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34-115-24601

Well Details

Well ID: 34-115-24601
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Country: United States
State: Ohio
County: Morgan
Municipality: York Township
Operator Name: SWINGLE DRILLING INC
Well Pad ID:
Farm/Lease Name: HILL ELDA
License Status: Producing
License Date: 2007-08-15
Spud Date: 2007-08-16
Spud Drilling Contractor: CENTURY WELL SERVICES,INC
Final Drill Date: 2007-11-23
Well Total Depth: 1033.00 ft
Configuration: Vertical
Latitude: 39.730000
Longitude: -82.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-08-15 Proposed Formations:BEREA, Issued Date:8/15/2007, Expired Date:8/14/2008 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2007-11-23
Construction Permit Expires 2008-08-14
Completion Report Received 2008-10-15
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-11-26 982 1001 20
982 1001 20
982 1001 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 24000 Gal 2000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 SWINGLE DRILLING INC 71.00 8.00 0
2008 SWINGLE DRILLING INC 71.00 8.00 0
2009 SWINGLE DRILLING INC 71.00 8.00 0
2010 SWINGLE DRILLING INC 71.00 8.00 0
2011 SWINGLE DRILLING INC 72.00 8.00 0
2012 SWINGLE DRILLING INC 244.00 8.00 0
2014 SWINGLE DRILLING INC 250.00 0.00 365
2016 SWINGLE DRILLING INC 235.00 0.00 365
2017 SWINGLE DRILLING INC 255.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 SWINGLE DRILLING INC Brine 8
2008 SWINGLE DRILLING INC Brine 8
2009 SWINGLE DRILLING INC Brine 8
2010 SWINGLE DRILLING INC Brine 8
2011 SWINGLE DRILLING INC Brine 8
2012 SWINGLE DRILLING INC Brine 8
2014 SWINGLE DRILLING INC Brine 0 365
2016 SWINGLE DRILLING INC Brine 0 365
2017 SWINGLE DRILLING INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2037983606 2013-9-10 0:00: PW No Violations 0.50
1229985184 2008-12-22 Preliminary Restoration No Violations Restoration work at site satisfactory,pit has been filled in and site restored and well is equipped with pumping unit and 2-100 bbl tanks and separator located within dike area.
1371479619 2013-06-17 Production Wells Violations Noted There are two 100 bbl tanks and a separator within the dike. One of the tanks shows signs of a small leak however it appeared to be empty. The separator has a small leak in a threaded section of pipe. There is no legible identification and production has never been reported to the state. Operator must repair or replace all leaking equipment, post legible id, and send in production. Well is just holding the lease right now as stated by Mark Swingle, and he said the well barely produces any gas these days. I told him he must make well capable of production within 60 days or plugging is required in 60 days.
2037983606 2013-09-10 Production Wells No Violations Compliance Action Follow-up 1371479619: Well is in compliance. There are no issues to report at this time.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1371479619 US-OH-110971 2013-10-22 Failure to legibly identify well
1371479619 US-OH-110972 2013-10-22 Equipment pressure rated below operating pressure
1371479619 US-OH-110973 2013-10-22 Well shall be plugged
1371479619 US-OH-110974 2013-10-22 Nonproduction; well shall be plugged or placed in temporary inactive status
1371479619 US-OH-110975 2013-10-22 Statement of annual production not filed

For data sources see[9]

References