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34-115-24618

Well Details

Well ID: 34-115-24618
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Country: United States
State: Ohio
County: Morgan
Municipality: York Township
Operator Name: TEMPLE OIL & GAS CO
Well Pad ID:
Farm/Lease Name: DALRYMPLE MERLE
License Status: Final Restoration
License Date: 2008-02-08
Spud Date: 2008-02-14
Spud Drilling Contractor: TEMPLE OIL & GAS
Final Drill Date: 2008-03-17
Well Total Depth: 1157.00 ft
Configuration: Vertical
Latitude: 39.740000
Longitude: -82.060000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-02-08 Proposed Formations:BEREA, Issued Date:2/8/2008, Expired Date:2/7/2009 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2008-03-17
Completion Report Received 2008-10-16
Construction Permit Expires 2009-02-07
Plugged/Abandoned 2014-11-03
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-12-17 1117 1137 20
1117 1137 20
1117 1137 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 300 Bbl 11000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 TEMPLE OIL & GAS CO 82.00 0.00 130
2009 TEMPLE OIL & GAS CO 0.00 0.00 30
2010 TEMPLE OIL & GAS CO 0.00 0.00 0
2011 TEMPLE OIL & GAS CO 0.00 66.00 365
2012 TEMPLE OIL & GAS CO 0.00 0.00 366
2013 TEMPLE OIL & GAS CO 0.00 0.00 365
2014 TEMPLE OIL & GAS CO 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 TEMPLE OIL & GAS CO Brine 0 130
2009 TEMPLE OIL & GAS CO Brine 155 30
2010 TEMPLE OIL & GAS CO Brine 0 0
2011 TEMPLE OIL & GAS CO Brine 90 365
2012 TEMPLE OIL & GAS CO Brine 0 366
2013 TEMPLE OIL & GAS CO Brine 0 365
2014 TEMPLE OIL & GAS CO Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1683161330 2014-8-11 0:00: PW No Violations
-1786215480 2013-6-17 0:00: PW No Violations 0.30
-514737995 2015-7-14 0:00: FR No Violations 1.00
-704681277 2014-2-4 0:00:0 PW No Violations 0.50
-905681038 2014-10-30 0:00 PB No Violations
0514737995 2015-07-14 Final Restoration No Violations The final restoration meets 1509.072.
0704681277 2014-02-04 Production Wells No Violations Compliance Action Follow-up -1786215480: I talked with Tracey and he stated he and MFC are partners on this well. It makes a lot of water and they are not sure if it is the formation or that there might be a hole in the casing. He will let me know what they plan on doing with the well after he talks with MFC owner. There has been no resolution to any of the issues.
0905681038 2014-10-30 Plug / Plug Back No Violations Operator was on location with rig. They had pulled the rods and tubing. The washed in 200 feet of clay for the bottom hole plug then ripped the 4.5 at 780. The operator then washed in another 200 of clay to 757. They will pull the 4.5 casing and return tomorrow to completely plug the rest of the hole.
1203702001 2008-02-21 Drill / Deepen / Reopen No Violations Stopped by cable tool rig for update on upcoming surface job,driller stated they hit mine shaft@148-153 told them they would have to set mine string to 203 they were going to pull 10 casing then ream out hole to 50 below shaft and cement pipe in place.
1210359970 2014-06-30 Production Wells No Violations Compliance Action Follow-up -1786215480: A Chiefs Order was issued to Temple Oil & Gas on May 15, 2014. The well is still shut in with no motor on the pumpjack. There are two 100bbl tanks in dike. There has been no resolution to any of the issues.
1219443284 2008-08-20 Preliminary Restoration No Violations Restoration work at site satisfactory, well is equipped with pumping unit and tubing&rods and 2-100 bbl tanks within dike area,also noted small gas compressor hooked to gas line coming from said well.
1229538784 2008-12-12 Production Wells No Violations Inspection revealed that well is equipped with pumping unit and tubing&rods and 1-100 bbl tank with dike in place.
1300451277 2014-03-28 Production Wells No Violations Compliance Action Follow-up -1786215480: The well is still shut in with no motor on the pumpjack. I will send the compliance notice to the supervisor for legal review.
1414764828 2014-10-31 Plug / Plug Back No Violations Operator continued with washing clay down the hole. They will return on Monday with more clay to finish the job.
1415019259 2014-11-03 Plug / Plug Back No Violations I was at this well to witness Temple Oil & Gas wash in plugging clay. They are currently working on the surface plug. The clay was filled to surface while I was there. I had them wait 1hr to let the clay settle then top the well off again.
1415032237 2014-11-03 Plug / Plug Back No Violations Operator was on location and washed in around 300 of clay to the surface. They have removed the tanks and restored the dike.
1420044971 2014-12-31 Plug / Plug Back No Violations Location has been graded and all of the production equipment has been removed however the operator has not restored vegetation. I will come back in the spring for another restoration inspection.
1575741261 2013-09-10 Production Wells No Violations Compliance Action Follow-up -1786215480: There has been no resolution to any of the issues.
1683161330 2014-08-11 Production Wells No Violations Compliance Action Follow-up -1786215480: A Chiefs Order was issued to Temple Oil & Gas on May 15, 2014. The well is still shut in with no motor on the pumpjack. There are two 100bbl tanks in dike. There has been no resolution to any of the issues.
1786215480 2013-06-17 Production Wells Violations Noted Well is currently shut in and there is no engine hooked up to the pumpjack and no electric box. I called and left Tracey with Temple a message regarding the issues. Operator must make well capable of production within 60 days; or plugging is required in 60 days.
2061371456 2008-02-25 Drill / Deepen / Reopen No Violations Stopped by cable tool rig for update on setting mine string,driller was reaming hole@165 he suspects possible deviation below shaft told him to contact inspector prior to running casing and cementing it in place.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1786215480 US-OH-117798 2014-11-07 Well shall be plugged
1786215480 US-OH-117799 2014-11-07 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References