Violations Visit location with Health Physicist Mr. Paul Carder on location for testing.
1946244458 2019-12-3 0:00: PW No Violations 0.50
1966669928 2012-07-26 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a follow-up to a recent work over. The well has been placed back into production and is on pump with a propane powered black/orange USS Oilwell pump jack. They have closed the earthen pit and spread gravel around the well head. Remnants of work that remain on-site are a metal flow back tank, a rack of rods, 21 joints of tubing and 4 joints of 4.5 casing. The well identification is marked at the well and storage.
208346919 2017-12-1 0:00: PW No Violations
2106729229 2018-02-28 Production Wells No Violations Inspected the Gillson #1 (#2058) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
226087017 2018-4-2 0:00:0 PW No Violations
424135638 2017-5-31 0:00: WR No Violations
431433582 2015-2-26 0:00: PW No Violations
973297691 2018-3-26 0:00: PW No Violations
PL9164 PL No Violations

For data sources see[9]

References