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34-115-22900

Well Details

Well ID: 34-115-22900
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Country: United States
State: Ohio
County: Morgan
Municipality: Bloom Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: FORRESTAL
License Status: Producing
License Date: 1982-08-27
Spud Date: 1982-11-23
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1982-11-24
Well Total Depth: 1641.00 ft
Configuration: Vertical
Latitude: 39.750000
Longitude: -81.840000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-08-27 Issued Date 8/27/82 Expired Date Acres 0020000 Tool Type RTA Proposed Formation BEREA Proposed Depth Proposed Drill Depth
Original Spud 1982-11-23 CHG IN FOOT. 11-13-82
Completed 1982-11-24 CHG IN FOOT. 11-13-82
Reached Total Depth 1982-11-24 CHG IN FOOT. 11-13-82
CO 1982-12-07 1177 ENERGY DISTRIBUTORS INC GeoDate 8/27/82
Completion Report Received 1982-12-08 CHG IN FOOT. 11-13-82
Construction Permit Expires 1983-02-15 CHG IN FOOT. 11-13-82
CO 1991-12-11 3071 KINGSTON OIL CORP GeoDate 8/27/82
Change of Owner 2001-01-12 Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC
Change of Owner 2004-03-03 Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC
Change of Owner 2017-10-17 Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-10-17 CHG IN FOOT. 11-13-82

