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34-115-24104

Well Details

Well ID: 34-115-24104
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Country: United States
State: Ohio
County: Morgan
Municipality: Marion Township
Operator Name: METCALF JAMIE DBA C&J OIL & GA
Well Pad ID:
Farm/Lease Name: ADRIAN CARL F
License Status: Producing
License Date: 1988-09-22
Spud Date: 1988-10-17
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 1988-10-19
Well Total Depth: 1615.00 ft
Configuration: Vertical
Latitude: 39.530000
Longitude: -81.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1988-09-22 Issued Date 9/22/88 Expired Date 9/22/89 Acres 0107750 Tool Type RTA Proposed Formation BEREA Proposed Depth 01615 Proposed Drill Depth 01615
Original Spud 1988-10-17 FDT=GRAY SHALE
Completed 1988-10-19 FDT=GRAY SHALE
Reached Total Depth 1988-10-19 FDT=GRAY SHALE
CO 1989-01-23 302 STEWART DRILLING CO. INC GeoDate 9/22/88
Construction Permit Expires 1989-09-22 FDT=GRAY SHALE
Completion Report Received 1990-07-12 FDT=GRAY SHALE
CO 1992-02-03 4074 OIL ENTERPRISES GeoDate 9/22/88
Change of Owner 1998-04-16 Operator changed from 4074, OIL ENTERPRISES to 1868, DUSTY DRILL & PRO CORP
Change of Owner 1998-08-12 Operator changed from 1868, DUSTY DRILL & PRO CORP to 5852, METCALF JOHN & JAMIE
Change of Owner 2010-06-09 Operator changed from 5852, METCALF JOHN & JAMIE to 8277, M H OILFIELD SERVICE LLC
Change of Owner 2010-12-09 Operator changed from 8277, M H OILFIELD SERVICE LLC to 8739, METCALF JAMIE DBA C&J OIL & GA
Record Last Modified 2017-02-15 FDT=GRAY SHALE

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1548 1562 0
1548 1562 0
2006-09-11 1550 1560 11
1550 1560 11
1548 1562 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
CO2 0 5 Tons 0
H2O 0 738 Bbl 20000 FRAC:WATER/SAND/CO2

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 STEWART DRILLING CO. INC 3348.00 0.00 334
1990 STEWART DRILLING CO. INC 2284.00 51.00 365
1993 OIL ENTERPRISES 552.00 0.00 365
1994 OIL ENTERPRISES 1351.00 0.00 365
1995 OIL ENTERPRISES 566.00 0.00 180
1996 OIL ENTERPRISES 0.00 0.00 0
1998 OIL ENTERPRISES 0.00 0.00 0
2002 METCALF JOHN C DBA METCALF DRI 200.00 0.00 100
2003 METCALF JOHN C DBA METCALF DRI 200.00 0.00 100
2005 METCALF JOHN C DBA METCALF DRI 950.00 0.00 365
2006 METCALF JOHN C DBA METCALF DRI 812.00 0.00 365
2010 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 0
2011 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 0
2012 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 0
2013 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 0
2014 METCALF JAMIE DBA C&J OIL & GA 257.00 0.00 365
2015 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 365
2016 METCALF JAMIE DBA C&J OIL & GA 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 STEWART DRILLING CO. INC Brine 0 334
1990 STEWART DRILLING CO. INC Brine 0 365
1993 OIL ENTERPRISES Brine 0 365
1994 OIL ENTERPRISES Brine 0 365
1995 OIL ENTERPRISES Brine 0 180
1996 OIL ENTERPRISES Brine 0 0
1998 OIL ENTERPRISES Brine 0 0
2002 METCALF JOHN C DBA METCALF DRI Brine 70 100
2003 METCALF JOHN C DBA METCALF DRI Brine 15 100
2005 METCALF JOHN C DBA METCALF DRI Brine 0 365
2006 METCALF JOHN C DBA METCALF DRI Brine 0 365
2010 METCALF JAMIE DBA C&J OIL & GA Brine 0 0
2011 METCALF JAMIE DBA C&J OIL & GA Brine 0 0
2012 METCALF JAMIE DBA C&J OIL & GA Brine 0 0
2013 METCALF JAMIE DBA C&J OIL & GA Brine 0 0
2014 METCALF JAMIE DBA C&J OIL & GA Brine 0 365
2015 METCALF JAMIE DBA C&J OIL & GA Brine 0 365
2016 METCALF JAMIE DBA C&J OIL & GA Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1078707699 2013-8-20 0:00: PW No Violations
-1396300428 2015-10-16 0:00 PW No Violations 1.00
0000PL9262 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0397488231 2013-02-26 Preliminary Restoration Violations Noted Upon inspection, I found the well producing through the 4.5. There was a service rig still on location. The rods were all pulled and laying on a rack. There was a separator and one 100 barrel tank at well location. There was no identification posted and last recorded production was in 2006. I called and left a message with Jamie Metcalf regarding the issues. Operator must post legible ID and get current on production.
1078707699 2013-08-20 Production Wells No Violations Compliance Action Follow-up 397488231: There is an identification posted at the wellhead and a new dike has been constructed around the tank and separator. Operator is also up to date with production however they are still trying to get someone to swab the well to increase production.
1367588123 2013-05-03 Production Wells No Violations Compliance Action Follow-up 397488231: Operator is now current on production, however service rig is still at well location and production equipment is still sitting by the wellhead. Fluid could be heard running in line from separator into the tank. There is still no identification posted and the tank dike is in poor condition as well as overgrown with vegetation. I called and left a message again for Jamie Metcalf concerning the issues.
1368048205 2013-05-08 Production Wells No Violations I met Jamie Metcalf and her son at the location and they agreed to get the rig out by July 1st. They will post identification, remove the rack of rods, and clear the vegetation from the tank area. Once the ground dries out they will also build up the dike.
1373032411 2013-07-05 Production Wells No Violations Compliance Action Follow-up 397488231: There has been no resolution to any of the issues. Some vegetation has been cleared from the area but there is still no identification and the service rig is still sitting idle. There is no dike and the stack of rods are still adjacent to the rig. I called and left a message with Jamie Metcalf regarding the issues. 7/10/2013: Jamie called and stated she is having the Altiers swab and put rods back in the well. She will also have someone finish the dike and post id this week.
1396300428 2015-10-16 Production Wells No Violations On my inspection today I found there to be no violations to report with this well.
1401706872 2014-01-21 Administrative Inspection No Violations I talked with Jamie Metcalf and she said Kenny Wright swabbed the well and that it is ready for production. Gatherco told her gas was good to go through their transmission lines, however she is still waiting to hear when they will put it back in commercial production. She will get an identification out there within the next few weeks.
397488231 2013-2-26 0:00: PL No Violations 2.50
PL9262 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0397488231 US-OH-124236 2014-01-28 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)

For data sources see[9]

References