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34-115-23207

Well Details

Well ID: 34-115-23207
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Country: United States
State: Ohio
County: Morgan
Municipality: Malta Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: SEES RUSSELL
License Status: Final Restoration
License Date: 2016-07-13
Spud Date: 1983-06-06
Spud Drilling Contractor: UNGER DRILLING
Final Drill Date: 1983-06-11
Well Total Depth: 4968.00 ft
Configuration: Vertical
Latitude: 39.610000
Longitude: -81.850000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-05-25 Issued Date 5/25/83 Expired Date 11/21/83 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04968 Proposed Drill Depth 04968
Original Spud 1983-06-06
Completed 1983-06-11
Reached Total Depth 1983-06-11
CO 1983-06-27 54 TITAN ENERGY CORP GeoDate 5/25/83
Completion Report Received 1983-07-22
CO 1996-11-04 2070 HALWELL COMPANY GeoDate 5/25/83
APP 2016-07-13 Proposed Formations:QUEENSTON SHALE, Issued Date:7/13/2016, Expired Date:7/13/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2016-10-12
Record Last Modified 2017-06-28
Construction Permit Expires 2018-07-13

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4761 4767 2
4761 4767 2
4761 4767 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
CO2 0 20 Tons 0
H2O 0 42000 Gal 24000 FRAC;42MG H2O,24M# SD,40M# SD