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1491 1510 0
1491 1510 0
2006-09-11 1495 1552 12
1495 1552 12
1491 1510 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 44000 Gal 30000 FRAC;44MG H2O,30M# SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 ENERGY DISTRIBUTORS INC 908.00 0.00 0
1988 KINGSTON OIL CORP 1346.00 0.00 0
1989 KINGSTON OIL CORP 956.00 15.00 365
1990 KINGSTON OIL CORP 1190.00 5.00 365
1991 KINGSTON OIL CORP 611.00 0.00 365
1992 KINGSTON OIL CORP 365.00 4.00 350
1993 KINGSTON OIL CORP 280.00 0.00 350
1994 KINGSTON OIL CORP 267.00 0.00 350
1995 KINGSTON OIL CORP 147.00 0.00 350
1996 KINGSTON OIL CORP 138.00 0.00 350
1997 KINGSTON OIL CORP 198.00 2.00 350
1998 KINGSTON OIL CORP 189.00 0.00 350
1999 KINGSTON OIL CORP 176.00 7.00 0
2000 KINGSTON OIL CORP 158.00 0.00 0
2001 CHEVRON APPALACHIA LLC 187.00 10.00 330
2002 CHEVRON APPALACHIA LLC 307.00 3.00 365
2003 ATLAS NOBLE LLC 432.00 10.00 365
2004 ATLAS NOBLE LLC 248.00 5.00 365
2005 ATLAS NOBLE LLC 239.00 4.00 365
2006 ATLAS NOBLE LLC 196.00 4.00 365
2007 ATLAS NOBLE LLC 165.00 0.00 365
2008 ATLAS NOBLE LLC 111.00 2.00 366
2009 ATLAS NOBLE LLC 99.00 6.00 365
2010 ATLAS NOBLE LLC 176.00 0.00 365
2011 ATLAS NOBLE LLC 100.00 5.00 0
2012 ATLAS NOBLE LLC 81.00 0.00 366
2013 ATLAS NOBLE LLC 114.00 0.00 365
2014 ATLAS NOBLE LLC 12.00 0.00 365
2015 ATLAS NOBLE LLC 72.00 4.00 334
2016 ATLAS NOBLE LLC 24.00 0.00 31
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 ENERGY DISTRIBUTORS INC Brine 14 0
1988 KINGSTON OIL CORP Brine 81 0
1989 KINGSTON OIL CORP Brine 81 365
1990 KINGSTON OIL CORP Brine 82 365
1991 KINGSTON OIL CORP Brine 29 365
1992 KINGSTON OIL CORP Brine 0 350
1993 KINGSTON OIL CORP Brine 0 350
1994 KINGSTON OIL CORP Brine 0 350
1995 KINGSTON OIL CORP Brine 0 350
1996 KINGSTON OIL CORP Brine 10 350
1997 KINGSTON OIL CORP Brine 55 350
1998 KINGSTON OIL CORP Brine 35 350
1999 KINGSTON OIL CORP Brine 28
2000 KINGSTON OIL CORP Brine 16
2001 CHEVRON APPALACHIA LLC Brine 0 330
2002 CHEVRON APPALACHIA LLC Brine 73 365
2003 ATLAS NOBLE LLC Brine 0 365
2004 ATLAS NOBLE LLC Brine 31 365
2005 ATLAS NOBLE LLC Brine 46 365
2006 ATLAS NOBLE LLC Brine 40 365
2007 ATLAS NOBLE LLC Brine 36 365
2008 ATLAS NOBLE LLC Brine 26 366
2009 ATLAS NOBLE LLC Brine 31 365
2010 ATLAS NOBLE LLC Brine 9 365
2011 ATLAS NOBLE LLC Brine 0
2012 ATLAS NOBLE LLC Brine 0 366
2013 ATLAS NOBLE LLC Brine 55 365
2014 ATLAS NOBLE LLC Brine 77 365
2015 ATLAS NOBLE LLC Brine 82 334
2016 ATLAS NOBLE LLC Brine 0 31
2017 ATLAS NOBLE LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1038634367 2016-11-21 0:00 PW No Violations 1.00
-1333493105 2016-4-4 0:00:0 PW No Violations 1.00
-992852343 2016-5-17 0:00: PW No Violations 1.00
0000PL9905 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0024577783 2016-08-24 Production Wells No Violations I returned to this well to do a follow-up on the compliance notice issued on this well. The well at this time still has the production valves shut at the well head making the well incapable of any production. The well is still currently still in violation. I took photos of the well today during my inspection.
0141984901 2015-06-23 Production Wells Violations Noted During the field inspection of this well I found the well does not appear to be in production. The company reported 12MCF for the production of this well but that is shared between 7 wells on this farm. The production reported does not meet the requirements by the state. Plugging of this well will be required within 180days.
0992852343 2016-05-17 Production Wells No Violations Upon my inspection today I found the well to still be idle at this time. No resolution to the issues on this well. Spoke with Supervisor Dan Goins and he informed me that he spoke with Atlas and they had made an agreement to plug at least 5 wells a year.
1038634367 2016-11-21 Production Wells No Violations The inspection today revealed that this well is still incapable of production at this time. The valves on the well head are still closed in on the production lines. There has been no resolution to the issues on this well.
1333493105 2016-04-04 Production Wells No Violations Upon my follow-up today I found this well to still have its valves closed and not producing. I called Pat Irvin from Atlas and he informed me they do plan on plugging the wells but, the company they use for cement has been having issues with money. They put the rigs in the Atlass yard and will be plugging as soon as they get the money to afford it. There has been no resolution to the issue.
141984901 2015-6-23 0:00: PW No Violations 1.00
1452174808 2016-01-06 Production Wells No Violations Upon my inspection today I found this well to be equipped with a pump jack on a 4 1/2 inch well head with 2 inch tubing and two 2 inch ball valves. The valves on the two inch tubing are open and the pump jack seems to have had some work done on it recently. I spoke with Atlas on the phone and he informed me that this well was open and the rest on the farm were currently closed. They were alternating the wells open during the year so they could see which were producing and which were not so they could plug accordingly. The production reports on all 7 wells is still very low and not enough for commercial use. Due to this I am leaving the compliance open on this well. This well is one of 7 that is connected to a single tank battery equipped with a separator and one 100 bbl tank. I informed Atlas that the notices would remain open until they had a plan and would call them back in 30 days for any updates they have on these wells.
1470759083 2016-08-09 Production Wells No Violations The inspection revealed the well to have 7 inch diameter casing with 4 1/2 inch diameter well head in the hole. There are 2 inch diameter production lines coming from the well. There is a pumping unit seated on the well head and the rods are in the hole. The valves on the 2 inch diameter lines are all open on the well head and the well is capable of production. All issues have been resolved on this well.
1820512775 2017-10-26 Production Wells No Violations I returned to this well today to do a follow-up inspection on it. The violation has been resolved. The production valves on the wellhead are now open and the well appears to be capable of production. There are no violations at this time.
24577783 2016-8-24 0:00: PW No Violations 1.00
PL9905 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0141984901 US-OH-112271 2017-10-30 NONE Well shall be plugged

For data sources see[9]

References