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34-111-24368

Well Details

Well ID: 34-111-24368
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Country: United States
State: Ohio
County: Monroe
Municipality: Center Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: WENDLING-HAYES
License Status: Producing
License Date: 2013-02-20
Spud Date: 2013-03-15
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC
Final Drill Date: 2013-03-06
Well Total Depth: 2305.00 ft
Configuration: Vertical
Latitude: 39.790000
Longitude: -81.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-02-20 Proposed Formations:BEREA/30 FOOT/GORDON, Issued Date:2/20/2013, Expired Date:2/20/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2013-03-06
Correction to Well 2013-03-22 PROPOSED TOTAL DEPTH CHANGED TO 2940 FT.
Completion Report Received 2013-06-04
Construction Permit Expires 2015-02-20
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-06-05 2140 2158 19
2140 2158 19
2140 2158 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-04-17 H2O 0 75000 Gal 0 Universal Well Services Inc. The said well was stimulated with fresh water only. Well was perferated and acid treaded on a prior date with 19-shots from 2140' to 2158'.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 BECK ENERGY CORPORATION 203.00 0.00 365
2015 BECK ENERGY CORPORATION 197.00 0.00 365
2016 BECK ENERGY CORPORATION 148.00 0.00 365
2017 BECK ENERGY CORPORATION 132.00 6.00 365
2018 BECK ENERGY CORPORATION 84.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 BECK ENERGY CORPORATION Brine 105 365
2015 BECK ENERGY CORPORATION Brine 0 365
2016 BECK ENERGY CORPORATION Brine 0 365
2017 BECK ENERGY CORPORATION Brine 79 365
2018 BECK ENERGY CORPORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-335907627 2013-3-14 0:00: DD No Violations
-704109582 2013-4-2 0:00:0 DD No Violations 2.00
-96337424 2013-3-20 0:00: DD No Violations
0096337424 2013-03-20 Drill / Deepen / Reopen No Violations Inspector on site @ 8:30 am to pressure test the surface cement casing remedial work squeeze job. Cement was tagged inside the casing at 270 with the perforations @ 276 to 280, at 282 we fell out of the cement and ran 3 Kellys past that point and circulated the hole clean. We then pulled the drill string out of the hole and put the cement reducing swage back on the 7 and pressure tested it to 350 psi with no recorded loss or communication to the annular side of the surface pipe. Inspector approved the remedial work as complete.
0335907627 2013-03-14 Drill / Deepen / Reopen No Violations A notification phone call was received by Kerry Brown from Monroe drilling asking permission to start the drill site excavation. I responded to the site and after reviewing the site and asking Kerry to try and stockpile and save as much top soil as possible permission was granted to excavate the site. Kerry stated He would be building Becks drill sites and would practice good site construction management trying to preserve the topsoil for reclamation purposes.
0533223198 2013-07-30 Preliminary Restoration No Violations Inspection of the well site found the drilling pits filled and the well in production with 4.5 production casing and 1.5 tubing and pumping rods and the production valves open and the well being produced by the means of a pumping unit. 2-100 barrel production tanks are present in a established dike along with a mechanical separator and production gas sales meter. Inspector will note that notification was made to Beck energy that final grade work still needs done around the well site as well as better vegetation needing established.
0704109582 2013-04-02 Drill / Deepen / Reopen No Violations Status check inspection of the current drilling progress. Notification was received by Becky Sims that the well pressure has been controlled and that they were running back into the hole with the drill string on fluid to complete the drilling of the well bore.
1363376365 2013-03-15 Drill / Deepen / Reopen No Violations Inspector on location to set the 9.625 conductor pipe and upon arrival I noticed they only had 64 of pipe on location. After speaking with the drilling contractor I made them aware that they did not have the minimum of 100 of conductor pipe as the permit required. The hole depth was then drilled to 140 and 130 of conductor was set and cemented back to surface. Inspector on site 6 hrs.
1363695647 2013-03-19 Drill / Deepen / Reopen No Violations Inspector on site for a 10PM callout on 03/18/1013 for a 7 surface job, Upon arrival the rig was still pulling drill pipe and not ready, 888 of 7 surface was set in 920 of borehole, The cement did not circulate and the plug stopped short of landing, The cementers and myself suspect the 1st red rock formation collapsed @ 625 which is where the plug sat down. The surface will be grouted on the long string cement job. Inspector off location 2 Am.
1363720895 2013-03-19 Drill / Deepen / Reopen No Violations On site status check on Surface job from the following evening found that once they run in the hole with the drill string the top of the cement is at 480 inside of the 7 surface pipe which is 888 in total depth. The cement will be drilled out within 40 of the casing shoe and the surface casing will be bond logged. Once we see the top of cement a remedial plan will be put into place if needed. Inspector will return @ 6PM to witness the bond log.
1364314542 2013-03-26 Drill / Deepen / Reopen No Violations Status up date of the drilling progress found the current drilling depth of 2230. The well has pressured up and the drilling company has pulled the drill string out of the hole and has a swage on the 7 surface and well head control in place. They have tried to kill the well with 10# mud unsuccessfully. With plans to mix heavier mud and try to kill the well with a pump truck.
1364506744 2013-03-28 Drill / Deepen / Reopen No Violations On this day I was on site with MRI 3 Pat Shreve to evaluate the well bore that has occurred a high amount of gas pressure during the drilling process. 3rd party fluid and high pressure pump contractors have been brought in to try and kill the well, but due to the unusual circumstances of the drill string being pulled out of the hole and a reducing swage being put on the 7 surface casing with a low pressure nipple and valve, the decision was made to put the well in line and sell the well down until proper pressure rated equipment can be installed.
1366238325 2013-04-17 Drill / Deepen / Reopen No Violations On this day I observed Universal Well Services- Completion Services Trucks traveling in the direction of the location. After attending to other business I traveled to the said well site and observed the stimulation process in progress. I observed and photographed the operation in progress then had a conversation on site with Ray Beck the company owner in regards to the no notification being made to me about the up and coming completion work on the well. Mr. Beck said His assistant Becky Sims had been very sick and most likely forgot to call me. I discussed the notification requirements per their permit conditions and advised Mr. Beck He must notify me as the permit required. I observed the complete stimulation process on this day.
2036419706 2014-07-31 Preliminary Restoration No Violations Preliminary Restoration status check inspection found the well site restoration meets ORC 1509.072 with proper vegetation established on location and the following equipment present at the well head 4.5 production casing- 1.5 tubing and pumping rods with the production valves open and the well set up to be produced by the means of a pumping unit, at the production fluid storage area 2-100 barrel production tanks are presen along with a mechanical separator and gas sales meter with a current sales chart all located in an established dike area with proper well identification posted.
533223198 2013-7-30 0:00: PL No Violations 2.00

For data sources see[9]

References