X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-115-21571

Well Details

Well ID: 34-115-21571
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Jackson Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: ALLEN CLAYTON ETAL
License Status: Producing
License Date: 1988-05-19
Spud Date: 1977-04-29
Spud Drilling Contractor:
Final Drill Date: 1977-05-19
Well Total Depth: 1860.00 ft
Configuration: Vertical
Latitude: 39.650000
Longitude: -81.580000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-04-29
CO 1977-05-03 1487 GEOSTRATA INC GeoDate 5/3/77
Completed 1977-05-19
Reached Total Depth 1977-05-19
CO 1988-05-19 1487 GEOSTRATA INC GeoDate 5/19/88
Unknown 1988-05-19 Issued Date 5/19/88 Expired Date 5/19/89 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1989-05-19
CO 1995-05-19 4540 PEOPLES PETROLEUM CORP. GeoDate 5/19/88
CO 1995-05-30 2070 HALWELL COMPANY GeoDate 5/19/88
Last Compliance Report 2013-08-26
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1762 1770 9
1762 1770 9
1762 1770 9

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 42000 Gal 21000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RESOURCE PRODUCTION INC 2943.00 472.00 0
1985 RESOURCE PRODUCTION INC 932.00 0.00 0
1986 RESOURCE PRODUCTION INC 2522.00 67.00 365
1987 RESOURCE PRODUCTION INC 384.00 0.00 365
1995 STONEBRIDGE OPERATING CO LLC 0.00 0.00 14
1996 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1997 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1998 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2000 STONEBRIDGE OPERATING CO LLC 0.00 0.00 366
2001 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2002 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2003 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2004 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2005 STONEBRIDGE OPERATING CO LLC 19.00 0.00 0
2006 STONEBRIDGE OPERATING CO LLC 33.00 0.00 0
2007 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2009 STONEBRIDGE OPERATING CO LLC 33.00 0.00 0
2010 STONEBRIDGE OPERATING CO LLC 50.00 0.00 70
2011 STONEBRIDGE OPERATING CO LLC 78.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 124.00 0.00 357
2013 STONEBRIDGE OPERATING CO LLC 82.00 0.00 365
2014 STONEBRIDGE OPERATING CO LLC 0.00 0.00 280
2015 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2017 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2018 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RESOURCE PRODUCTION INC Brine 300 0
1985 RESOURCE PRODUCTION INC Brine 2175 0
1986 RESOURCE PRODUCTION INC Brine 5365 365
1987 RESOURCE PRODUCTION INC Brine 400 365
1995 STONEBRIDGE OPERATING CO LLC Brine 0 14
1996 STONEBRIDGE OPERATING CO LLC Brine 0 0
1997 STONEBRIDGE OPERATING CO LLC Brine 0 0
1998 STONEBRIDGE OPERATING CO LLC Brine 0 0
2000 STONEBRIDGE OPERATING CO LLC Brine 0 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 0
2002 STONEBRIDGE OPERATING CO LLC Brine 0 0
2003 STONEBRIDGE OPERATING CO LLC Brine 0 0
2004 STONEBRIDGE OPERATING CO LLC Brine 0 0
2005 STONEBRIDGE OPERATING CO LLC Brine 0 0
2006 STONEBRIDGE OPERATING CO LLC Brine 0 0
2007 STONEBRIDGE OPERATING CO LLC Brine 0 0
2009 STONEBRIDGE OPERATING CO LLC Brine 0 0
2010 STONEBRIDGE OPERATING CO LLC Brine 0 70
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 357
2013 STONEBRIDGE OPERATING CO LLC Brine 42 365
2014 STONEBRIDGE OPERATING CO LLC Brine 0 280
2015 STONEBRIDGE OPERATING CO LLC Brine 0 0
2016 STONEBRIDGE OPERATING CO LLC Brine 0 0
2017 STONEBRIDGE OPERATING CO LLC Brine 0 0
2018 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1627311511 2019-9-13 0:00: PW No Violations 0.80
-1661446098 2019-11-27 0:00 PW No Violations 1.00
-2002480167 2019-2-6 0:00:0 PW No Violations 1.50
0117539260 2013-03-05 Production Wells Violations Noted Upon inspection, as part of a landowner complaint, I found the wellhead with all valves shut and the steel production line running from the wellhead to the tank battery disconnected just inside the dike. There is another steel production line that runs just adjacent to the wellhead and also leads to the tank battery where it is disconnected inside the dike. The separator has been removed from inside the dike. The two orange and black plastic lines, which are attached to the tank and run towards the wellhead have been disconnected, so there is no way this well is producing. There is an access road just off of Twp Rd 76 where there are several meters. Two are labeled for Northwood and Artex. The 3rd isnt labeled but all three have charts showing production. There is a gas line with a flow meter that has an identification listed as the Clayton Allen 2A/#1571. I followed these lines and they run in the opposite direction from the actual Clayton Allen 2A. ID is incorrect and production has been consistently reported for a well that is not capable of producing. Operator needs to change the ID to the correct well. Operator must make well capable of production within 30 days; or plugging is required in 30 days. Failure to comply may result in forfeiture of bond. 3/8/2013: John Schneider with Stonebridge called and said he would get ID taken care of and he would look into idle well.
0701771344 2008-03-24 Annular Disposal No Violations A.D. not hooked up, well is equipped with 4.5 casing and tubing&rods and 2-100 bbl tanks,well is shut in at present time called company and inquired about status they claim sales line needs to be repaired.
