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Well ID: 34-115-22593 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: THOMPSON | |
License Status: Producing | |
License Date: 1982-06-18 | |
Spud Date: 1982-07-19 | |
Spud Drilling Contractor: DUSTY DRILLING | |
Final Drill Date: 1982-07-20 | |
Well Total Depth: 1397.00 ft | |
Configuration: Vertical | |
Latitude: 39.690000 | |
Longitude: -81.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-06-18 | Issued Date 6/18/82 Expired Date 12/15/82 Acres 0020000 Tool Type CT Proposed Formation BEREA Proposed Depth 01397 Proposed Drill Depth 01397 |
Original Spud | 1982-07-19 | FDT=GRAY |
Completed | 1982-07-20 | FDT=GRAY |
Reached Total Depth | 1982-07-20 | FDT=GRAY |
CO | 1982-08-09 | 1868 DUSTY DRILL & PRO CORP GeoDate 6/18/82 |
Construction Permit Expires | 1982-12-15 | FDT=GRAY |
Completion Report Received | 1982-12-16 | FDT=GRAY |
Change of Owner | 2003-09-24 | Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP |
Change of Owner | 2007-07-11 | Operator changed from 2867, DNL OIL CORP to 8227, DEEP RESOURCES LLC |
Change of Owner | 2011-10-13 | Operator changed from 8227, DEEP RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-02-15 | FDT=GRAY |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1333 | 1335 | 1 |
1333 | 1335 | 1 | |
1333 | 1335 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 700 Bbl | 14000 | FRAC;700BBL H2O,14M# SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DUSTY DRILLING & PRODUCING COR | 668.00 | 299.00 | 0 |
1985 | DUSTY DRILLING & PRODUCING COR | 764.00 | 230.00 | 358 |
1986 | DUSTY DRILLING & PRODUCING COR | 1077.00 | 198.00 | 365 |
1987 | DUSTY DRILLING & PRODUCING COR | 944.00 | 151.00 | 365 |
1988 | DUSTY DRILLING & PRODUCING COR | 676.00 | 117.00 | 358 |
1989 | DUSTY DRILLING & PRODUCING COR | 650.00 | 133.00 | 358 |
1990 | DUSTY DRILLING & PRODUCING COR | 510.00 | 112.00 | 351 |
1991 | DUSTY DRILLING & PRODUCING COR | 603.00 | 103.00 | 365 |
1992 | DUSTY DRILLING & PRODUCING COR | 718.00 | 88.00 | 365 |
1994 | DUSTY DRILLING & PRODUCING COR | 717.00 | 46.00 | 365 |
1995 | DUSTY DRILLING & PRODUCING COR | 622.00 | 55.00 | 365 |
2004 | DNL OIL CORP | 337.00 | 78.00 | 275 |
2005 | DNL OIL CORP | 368.00 | 118.00 | 365 |
2006 | DNL OIL CORP | 392.00 | 120.00 | 365 |
2007 | DNL OIL CORP | 295.00 | 51.00 | 183 |
2008 | DEEP RESOURCES LLC | 373.00 | 6.00 | 365 |
2009 | DEEP RESOURCES LLC | 456.00 | 63.00 | 365 |
2010 | DEEP RESOURCES LLC | 317.00 | 71.00 | 365 |
2011 | M & R INVESTMENTS OHIO LLC | 226.00 | 0.00 | 365 |
2012 | M & R INVESTMENTS OHIO LLC | 0.00 | 49.00 | 366 |
2013 | M & R INVESTMENTS OHIO LLC | 76.00 | 146.00 | 365 |
2014 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
2015 | M & R INVESTMENTS OHIO LLC | 10.00 | 0.00 | 365 |
2016 | M & R INVESTMENTS OHIO LLC | 10.00 | 0.00 | 0 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1575402813 | 2013-10-21 0:00 | PW | No Violations | 1.50 |
0000PL9977 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1378753797 | 2013-09-09 | Production Wells | No Violations | Compliance Action Follow-up 1453278961: Andy posted identification and threw down some adsorbent material however there is still minor contamination around wellhead. He said he will take care of it next week. |
1396022667 | 2014-03-28 | Production Wells | No Violations | Compliance Action Follow-up 1453278961:Contamination has been removed from wellhead and Andy has repaired the stuffing box. Well is in compliance. There are no issues to report at this time. |
1453278961 | 2013-02-12 | Production Wells | Violations Noted | Well is capable of producing. The stuffing box is leaking and there is an area of contamination about 3 x 3 around wellhead. There is no identification at wellhead. There is a tank battery up on County Road 3, however identification is not legible. Operator needs to repair leaking equipment at well site and remove contamination around the wellhead. Operator needs to post correct legible IDs. 3/20/2013: ID has been posted at tank battery. Andy just got the ID stickers and will post IDs at all of the wellheads today. |
1575402813 | 2013-10-21 | Production Wells | No Violations | Compliance Action Follow-up 1453278961: There has been no resolution to any of the issues. I called Andy and Jody Jasper to notify them of the contamination. |
2061908436 | 2014-03-04 | Production Wells | No Violations | Compliance Action Follow-up 1453278961: The stuffing box still appears to have issues and there is still some minor contamination around wellhead, however the ground is hard and covered with snow. I will return in a few weeks when it is warmer to check the extent of cleanup. |
PL9977 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1453278961 | US-OH-113106 | 2014-10-10 | Well operation causing pollution and contamination | |
1453278961 | US-OH-113107 | 2014-10-10 | Failure to legibly identify well | |
1453278961 | US-OH-113108 | 2014-10-10 | Equipment pressure rated below operating pressure |
For data sources see[9]