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Well ID: 34-115-21237 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Center Township | |
Operator Name: POORBOY EXPLORATION LLC | |
Well Pad ID: | |
Farm/Lease Name: LAWRENCE CECIL | |
License Status: Producing | |
License Date: 1971-10-28 | |
Spud Date: 1971-12-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-04-05 | |
Well Total Depth: 1567.00 ft | |
Configuration: Vertical | |
Latitude: 39.630000 | |
Longitude: -81.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1971-10-28 | 594 RMB CORPORATION GeoDate 10/28/71 |
Original Spud | 1971-12-12 | RE-TYPED 2-6-88 |
Completed | 1972-04-05 | RE-TYPED 2-6-88 |
Reached Total Depth | 1972-04-05 | RE-TYPED 2-6-88 |
Change of Owner | 1998-12-04 | Operator changed from 594, RMB CORPORATION to 4350, CENTURY WELL SERVICE |
Change of Owner | 2007-10-03 | Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY |
Change of Owner | 2008-02-14 | Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC |
Change of Owner | 2010-12-29 | Operator changed from 8312, BROAD STREET SERV LLC to 8740, DART ENERGY LLC |
Change of Owner | 2013-08-01 | Operator changed from 8740, DART ENERGY LLC to 9156, POORBOY EXPLORATION INC |
Record Last Modified | 2013-10-03 | RE-TYPED 2-6-88 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 500 Bbl | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1999 | CENTURY WELL SERVICE | 73.00 | 0.00 | 365 |
2000 | CENTURY WELL SERVICE | 52.00 | 11.00 | 365 |
2001 | CENTURY WELL SERVICE | 52.00 | 11.00 | 365 |
2002 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2003 | CENTURY WELL SERVICE | 28.00 | 0.00 | 365 |
2004 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2005 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2006 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2007 | BROAD STREET SERV LLC | 10.00 | 0.00 | 365 |
2008 | BROAD STREET SERV LLC | 0.00 | 0.00 | 0 |
2009 | BROAD STREET SERV LLC | 367.00 | 0.00 | 365 |
2010 | BROAD STREET SERV LLC | 71.00 | 0.00 | 365 |
2011 | DART ENERGY LLC | 411.00 | 63.00 | 123 |
2012 | DART ENERGY LLC | 298.00 | 0.00 | 300 |
2013 | DART ENERGY LLC | 0.00 | 0.00 | 0 |
2014 | POORBOY EXPLORATION LLC | 500.00 | 25.00 | 0 |
2016 | POORBOY EXPLORATION LLC | 534.00 | 0.00 | 150 |
2017 | POORBOY EXPLORATION LLC | 109.00 | 0.00 | 360 |
2018 | POORBOY EXPLORATION LLC | 148.00 | 0.00 | 360 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1999 | CENTURY WELL SERVICE | Brine | 450 | 365 |
2000 | CENTURY WELL SERVICE | Brine | 91 | 365 |
2001 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2002 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2003 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2004 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2005 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2006 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2007 | BROAD STREET SERV LLC | Brine | 0 | 365 |
2008 | BROAD STREET SERV LLC | Brine | 0 | 0 |
2009 | BROAD STREET SERV LLC | Brine | 384 | 365 |
2010 | BROAD STREET SERV LLC | Brine | 50 | 365 |
2011 | DART ENERGY LLC | Brine | 215 | 123 |
2012 | DART ENERGY LLC | Brine | 75 | 300 |
2013 | DART ENERGY LLC | Brine | 0 | 0 |
2014 | POORBOY EXPLORATION LLC | Brine | 0 | 0 |
2016 | POORBOY EXPLORATION LLC | Brine | 0 | 150 |
2017 | POORBOY EXPLORATION LLC | Brine | 0 | 360 |
2018 | POORBOY EXPLORATION LLC | Brine | 0 | 360 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-240242819 | 2017-1-23 0:00: | PW | No Violations | 1.00 |
0240242819 | 2017-01-23 | Production Wells | No Violations | The inspection this day revealed that this well is equipped with a pumping unit, a 4 1/2 inch diameter wellhead, 2 inch diameter steel production lines, and 1 1/2 inch diameter production tubing. The pumping unit arm is currently stuck in the down position at the time of inspection. The valves on the wellhead are currently open at the time of inspection. The tank battery is right by the road and consists of two (2) 100 barrel steel tanks, a meter box with a current chart in it with the date of 1/18/17, and a vertical separator. Fluid could be heard going through the lines into the tanks at the time of inspection. There is proper identification at the time of inspection but is beginning to weather away. There are no issues to report at this time and the well is in production at the time of inspection. |
1193421338 | 2007-10-25 | Production Wells | Violations Noted | Complaint received at Cambridge Office 10/22/07@9:15 am from Mrs.Larwence of idle well on property,upon inspecting site found well to be idle.
Well is equipped with pump jack tubing and rods no motor on pumping unit and all valves on wellhead were closed on the day of my inspection, also 2-100 bbl tanks on site to close to highway,last production reported on well was in 2003.Photos taken of site(2). |
1574131798 | 2009-03-20 | Production Wells | Violations Noted | Well has been placed back into production resolving previous Notice of Violation. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1193421338 | US-OH-105110 | 2007-10-26 | Failure to legibly identify well | |
1193421338 | US-OH-105111 | 2007-10-26 | Violation of tank spacing requirements | |
1193421338 | US-OH-105112 | 2007-10-26 | Well shall be plugged | |
1574131798 | US-OH-115388 | 2007-10-26 | Failure to legibly identify well | |
1574131798 | US-OH-115389 | 2007-10-26 | Violation of tank spacing requirements | |
1574131798 | US-OH-115390 | 2007-10-26 | Well shall be plugged |
For data sources see[8]