104885418 2019-10-28 0:00 PW No Violations 0.20
117539260 2013-3-5 0:00:0 PW No Violations 3.50
1323266980 2011-12-06 Production Wells No Violations Inspection this day due to complaint by landowner, Myron Allen, that well is not producing. He has not received royalties in years, believes that the operator is dumping brine and that the identification signs and meter are on the wrong sales line (believes they are for the D. Morris #7). My inspection revealed the pumping unit has been removed and the well is equipped with rods and tubing. There is no identification posted at the well or the tank which is located on a small hill beside the well. There is a large tree growing through the ladder on the tank. Down along the road I found a 2 line with a small flowmeter registering zero and labeled as the Allen well. This line is coming from the north, so it possibly could be for the D. Morris well. The Allen well is to the south and the valves are all shut. There are numerous plastic lines in area and cant tell where any of them are going or if they are in use. Annual production is being turned in for Allen well but it is not producing now (well valves are shut) and all indications are that it has not produced in years. Inspection from 2008 reports that well is shut in due to sales line problems. DNR records show the operator reported 50 mcf for 2010, 33 mcf for 2009. I will not write a Notice of Violation until requested. Pictures taken. I found no evidence of brine dumping. There is a small plastic tank along road that belongs to Northwood, along with master meters for Northwood and Artex. There is no indication where gas from Stonebridge is being metered.
1324039707 2011-12-14 Production Wells No Violations I re-inspected this well after getting word that the Dominion pipeline is now back in operation. I checked the small flowmeter below well identified as the Clayton Allen meter and it was still registering zero gas. If it had been metering the Don Morris well, as landowner contends, there should have been some gas moving through it. All evidence still shows this well is idle and not producing.
1365433254 2013-04-08 Production Wells No Violations Compliance Action Follow-up 117539260: Landowner informed me that Stonebridge had put a pumping unit on the well and had not used a culvert crossing the stream at the access road. Upon inspection, I found the stream had been cut off leaving a pool of water in middle of access road. They had not corrected the stream flow. I found the area completely cleaned up and an ID posted at the tank battery. There was a pumping unit hooked up to the well with new line valves. The tank was equiped with new valves and bull plugs. The 2 tubing was shut in but the 4.5 valve was open on one side which ran to tank and the other side was hooked to a new 2 line which ran back down to access road where it is tied into transmission line. It was shut in at the meter location as well as the access road. The meter has no chart. Rob Nutter arrived and said he would open the stream back up and was going to put a chart on the meter. He was going up to inspect the work and will call me once well is in production.
1365775148 2013-04-12 Administrative Inspection No Violations Compliance Action Follow-up 117539260: I called Rob Nutter with Stonebridge and he stated he put 15 gallons of solvent down hole to help clean wellbore. I talked again with him this morning and he said they are going to bring a service rig out to pull out and replace the downhole pump. He believes it isnt working properly however they have recovered some oil and brine and have about 18 pounds of pressure. He will call me beginning of next week. 4/24/2013: I bumped into Rob in the field and he said a service rig was on location today fixing downhole pumpjack issues. He will call me when the well is back in production.
1698465883 2013-06-11 Production Wells No Violations Well is now in compliance. The well is currently producing oil and water from the formation. Rob Nutter stated that they need to relieve the formation of this fluid in order to increase the gas pressure. The meter at the wellhead is not currently pressurized for reporting gas production. The oil and water are moving from the wellhead to the tank in the dike.
1779750031 2020-4-15 0:00: TD No Violations 0.50
2002480167 2019-02-06 Production Wells Violations Noted I was on location today to follow-up on a complaint by landowner Myron Allen about this well not being in production and the production lines on his property. At the time of my inspection I found the well to appear idle and not have been producing. The last production reported on this well was in 2013. The well owner/operator shall submit a written plugging schedule to (Justin Smith) at (5880 Memory Rd Zanesville Oh, 43701) within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
2061966359 2020-5-29 0:00: PW No Violations 1.00
701771344 2008-3-24 0:00: AD No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0117539260 US-OH-104646 2013-06-11 Forfeiture of bond
0117539260 US-OH-104647 2013-06-11 Failure to legibly identify well
0117539260 US-OH-104648 2013-06-11 Well shall be plugged
0117539260 US-OH-104649 2013-06-11 Nonproduction; well shall be plugged or placed in temporary inactive status
2002480167 US-OH-120326 2019-02-11 NONE Well shall be plugged

For data sources see[9]

References