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34-115-24454

Well Details

Well ID: 34-115-24454
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Country: United States
State: Ohio
County: Morgan
Municipality: Center Township
Operator Name: GENESIS RESOURCES LLC
Well Pad ID:
Farm/Lease Name: MORETZ UNIT
License Status: Producing
License Date: 2000-01-26
Spud Date: 2000-02-01
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 2000-02-06
Well Total Depth: 5399.00 ft
Configuration: Vertical
Latitude: 39.650000
Longitude: -81.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2000-01-26 Proposed Formations:CLINTON/MEDINA, Issued Date:1/26/00, Expired Date:1/25/01 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2000-02-01 RBDMS Rec
Completed 2000-02-06 RBDMS Rec
Reached Total Depth 2000-02-06 RBDMS Rec
Completion Report Received 2000-07-17 RBDMS Rec
Construction Permit Expires 2001-01-25 RBDMS Rec
Change of Owner 2015-07-10 Operator changed from 6288, ALLIANCE PETROLEUM CORPORATION to 9086, GENESIS RESOURCES LLC
Record Last Modified 2015-09-24 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-10-06 5124 5194 34
2000-10-06 5260 5272 28
5124 5194 34
5260 5272 28
5124 5194 34

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 78000 Gal 20000 FRAC PLUG @ 5230'
H2O 15 100000 Gal 17500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2000 OHIO L & M CO INC 9348.00 50.00 294
2001 OHIO L & M CO INC 8727.00 34.00 365
2002 OHIO L & M CO INC 5170.00 0.00 365
2003 OHIO L & M CO INC 5128.00 34.00 365
2004 OHIO L & M CO INC 4299.00 30.00 365
2005 OHIO L & M CO INC 3352.00 23.00 365
2006 ALLIANCE PETROLEUM CORPORATION 3434.00 0.00 365
2007 ALLIANCE PETROLEUM CORPORATION 3168.00 0.00 365
2008 ALLIANCE PETROLEUM CORPORATION 2759.00 0.00 365
2009 ALLIANCE PETROLEUM CORPORATION 2422.00 0.00 365
2010 ALLIANCE PETROLEUM CORPORATION 2050.00 0.00 365
2011 ALLIANCE PETROLEUM CORPORATION 2028.00 46.00 365
2012 ALLIANCE PETROLEUM CORPORATION 2412.00 0.00 366
2013 ALLIANCE PETROLEUM CORPORATION 2085.00 0.00 365
2014 ALLIANCE PETROLEUM CORPORATION 2226.00 0.00 365
2015 GENESIS RESOURCES LLC 597.00 0.00 184
2016 GENESIS RESOURCES LLC 1344.00 0.00 342
2017 GENESIS RESOURCES LLC 809.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2000 OHIO L & M CO INC Brine 0 294
2001 OHIO L & M CO INC Brine 0 365
2002 OHIO L & M CO INC Brine 0 365
2003 OHIO L & M CO INC Brine 0 365
2004 OHIO L & M CO INC Brine 0 365
2005 OHIO L & M CO INC Brine 0 365
2006 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2007 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2008 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2009 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2010 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2011 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2012 ALLIANCE PETROLEUM CORPORATION Brine 0 366
2013 ALLIANCE PETROLEUM CORPORATION Brine 36 365
2014 ALLIANCE PETROLEUM CORPORATION Brine 46 365
2015 GENESIS RESOURCES LLC Brine 0 184
2016 GENESIS RESOURCES LLC Brine 0 342
2017 GENESIS RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-114861807 2015-10-27 0:00 PW No Violations 1.50
001289i343 2002-04-26 Preliminary Restoration No Violations PRELIMENARY RESTORATION
0114861807 2015-10-27 Production Wells No Violations Upon arriving at the well, the well utilized a gas lift system for the means of production. The well head and the production pipe at the well head all appeared in good shape. The well head was properly IDd. The tank also had ID. The 100 barrel steel tank had what would appear to be a brine scald around the south and southeast sides of the tank from leaking production lines. The drip also was leaking around fittings and plugs causing contamination. Both of these were contained in the dike but will need to be corrected.
0390159320 2017-02-27 Production Wells No Violations The inspection this day revealed that this well is equipped with a plunger lift system, a 4 1/2 inch diameter wellhead, and 1 1/2 inch diameter production tubing. The valves on the wellhead are open at the time of inspection. The tank battery for this well is equipped with a horizontal separator, one (1) 100 barrel steel tank with proper identification, and a meter with a current chart inside it. There are no issues to report and the well is in production at the time of inspection.
1125140997 2005-08-22 Production Wells No Violations No violations noted,well is equipped with 1-100bbl tank and is a rabbit well.
1289i343 2002-4-26 0:00: PL No Violations
390159320 2017-2-27 0:00: PW No Violations 2.00

For data sources see[9]

References