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34-115-24351

Well Details

Well ID: 34-115-24351
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield Township
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name: HIPP G
License Status: Final Restoration
License Date: 2008-02-21
Spud Date: 1993-09-07
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1993-09-09
Well Total Depth: 4351.00 ft
Configuration: Vertical
Latitude: 39.640000
Longitude: -82.000000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1993-02-02 Issued Date 2/2/93 Expired Date 2/2/94 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04351 Proposed Drill Depth 04351
Original Spud 1993-09-07
Completed 1993-09-09
Reached Total Depth 1993-09-09
CO 1994-03-10 133 QUAKER STATE OIL REF CORP GeoDate 2/2/93
Completion Report Received 1994-03-15
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/2/93
Change of Owner 2002-08-09 Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC
APP 2007-04-16 Proposed Formations:CLINTON, Issued Date:4/16/2007, Expired Date:4/15/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2007-06-26 Operator changed from 1966, PETROX, INC to 6295, KNOX ENERGY INC.
Plugged/Abandoned 2008-02-14
APP 2008-02-21 Proposed Formations:CLINTON, Issued Date:2/21/2008, Expired Date:2/20/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2009-02-20
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4107 4160 0
4107 4160 0
2006-09-11 4126 4164 21
4126 4164 21
4107 4160 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 105520 Gal 0 FRAC W/105,520 GAL SLICKWATER

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 QUAKER STATE OIL REF CORP 5800.00 0.00 365
1994 QUAKER STATE OIL REF CORP 18408.00 0.00 365
1995 BELDEN & BLAKE CORPORATION 2499.00 0.00 98
1996 BELDEN & BLAKE CORPORATION 2829.00 0.00 279
1997 BELDEN & BLAKE CORPORATION 2137.00 0.00 165
1998 BELDEN & BLAKE CORPORATION 34.00 0.00 365
1999 BELDEN & BLAKE CORPORATION 16.00 0.00 366
2001 BELDEN & BLAKE CORPORATION 0.00 0.00 366
2002 PETROX, INC 0.00 0.00 0
2003 PETROX, INC 0.00 0.00 0
2004 PETROX, INC 0.00 0.00 0
2005 PETROX, INC 14.00 0.00 365
2006 PETROX, INC 0.00 0.00 0
2007 PETROX, INC 0.00 0.00 0
2008 KNOX ENERGY INC. 0.00 0.00 45

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 QUAKER STATE OIL REF CORP Brine 0 365
1994 QUAKER STATE OIL REF CORP Brine 1217 365
1995 BELDEN & BLAKE CORPORATION Brine 0 98
1996 BELDEN & BLAKE CORPORATION Brine 2 279
1997 BELDEN & BLAKE CORPORATION Brine 2 165
1998 BELDEN & BLAKE CORPORATION Brine 0 365
1999 BELDEN & BLAKE CORPORATION Brine 0 366
2001 BELDEN & BLAKE CORPORATION Brine 0 366
2002 PETROX, INC Brine 0 0
2003 PETROX, INC Brine 0 0
2004 PETROX, INC Brine 0 0
2005 PETROX, INC Brine 0 365
2006 PETROX, INC Brine 0 0
2007 PETROX, INC Brine 0
2008 KNOX ENERGY INC. Brine 0 45

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000011677 Preliminary Restoration No Violations PASSED Y WITNESSED 12/14/94 INSPECTOR GERALD YOUNG DATE 12/1419/94 DATA FROM OLD VAX INFO
11677 PL No Violations
1202768710 2008-02-11 Plug / Plug Back No Violations Stopped by service rig for update on upcoming plugging operation,rig was on site crew was moving pumping unit off well site so they could move rig in on site operator stated they would pull rods and check fluid level should be ready to set bottom hole plug 2/12/08.
1203033621 2008-02-14 Annular Disposal No Violations Well has been plugged,it needs to be removed from annular disposal inspection list.
1228061590 2008-11-26 Final Restoration No Violations Final restoration work at site satisfactory,pit has been filled in and site restored and vegetation has been established.

For data sources see[9]

References