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 FUTURE ENERGY CORP 1185.00 133.00 365
1989 FUTURE ENERGY CORP 2550.00 267.00 365
1990 FUTURE ENERGY CORP 952.00 126.00 365
1991 FUTURE ENERGY CORP 5.00 0.00 365
1994 TITAN ENERGY CORP 0.00 0.00 365
1995 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1996 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1997 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1998 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2000 STONEBRIDGE OPERATING CO LLC 0.00 0.00 366
2001 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2002 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2003 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2004 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2005 STONEBRIDGE OPERATING CO LLC 12.00 0.00 0
2006 STONEBRIDGE OPERATING CO LLC 7.00 0.00 0
2007 STONEBRIDGE OPERATING CO LLC 4.00 0.00 0
2008 STONEBRIDGE OPERATING CO LLC 7.00 0.00 98
2009 STONEBRIDGE OPERATING CO LLC 33.00 0.00 7
2010 STONEBRIDGE OPERATING CO LLC 60.00 0.00 273
2011 STONEBRIDGE OPERATING CO LLC 70.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 83.00 0.00 364
2013 STONEBRIDGE OPERATING CO LLC 42.00 0.00 365
2014 STONEBRIDGE OPERATING CO LLC 10.00 0.00 365
2015 STONEBRIDGE OPERATING CO LLC 0.00 0.00 357
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 FUTURE ENERGY CORP Brine 0 365
1989 FUTURE ENERGY CORP Brine 0 365
1990 FUTURE ENERGY CORP Brine 0 365
1991 FUTURE ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1995 STONEBRIDGE OPERATING CO LLC Brine 0 0
1996 STONEBRIDGE OPERATING CO LLC Brine 0 0
1997 STONEBRIDGE OPERATING CO LLC Brine 0 0
1998 STONEBRIDGE OPERATING CO LLC Brine 0 0
2000 STONEBRIDGE OPERATING CO LLC Brine 0 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 0
2002 STONEBRIDGE OPERATING CO LLC Brine 52 0
2003 STONEBRIDGE OPERATING CO LLC Brine 0 0
2004 STONEBRIDGE OPERATING CO LLC Brine 0 0
2005 STONEBRIDGE OPERATING CO LLC Brine 0 0
2006 STONEBRIDGE OPERATING CO LLC Brine 0 0
2007 STONEBRIDGE OPERATING CO LLC Brine 0 0
2008 STONEBRIDGE OPERATING CO LLC Brine 0 98
2009 STONEBRIDGE OPERATING CO LLC Brine 0 7
2010 STONEBRIDGE OPERATING CO LLC Brine 0 273
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 364
2013 STONEBRIDGE OPERATING CO LLC Brine 0 365
2014 STONEBRIDGE OPERATING CO LLC Brine 0 365
2015 STONEBRIDGE OPERATING CO LLC Brine 0 357
2016 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1100068012 2011-3-2 0:00:0 PW No Violations 0.50
-182948275 2015-11-18 0:00 PW No Violations 1.00
-575944741 2015-7-21 0:00: NF No Violations 2.00
-842659890 2015-8-17 0:00: PW No Violations 1.00
0000PL9731 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0072095241 2016-10-11 Plug / Plug Back No Violations I was on location on 10/11/2016 to witness the well plugged by Huffman & Bowers. Barry set a Clinton Sand plug (4770-4370 feet), a Big Lime/rip plug (3512-3312 feet), a bottom of surface plug (1770-1570 feet), and a surface plug (200-0 feet). Barry was able to rip the pipe off at around 3480 feet. They then pulled one joint to about 3439 feet where we set our rip plug. All 4 1/2 inch diameter casing was pulled from the hole after plugging was finished. The Berea was covered by the surface casing and no individual plug was needed.
0182948275 2015-11-18 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The well is still currently sitting idle with no change in it being capable of production. The well is in violation.
0560650035 2013-06-28 Production Wells Violations Noted Well is idle and completely overgrown with vegetation. The valve is closed on the 4.5 casing and the well is not connected to any lines. Previous inspection by Cindy Van Dyke was for the tank battery along road and not the wellhead. There is no current production. I spoke to Dave Crippen and he said he would pass along the information in regards to the idle well. The operator must post proper id and report production to the state. Operator must make well capable of production within 60 days; or plugging is required in 60 days.
0575944741 2015-07-21 Field Inspected, Well Not Found No Violations I tried to find the location of this well. I was unable to find any entrance for it so I walked what I thought was the lease road. I never did find a well. I ended up contacting Jake Glasscock and he will be meeting me next week to help me find it.
0588388390 2017-06-20 Final Restoration No Violations The final restoration meets 1509.072(B),
0609115286 2014-02-21 Production Wells No Violations Compliance Action Follow-up 560650035:The well is still idle and there has been no resolution to any of the issues. I called Dave Crippen and left a message in regards to the well issues.
0674100211 2015-07-28 Production Wells No Violations I went out to this well to do a follow-up inspection on it. At this time the well is still idle and not capable of production. The valves are shut at the wellhead making it incapable of production. I took pictures of my findings today during my inspection.
0842659890 2015-08-17 Production Wells No Violations I was on location to do a follow-up inspection on the well. There has been no change to the well. The well is still incapable of production and is still in violation. I took updated photos of the well during my inspection.
1100068012 2011-03-02 Production Wells No Violations Inspection this day found tank but not well - must be across the road. No meter found, tank has peeling IDs, fair to good dike, no one has been to tanks in awhile. I dont believe well is producing, annual production falls below minimums.
1202196080 2014-08-19 Production Wells No Violations Compliance Action Follow-up 560650035: There was a new meter box installed up at the tank battery however there was no chart and the well is still shut in.
1277887975 2014-03-20 Production Wells No Violations Compliance Action Follow-up 560650035:The well is still idle and equipped with a swage. There is a closed ball valve and there are no flow lines attached to the well. The landowner was present and stated the well has not produced in over 10 years. There has been no resolution to any of the issues.
1383059964 2013-10-29 Production Wells No Violations Compliance Action Follow-up 560650035: There has been no resolution to any of the issues.
1400692953 2014-05-20 Production Wells No Violations Compliance Action Follow-up 560650035: The well is still idle and there has been no resolution to any of the issues. There has been some recent logging operation in and around the well location.
1403018627 2014-06-17 Production Wells No Violations Compliance Action Follow-up 560650035: I received a call from the landowner and he stated someone from Stonebridge was on property with heavy equipment clearing access road. He stated that they had worked on the wellhead. Upon inspection, I found that the well has been recently equipped with a reducer swage and connected to a flow line. The valve is shut on the wellhead. The tank battery is across the road and is hared with several other wells. There is an id on one of the tanks however all of the separators are disconnected and overgrown. I talked to Dave Crippen of Stonebridge and he stated that he needs to work more on the well. He said that he needs to get a new meter box up to see if he can get well back in production.
1410802436 2014-09-15 Production Wells No Violations Compliance Action Follow-up 560650035: The well is currently shut in at the wellhead and at the separator. There is still no chart in the new meter box.
1477068816 2016-11-11 Plug / Plug Back No Violations I was on location on 10/11/2016 to witness the well plugged by Huffman & Bowers. Barry set a Clinton Sand plug (4770-4370 feet), a Big Lime/rip plug (3512-3312 feet), a bottom of surface plug (1770-1570 feet), and a surface plug (200-0 feet). Barry was able to rip the pipe off at around 3480 feet. They then pulled one joint to about 3439 feet where we set our rip plug. All 4 1/2 inch diameter casing was pulled from the hole after plugging was finished. The Berea was covered by the surface casing and no individual plug was needed.
560650035 2013-6-28 0:00: PW No Violations 3.00
588388390 2017-6-20 0:00: FR No Violations 1.00
609115286 2014-2-21 0:00: PW No Violations 0.70
674100211 2015-7-28 0:00: PW No Violations 1.00
72095241 2016-10-11 0:00 PB No Violations 10.00
PL9731 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0560650035 US-OH-126184 2013-06-28 Failure to legibly identify well
0560650035 US-OH-126185 2013-06-28 Well shall be plugged
0560650035 US-OH-126186 2013-06-28 Nonproduction; well shall be plugged or placed in temporary inactive status
0560650035 US-OH-126187 2013-06-28 Statement of annual production not filed

For data sources see[9]

References