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34-115-24408

Well Details

Well ID: 34-115-24408
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Country: United States
State: Ohio
County: Morgan
Municipality: Union Township
Operator Name: GLADDEN MERRILL L
Well Pad ID:
Farm/Lease Name: GLADDEN
License Status: Domestic Well
License Date: 2009-07-29
Spud Date: 1995-03-04
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 1995-03-08
Well Total Depth: 4247.00 ft
Configuration: Vertical
Latitude: 39.560000
Longitude: -82.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1995-02-03 198 VIKING RESOURCES CORP GeoDate 2/3/95
Oil and Gas 1995-02-03 Issued Date 2/3/95 Expired Date 2/3/96 Acres 0268300 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04247 Proposed Drill Depth 04247
Original Spud 1995-03-04
Completed 1995-03-08
Reached Total Depth 1995-03-08
Annular Disposal Well 1995-03-10
Completion Report Received 1995-04-27
Change of Owner 1998-07-01 Operator changed from 198, VIKING RESOURCES CORP to 3793, ENERGY SEARCH INC
Revocation 2000-04-30
Change of Owner 2008-02-26 Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC
Last Compliance Report 2008-10-01
APP 2009-01-23 Proposed Formations:CLINTON, Issued Date:1/23/2009, Expired Date:1/23/2010 6:00:00 AM, Drilling unit acres:268.3, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2009-07-01 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7640, SMITH RONALD DBA CHIPCO
APP 2009-07-29 Proposed Formations:CLINTON, Issued Date:7/29/2009, Expired Date:7/29/2010 6:00:00 AM, Drilling unit acres:268.3, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2009-10-19 Operator changed from 7640, SMITH RONALD DBA CHIPCO to 8562, GLADDEN MERRILL L
Construction Permit Expires 2010-07-29
Record Last Modified 2017-07-17

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-03-18 3990 4020 20
3990 4020 20
3990 4020 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 58220 Gal 75000 BKDN 570 PSI, ISIP 750 PSI.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 VIKING RESOURCES LLC 6947.00 595.00 0
1996 VIKING RESOURCES LLC 6529.00 451.00 0
1997 VIKING RESOURCES LLC 3591.00 258.00 0
1998 ENERGY SEARCH INC 562.00 213.00 244
1999 ENERGY SEARCH INC 2338.00 95.00 365
2000 ENERGY SEARCH INC 0.00 0.00 365
2001 ENERGY SEARCH INC 788.00 48.00 365
2002 ENERGY SEARCH INC 323.00 0.00 365
2003 ENERGY SEARCH INC 59.00 0.00 365
2004 ENERGY SEARCH INC 73.00 0.00 365
2005 ENERGY SEARCH INC 0.00 0.00 365
2006 ENERGY SEARCH INC 0.00 0.00 0
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 VIKING RESOURCES LLC Brine 754 0
1996 VIKING RESOURCES LLC Brine 196 0
1997 VIKING RESOURCES LLC Brine 132
1998 VIKING RESOURCES LLC Brine 0 365
1999 ENERGY SEARCH INC Brine 0 365
2000 ENERGY SEARCH INC Brine 365
2001 ENERGY SEARCH INC Brine 0 365
2002 ENERGY SEARCH INC Brine 365
2003 ENERGY SEARCH INC Brine 365
2004 ENERGY SEARCH INC Brine 0 365
2005 ENERGY SEARCH INC Brine 0 365
2006 ENERGY SEARCH INC Brine 0 0
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-479250148 2018-6-7 0:00:0 TD No Violations 0.30
0000017214 Preliminary Restoration No Violations PASSED Y WITNESSED 5/13/96 INSPECTOR MIKE KAVAGE DATE 05/1319/96 DATA FROM OLD VAX INFO
0479250148 2018-06-07 Temporary Abandoned Annular Disposal No Violations My inspection revealed that the well was not equipped for annular disposal use. Time of inspection: 1:10 PM. Weather: 71 degrees F, Sunny
1041875150 2005-05-11 Annular Disposal No Violations A.D.not being used, brine is being stored in common tank site shared with other wells on the farm.
17214 PL No Violations
2081069616 2008-09-23 Annular Disposal No Violations A.D. not hooked up well is equipped with pumping unit and 2-100 bbl tanks well does not appear to be produced much according to division records will call well owner and discuss future plans for said well.

For data sources see[9]

References