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34-115-24427

Well Details

Well ID: 34-115-24427
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Country: United States
State: Ohio
County: Morgan
Municipality: Bristol Township
Operator Name: THOMPSON CONSUMER ELECTRONICS
Well Pad ID:
Farm/Lease Name: LITTLE- RAY UNIT
License Status: Final Restoration
License Date: 2000-11-20
Spud Date: 1996-01-19
Spud Drilling Contractor: UNGER DRILLING
Final Drill Date: 1996-01-29
Well Total Depth: 5109.00 ft
Configuration: Vertical
Latitude: 39.680000
Longitude: -81.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1995-12-28 Issued Date 12/28/95 Expired Date 12/27/96 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05109 Proposed Drill Depth 05109
Original Spud 1996-01-15
Completed 1996-01-29
Reached Total Depth 1996-01-29
CO 1996-02-15 4339 MISSION GAS COMPANY INC GeoDate 12/28/95
Completion Report Received 1996-09-13
APP 2000-11-20 Proposed Formations:CLINTON, Issued Date:11/20/2000, Expired Date:11/20/2001 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2001-06-29
Construction Permit Expires 2001-11-20
Record Last Modified 2013-03-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4806 4882 0
4806 4882 0
2006-09-11 4845 4860 13
4845 4860 13
4806 4882 0
2006-09-11 4948 4956 5

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2100 Bbl 80000 FRAC W/2100 BW & 80M# SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1996 THOMPSON CONSUMER ELECTRONICS 27499.00 430.00 336
1997 THOMPSON CONSUMER ELECTRONICS 7282.00 294.00 365
1998 THOMPSON CONSUMER ELECTRONICS 3414.00 202.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1996 THOMPSON CONSUMER ELECTRONICS Brine 402 336
1997 THOMPSON CONSUMER ELECTRONICS Brine 197 365
1998 THOMPSON CONSUMER ELECTRONICS Brine 63 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
001289i357 2002-04-29 Final Restoration No Violations FINAL RESTORATION, KEEP AN EYE ON THE GRASS!
1289i10451 2001-04-13 Final Restoration No Violations inspected wellsite with Dick Shockley, Gary Green, and Mr. Hook, Central Ohio coal Co. found area north west of wellhead has slipped downhill taking wellhead and laying it over. 8 csg. Cannot be seen, only 1.5 tubing, well is gassing. Mission Gas has permit to plug well, but wants Central Ohio Coal to furnish heavy equipment to rebuild location to move rig on to plug well. Steve Hook,Central Ohio Coal, alledges mission gas caused slip and that coal company is not at fault. A settling pond was constructed by coal company, to the north of wellhead, for reclamation purposes. Miision Gas Co. alledges, the pond construction started the location to slip. In any event the well will have to be properly plugged, and restoration performed
1289i10451285 2001-4-13 0:00: FR No Violations
1289i357 2002-4-29 0:00: FR No Violations

For data sources see[9]

References