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34-115-24038

Well Details

Well ID: 34-115-24038
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Country: United States
State: Ohio
County: Morgan
Municipality: Morgan Township
Operator Name: KILLBUCK CREEK OIL CO LLC
Well Pad ID:
Farm/Lease Name: DIOCESE OF STUBENVILLE
License Status: Producing
License Date: 1987-07-15
Spud Date: 1987-07-29
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 1987-07-30
Well Total Depth: 1800.00 ft
Configuration: Vertical
Latitude: 39.660000
Longitude: -81.820000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1987-07-15 471 EAGLE MOUNTAIN ENERGY GeoDate 7/15/87
Oil and Gas 1987-07-15 Issued Date 7/15/87 Expired Date 7/14/88 Acres 0010000 Tool Type RTA Proposed Formation BEREA Proposed Depth 01800 Proposed Drill Depth 01800
Original Spud 1987-07-29
Completed 1987-07-30
Reached Total Depth 1987-07-30
Completion Report Received 1987-08-21
Construction Permit Expires 1988-07-14
Change of Owner 1999-06-30 Operator changed from 471, EAGLE MOUNTAIN ENERGY to 1512, ALTIER H L SERVICE CO INC
Change of Owner 2008-06-24 Operator changed from 1512, ALTIER H L SERVICE CO INC to 8026, KILLBUCK CREEK OIL CO LLC
Last Compliance Report 2014-10-09
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1692 1704 12
1692 1704 12
1692 1704 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 600 Bbl 14000 FRAC W/600 BW & 140 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 EAGLE MOUNTAIN ENERGY 666.00 0.00 114
1988 EAGLE MOUNTAIN ENERGY 2890.00 58.00 365
1989 SCION ENERGY INC 2210.00 67.00 365
1990 EAGLE MOUNTAIN ENERGY 2247.00 38.00 365
1991 EAGLE MOUNTAIN ENERGY 1697.00 0.00 365
1996 EAGLE MOUNTAIN ENERGY 0.00 0.00 365
2001 H L ALTIER SERVICE CO INC 0.00 0.00 360
2009 KILLBUCK CREEK OIL CO LLC 249.00 0.00 365
2010 KILLBUCK CREEK OIL CO LLC 233.00 0.00 365
2012 KILLBUCK CREEK OIL CO LLC 101.00 0.00 366

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 EAGLE MOUNTAIN ENERGY Brine 106 114
1988 EAGLE MOUNTAIN ENERGY Brine 66 365
1989 SCION ENERGY INC Brine 19 365
1990 EAGLE MOUNTAIN ENERGY Brine 23 365
1991 EAGLE MOUNTAIN ENERGY Brine 2 365
1996 EAGLE MOUNTAIN ENERGY Brine 0 365
2001 H L ALTIER SERVICE CO INC Brine 0 360
2009 KILLBUCK CREEK OIL CO LLC Brine 0 365
2010 KILLBUCK CREEK OIL CO LLC Brine 0 365
2012 KILLBUCK CREEK OIL CO LLC Brine 0 366

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1129088688 2020-4-3 0:00:0 TD No Violations 0.50
-1798325660 2010-3-15 0:00: AD No Violations
0000017834 Preliminary Restoration No Violations PASSED Y WITNESSED 10/6/87 INSPECTOR DATE 10/0619/87 DATA FROM OLD VAX INFO
0000PL9309 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0200087629 2003-04-24 Production Wells No Violations well in production no violations noted the day of my inspection.
0204211364 2018-10-10 Production Wells No Violations I was on location today to do a field inspection on this well. The well appears to be capable of production at this time. The well has a pumping unit on it with rods and tubing in it. The production valve on the tubing and casing are open at this time to the production tank and sales line. There is a new gas chart at the sales meter recording the production. The identification for the well is located at the production tank. There are no violations at this time.
1112869098 2006-10-13 Annular Disposal No Violations A.D. not hooked up well is equipped with pump jack and tubing&rods and 1-100 bbl tank.
1203695972 2008-02-20 Annular Disposal Violations Noted Upon inspecting site at request of county engineer Steve Marshall found well to be idle,motor has been removed from pump jack and no production has been reported on well since 1991,all valves at wellhead were shut on the day of my inspection.
1238671694 2009-04-02 Annular Disposal Violations Noted A.D. not hooked up, well is back into production resolving previous Notice of Violation.
1411568249 2014-09-24 Annular Disposal No Violations An inspection of this well was requested by Central Office to verify Annular Disposal (AD) connection. AD is not connected to the wellhead at this time.
17834 PL No Violations
1798325660 2010-03-15 Annular Disposal No Violations No violations at time of inspection.
200087629 2003-4-24 0:00: PW No Violations
204211364 2018-10-10 0:00 PW No Violations 0.50
PL9309 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1203695972 US-OH-105320 2008-02-22 Failure to legibly identify well
1203695972 US-OH-105321 2008-02-22 Well shall be plugged
1238671694 US-OH-106358 2008-02-22 Failure to legibly identify well
1238671694 US-OH-106359 2008-02-22 Well shall be plugged

For data sources see[9]

References